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SERVICEMAN'S LOG
One repair leads to another
Dave Thompson
There are people out there who obviously love their older radios and
stereos. Since word got around that I can repair these devices, quite a
few have come through the workshop. While most repairs are simple,
there have been some that required a good bit of thinking.
Most of these type of repairs don’t
warrant much attention due to being
relatively simple fixes; replace the
odd component here, or reflow dry
joints there, and away we go for another 40 years.
But there were a couple of recent
fixes of which I have been quite proud.
While they didn’t require me to do
enough research to earn a doctorate,
I did have to do some searching and
thinking to come up with a solution.
The first was an amplifier which is
no stranger to my workshop. This is
one of those jobs that proves the old engineering maxim: as soon as you mess
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with something that has been working
well for years, it will develop a heap
of problems (perhaps a corollary to “if
it ain’t broke, don’t fix it”?)
There’s probably a rational explanation for this phenomenon. It often
happens that you take the case off an
old amplifier just to check it over and
huff the cobwebs out, then a month
later the caps fail, and the transistors
or valves need replacing.
Perhaps I disturbed something with
my low-pressure air, or the journey to
Australia’s electronics magazine
the workshop shook up those old solder joints. Or maybe I just displeased
the audio gods by intruding on sacred
ground!
Mechanics often claim that a car
engine is never the same once the
head has been off, and I’m convinced
there are many parallels in electronics. Whatever the cause, there is always the sneaking suspicion that I’ve
done something to cause a rift in the
space-time continuum, and now I’m
paying the price.
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Welcome back, old friend
This lump of a stereo amplifier is
one of those old 70s jobs that appear
to be milled out of a solid billet of
brushed steel, with a couple of polished wooden caps slapped on each
end of the case.
The power transformer alone is
heavier than most modern audio systems, including their speakers! Everything inside is heavy-duty, and the
connections are wire-wrapped, a construction method peculiar to that era.
While wrapping is an excellent
way of connecting individual circuit
boards together, and the cabling has
obviously stood the test of time, it is
a royal pain in the woofer to work on.
This is especially true if I need to uninstall and reinstall the board several
times for testing purposes – re-wrapping it each time is highly impractical.
While I still possess a wire-wrapping tool and a few spools of wrapping wire, purchased circa 1975, I
haven’t used them for many years.
In cases like this, unless the custom-
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er specifically wants to retain the
vintage authenticity of the device, I
replace wrapped joints with soldered
connections.
While I know my way around this
Pioneer SX-series amp, having repaired it before, I think I was the first
person to take the covers off. Initially, the problem was that the speaker
protection relay was not kicking in
at switch-on, and if it did, it would
randomly drop out. I documented
that repair in the February 2020 issue
(siliconchip.com.au/Article/12339).
Now I’m wondering if by opening it
up I somehow jinxed it, because here
it is again less than a year later with
a different fault. I knew I shouldn’t
have disturbed the gremlins slumbering within its circuitry...
The customer reported that, while
using it, it made some loud static and
clicking and popping noises, then the
amp fell silent. The panel lights still
glow, but there is no action from the
speaker-protection circuit and no other
signs of life.
At first, I thought my previous repair might have failed, but I removed
the protection board and relay and inspected and tested them; all appeared
Australia’s electronics magazine
Items Covered This Month
•
•
•
It’s never as easy as it seems
The water-logged electric
toothbrush
Fixing substandard industrial
machinery
*Dave Thompson runs PC Anytime
in Christchurch, NZ.
Website: www.pcanytime.co.nz
Email: dave<at>pcanytime.co.nz
OK. This is where the now-soldered
interconnecting wiring came in handy
– if I had re-wrapped the boards back
in, it would have made removing them
again that much more work.
And though there was some slack
left in the factory wiring, wrapping
uses up a couple more centimetres of
wire length each time, so I would have
had to replace all the wires. Instead, I
could just desolder it, then reconnect
everything when I was done.
The power supply seemed to be the
next place to check. Fortunately, the
circuit diagram is freely available online, and I had already downloaded it.
November 2020 65
This made things a whole lot easier.
The annotation on the schematic is also excellent, with test points
and current and voltage values clearly marked. With my trusty (and still
working!) analog multimeter – after
last month’s shenanigans – I rang out
the various outputs on the power supply board and found three of the nine
listed were well out of spec.
As mentioned earlier, the power
supply is a heavy-duty unit and delivers a range of voltages from 5.4V to
±51.5V DC, as well as 7.5V AC. I measured around ±14V on the nominally
±51.5V lines, and zero on two other
points, which both should have been
+13.5V. I knew I wouldn’t get any joy
without these voltages present and
fully accounted for.
In the last repair, I replaced all the
electrolytic capacitors on this board,
and a couple of the power transistors.
However, there were still about a dozen smaller transistors I hadn’t tested.
Looking through the circuit diagram,
it was apparent that I was going to at
least have to remove some of those in
the part of the circuit responsible for
these sub-par readings.
Pulling them out is as easy as using a
solder-sucker and a hot soldering iron.
Unhealthy though it might be, I love
the smell of that old solder burning
– it reminds me of watching my dad
working in his workshop.
I found several open-circuit transistors, or more accurately, my Peak
Semiconductor Analyser found them.
I know that I could have used my multimeter to discover them, but I have an
analyser, so I use it.
Amplifiers of this era often used
proprietary components, or possibly transistors and diodes that were
manufactured at the time in relatively
small batches and ended up not being used in much else. In this case,
the part numbers weren’t familiar, so
I hit the web and discovered an abundance of forum posts regarding the
same problem.
After some research, I discovered
that these transistors aren’t overly
specialised, and audio purists derided several as being too noisy for use
in amplifier circuits anyway.
Editor’s note: that probably doesn’t
matter if they’re in the power supply,
unless the audio circuitry is particularly poorly designed.
Luckily, there were recommendations for substitute transistors that
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Australia’s electronics magazine
would offer significantly quieter performance. Many of these types are
still widely available and inexpensive.
While I had some on hand, my supply
of new old stock (NOS) components
is dwindling. So I decided just to buy
what I needed new from element14
and Digi-key.
After receiving the parts, I replaced
all the transistors in that section of the
supply. After re-soldering the board in,
but without hooking up the outputs
yet, I powered it on and measured the
output voltages. The numbers were
better, but still way off, so something
else was clearly wrong.
It wasn’t that easy
Referring to the circuit diagram, I
measured as many of the resistors and
caps as I could in-situ, in case one had
failed. While not an ideal method, the
figures on my LCR meter were within
tolerance. That left the diodes. This
board has 12, and most are straightforward silicon varieties, with the
only difference being their currenthandling characteristics. Two of the
diodes are zeners, one rated at 13V
and one at 14V, 500mW.
I couldn’t measure them properly
in-circuit, so I removed them and tested them with my analyser. Both were
open-circuit. I replaced them with
suitable parts from my own stocks and
powered the amp up again; this time, I
had voltage outputs that, while a little
high, were within 10% of stated values.
After connecting the power supply
board outputs, I switched the amp on,
and after a few seconds the speakerprotection relay kicked in – an excellent sign!
I ran the amp on my workbench at
half-volume for 24 hours and periodically checked the voltages and component temperatures on the supply
board. All remained normal, though
as expected, a couple of fibre-sleeved
load resistors got warm.
I then cycled the power on and off
around 20 times within an hour, and
the relay kicked in every time. I reassembled everything, re-soldering any
connections that were a bit temporary and buttoned it all back up. The
customer picked it up and hopefully
that’s the last I see of this behemoth
for a while!
The radio repair
The second repair came by way of
an enquiry from a reader; he had an
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older General Electric Superadio 3 radio that had started drifting off-station.
The radio was usually used in a setting that once the station was selected,
it didn’t change, but lately, he’d turn
it on and after a few minutes, the radio de-tuned and was thus unusable.
For people of a certain age, modern
radios often don’t cut the mustard.
While they might have much more
sophisticated circuitry, and accurate
and stable digital tuner sections, the
sound output is often not as good when
compared to older models. I’ve found
many newer sets sound ‘tinny’, which
could be due to smaller speakers and
flimsier construction.
While perhaps not as portable (in
the modern sense), many of us prefer
our older radios. So that is why we try
to keep them going as long as we can.
The Superadio duly arrived at the
workshop, and I fired it up to test it.
It did sound good, which was likely
down to the substantial dual speaker
system, consisting of a 165mm woofer
and a 50mm tweeter.
However, after a short period, the station slowly drifted off, and the audio
sounded like any other radio does when
slightly off-tune; awful! Fortunately,
this model was popular in its day, so it
didn’t take me long to find a lot of information about it online. It turns out
that the station drift is a known problem, and is usually down to the tuning
potentiometer wearing out.
The job was made slightly more difficult due to there being two different
circuits (and circuit boards) employed
in this model, so determining which
one I had was the first hurdle. Luckily,
the online ‘fan pages’ I found enabled
me to quickly determine that it was an
earlier board. This information also
documented several other inherent
‘flaws’ with the original design, and
offered fixes for these issues.
Older radios are typically tuned
using a variable capacitor, a so-called
“tuning gang”. I have a drawer full of
these sometimes-substantial components, salvaged from radios over the
years, and they are a marvel of engineering.
Essentially, they are just a set of rotating metal plates that intertwine.
The degree they overlay determines
the overall capacitance. One of the
marvels of modernisation (and circuit design) was to shrink the size of
these variable capacitors down to a
small mostly-plastic version which
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was used in the majority of ‘pocket’
transistor radios.
These ‘miniature’ tuning gangs are
still being manufactured, and are available from the usual suppliers.
In this radio, though, varactor-diode
tuning was employed. While this is
usually a robust system, it relies on the
integrity of the potentiometer used to
tune the radio. When the carbon track
inside the pot inevitably wears out,
tuning becomes increasingly erratic.
And to make matters worse, the value
of that potentiometer is 300kW, a rather
oddball figure and (for me) very difficult to source.
It is also an unusual size, 16.5mm
in diameter, and I couldn’t find any
new versions to replace it with, regardless of electrical value. While I could
squeeze a modern pot in there with
modifications, it would be preferable
to use a similar-sized replacement.
Back when this radio was designed,
there was no doubt a good supply of
different potentiometer values and
physical sizes; but over time, manufacturers pared down their product lines
to supply only standard sizes and values. So replacing pots in older equipment is increasingly problematic.
I went through my pots bins and
trawled the usual supplier suspects,
but nobody had a 300kW pot of any size.
Needing to compromise
Fortunately, one of the websites
included a ‘mod’ where a 500kW pot
could be used instead. However, even
if I could find one to fit on the board,
Australia’s electronics magazine
this would have the effect of shifting
stations down the scale and making
tuning in the upper regions of the band
very finicky.
I went back to the customer and
asked if this would matter; his original communication stated he tuned the
radio to one station and left it there.
Assured this wouldn’t be an issue, I
proceeded to disassemble the unit.
Like most of these jobs, it was merely
a matter of removing the external
knobs, taking out some standard
screws, desoldering a couple of flying leads and removing the back half
of the case. If only modern manufacturers would use these methods, instead of those pesky security fasteners
and breakaway clips; life would be so
much easier for us servicemen!
Once exposed, I removed the old
tuning pot by the usual methods and
replaced it with a similarly-sized
500kW model sourced from an online
supplier. I didn’t bother with matters
like choosing a logarithmic or linear
taper; I found a 500kW pot the right
size, so it would have to do! After all,
tuning wasn’t going to be the same after the fix anyway, and the customer
would simply ‘set and forget’.
I considered making the suggested
mods for the first-revision board that
aimed to improve performance. While
they might not be pertinent to the
owner, I figured that as the thing was
already dissected on my workbench,
I might as well do them.
The antenna circuit Q can be increased by changing one resistor on the
November 2020 67
board. The original is 100kW; changing
it to around 50kW apparently helps, so
I just soldered another 100kW resistor
across the original. There is another
similar mod that significantly lowers
the AM noise floor. The fix is again
to parallel a 100kW resistor across an
existing 100kW on the board, halving
the resistance.
The radio can apparently also benefit from a narrower ceramic filter, and
as I already had a suitable replacement
in my parts boxes, I removed the original 280kHz component and replaced it
with a 120kHz version. Later revisions
of the radio had these mods already
implemented at the factory.
Another mod is to improve bass response by increasing the size of certain off-board capacitors. However, as
the customer already liked the sound,
and the case would require modification to cram in bigger capacitors, I
didn’t bother. Once reassembled, I ran
the radio for three days on the bench,
and it didn’t drift at all.
So that was my jobs done, and thank
goodness for resources like the internet
and decent documentation. Perhaps I
should also thank the electronic spirits
inside these devices, lest I incur their
wrath once again!
Do you have any good servicing stories that you would like to share in The Serviceman
column? If so, why not send those stories in to us?
We pay for all contributions published but please note that your material must
be original. Send your contribution by email to: editor<at>siliconchip.com.au
Please be sure to include your full name and address details.
way through before slowing to a crawl
as the formed product exited the machine, with the motor protesting, and
finally the variable speed drive shutting down to protect itself.
The machine was supposed to roll a
96mm top hat from up to 1.2mm steel,
yet plainly did not have the torque to
run smaller gauge.
The motor was rated at 5.5kW; we
replaced it with an 11kW unit with
a chunky gearbox, along with a very
much larger VSD. Suddenly, these machines didn’t look so cheap.
We fired it up again and found the
current drain was precisely the rated
current of the new motor, which was
sort of good but it needed to roll thicker steel, so it would probably need
more torque.
Furthermore, the section emerging
from the machine was quite warm to
the touch, which indicated it was being rolled up too abruptly as the machine was too short, and the roller stations were too close together. This was
resulting in the product being forced
into shape instead of being guided.
So, hoping for the best, we loaded
the thicker material and off it went
for a few metres, until the drive chain
shattered. An examination revealed
that the strain was so great the links
had stretched until one gave up.
A good quality chain was fitted and
tried again; the motor was protesting,
and disturbing noises were coming
from the front roller set, but the piece
was emerging from the machine. After
the machine had measured and cut off
the section, one of the workers picked
it up and promptly dropped it with a
yelp, saying something along the lines
of “it was rather hot’.
He was right! It was dangerously
hot, with zinc flaking off the steel, so
a tremendous amount of friction was
being generated in the last roller set.
Checking the gap between the roller
pairs that sandwich the steel, we measured 0.8mm but it should have been
1.5mm, to allow for the full range of
steel used.
So the machine had become a roller
mill trying to compress the steel thinner. Goodness knows how the bearings coped!
The rollers now needed to be turned
down slightly in a lathe, as there was
no gap adjustment. This is not an easy
thing as they usually are extremely
hard steel. Fortunately(?) the manufacturer hadn’t bothered with that
Australia’s electronics magazine
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Fixing substandard industrial
machinery
G. S. of Montrose, Tasmania, has
sent in the following saga both as a
servicing story and also to remind our
readers that if the price seems too good
to be true, it probably is. That includes
industrial equipment!
In previous submissions to Serviceman’s Log, I reported on work I do for
a long-term client that manufactures
steel building products. He has made a
habit of purchasing old, worn-out machines, and as he is blessed by having
a very skilled fitter in his employ, we
have been largely successful in bringing them back to life.
Recently, he strayed from this policy
and elected to purchase two new “top
hat” roll formers from a manufacturer
in Asia. He paid around 30% of what
locally built machines cost, which
should have rung alarm bells, but he
saw it as a great deal.
Roll formers are essentially a long
heavy steel frame with ‘stations’
spaced along its length that are fitted
with rollers. They are progressively
shaped to slowly form the required
product profile from a steel strip.
There are generally top and bottom
rollers that sandwich the material between them and either the top or bottom row are driven by heavy chains
and sprockets, in turn, driven by an
electric or hydraulic motor. There are
plenty of examples of such machines
on YouTube if you are interested.
I received a call saying the machines
had shown up, but the electrician refused to connect them, stating they
were substandard and wasn’t risking
his license to do so. As I was eyeing
retirement, we were trying to get a new
electrician up to speed, and he was on
a steep learning curve. His background
was commercial, so he had a bit of a
hard road ahead learning to be an industrial electrician.
I went to the factory and found
two nicely painted machines, which
looked very short for the task at about
eight metres (more about this later).
Looking them over, I discovered all
the problems we get with a lot of Asian
machines: no Earthing on the motors,
green Active conductors, no emergency stop system, no guards, no motor
overload protection on the hydraulic
pump and so on. So refusing to connect
them as they stood was valid.
I got the electrician onto replacing
the switchgear and rewiring it while I
sorted out the safety circuitry. This required the installation of a safety relay
and the addition of three emergency
stop buttons, low voltage control circuity and circuit breakers. Meanwhile,
the fitter fabricated guards for the roller
stations and guillotine, finally resulting in something you could use with
a reasonable chance of survival.
So all should be well, but of course,
it wasn’t. We loaded a strip of 1mm
steel and set it going. It got most of the
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and had made them from mild steel,
so it was easy to run them down to the
proper size.
Just to be sure, we added an oil feed
so that lubricant was sprayed on the
strip. This resulted in a motor current
about 20% less than the rating, so finally, all was well. Well, almost; the
bearings also needed replacing, as they
just weren’t up to the job.
So several thousand dollars later,
we got to a machine that would do
what it was supposed to do, without
the operator risking life and limb. The
final cost was perilously close to what
a locally-built machine would have
cost (which presumably would have
worked off the bat).
The second machine purchased has
an even deeper profile, and the feeling
is we will need to change its sprockets
to slow it down and get enough torque
to do the job. We haven’t started on
that one yet, as the client still needs
to get over the shock of the first unit.
There are some very good Asian
machines on the market, but it is an
expensive process to discover which
ones they are, so caveat emptor!
The water-logged electric
toothbrush
G. C. of Nelson Bay, NSW, was getting ready to use his electric toothbrush when, as he lifted it off the
charger, it started all by itself. Unfortunately, the toothbrush then decided
to switch off after 30 seconds and then
wouldn’t start again, so he decided to
see if it was repairable...
My toothbrush cost less than $30,
so it was uneconomical to repair on a
commercial basis, but that’s irrelevant
in this case as it was my own toothbrush and it’s never useful to charge
yourself.
Upon inspection, it appeared that
the inner bottom (charging) end was removable, so I used the tiny knife from
my Swiss Army Card to pry this bottom
base part out of the handle (this blade
is great for opening iPhone screens
too). When the bottom popped out, unfortunately, so did some gungy looking
water, so the reason for the toothbrush
malfunctioning was obvious.
I kept going and eventually found
that the complete motor, battery and
charger electronics assembly could be
pushed out by pressing (very) firmly
on the brush end. I always found it a
challenge the first time I have to open
something, as I have to figure out how
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hard each part can be pushed before it
either opens or breaks.
The PCB has a wireless charging coil
at the bottom end, diodes to rectify it
and quite a few SMD components, presumably to make the regulated charger
for the NiMH 2.4V/500mAH battery.
The 8-pin SMD IC has to be a microcontroller of some sort as it would
have to control the charging, monitor
the tiny pushbutton and control the
transistor that switches the DC motor
on and off.
The final part is, of course, the little DC motor that moves the brush.
Everything was slipped into, clipped
or soldered to a cunningly designed
moulded plastic part which holds it
all in place.
The electronics was wet and had
some slight corrosion; toothpaste and
water is not a recommended environment for electronics, so I unsoldered
the PCB and followed my usual routine for wet electronics. I got out my
trusty Jaycar ultrasonic cleaner, waited
90 seconds and voilà – no more visible
contamination. After a quick rinse in
clean water, out came the hot air gun
until everything was dry.
I decided to set up a simple test jig
before trusting the NiMH battery. I just
soldered wires to the + and - battery
pads on the PCB and reconnected the
motor leads, then set the voltage to
2.4V with a low current limit on my
bench supply. Switching it on, nothing happened and the motor stayed
off when the tiny pushbutton was depressed, but at least no smoke escaped.
After years of experience, I’ve found
that mechanical parts fail much more
often than solid-state parts, so next, I
checked the miniature switch. Press-
Australia’s electronics magazine
ing it produced quite inconsistent resistance readings, varying between
1W and 10W. I’ve found this frequently happens with these little switches,
especially when they have been wet,
so the switch had to go.
I had ordered 100 of these switches
when I had to repair several car remote
controls (all love jobs too, and all had
been wet) and I still had a great many
of them left, so it was just a matter of
out with the old switch and in with
the new. I also decided, as the solder
joints didn’t look quite ‘right’ to me,
to apply flux and redo every solder
joint, which only took a few minutes
for this little PCB.
This time, when I applied power,
the toothbrush worked correctly, with
the motor turning on and off as usual.
It was then just a matter of resoldering the connections to the PCB. I did
make two changes – I replaced the very
thin motor wires with some stripped
out of Cat6 cable, and also added some
1mm Teflon insulation to one lead of
the charging coil where it came very
close to other components.
I even remembered to finally check
that the wireless charging light turned
on when the toothbrush was very close
to the charger base station. All that
remained was to reassemble it, but as
I wasn’t impressed with the original
sealing method, I made new seals at
the motor end and to the bottom base
part with neutral-cure silicone sealant.
Over many years I’ve found that silicone seals 100%, but can usually be
removed, even if requiring a bit more
force than the original sealing method.
At least it will never leak and kill the
insides again, so it shouldn’t need to
be disassembled again!
SC
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