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SERVICEMAN'S LOG
Decisions, decisions, decisions...
Dave Thompson
Ford or Holden? CD or vinyl? Mica or polystyrene? Hybrid or electric?
Digital or analog? PC or Mac? Petrol or diesel? Topics like these generate
a lot of debate in workshops, pubs and internet forums. While there
are no correct answers, this doesn’t usually stop us from holding strong
opinions. Which brings me to my love of analog multimeters...
I’d like to think I’m not the only
one who ponders these important
philosophical questions. Servicemen
of my generation have had the good
fortune to have plied their trade in an
era of almost unparalleled technological growth.
Believe it or not, there are still people around – they are admittedly getting on now – who cut their servicing
teeth on valve-based hardware.
They then had to ‘upskill’ to stay
current as transistors and integrated
circuits became more commonplace,
while tubes disappeared into history
(and expensive guitar amplifiers!).
Many industries lag behind the
“bleeding edge” due to the systems
involved, meaning there can be considerable overlap in old and new technologies.
I started work at our national
airline as a know-nothing slip of
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a lad in early 1980. Even then, there
was still some valve-based aircraft
hardware being serviced in the various avionics workshops.
Don’t get me wrong; it wasn’t a lot,
but because at that point there were
some relatively old aircraft still being
maintained by the airline, I did get to
work on a few tube-based components
of that era.
Remember, this is “only” 40 years
ago, and there were many other areas
aside from the aircraft industry where
vacuum tube technology was still in
wide use (broadcasting and music
amps to name a few).
While it might seem old-fashioned
by today’s standards, I
was experiencing the
Australia’s electronics magazine
tail-end of an era of huge technological
growth brought about by World War 2.
To the people involved at the time, it
was just as awe-inspiring as anything
we see happening today.
The evolution of digital displays
Digital displays are one example.
Of course, they were around even in
my earliest days of dabbling in hobby
electronics. In my early days, I saw the
exotic (for the time) Nixie tubes, which
could spell out numbers and letters,
and it seemed like the devil’s magic.
Nowadays, Nixie tubes are considered
retro-chic and while relatively expensive, such is their popularity that they
are still being manufactured.
October 2020 61
I still clearly recall seeing my first
LED display, a red bubble-style arrangement on a clunky HP calculator
my dad bought in the mid-70s.
Aside from the mind-boggling capabilities of the device itself (four
functions!) with that LED display, the
whole machine seemed nothing short
of miraculous.
I’d seen calculating machines before, and had even built a crude model
as part of a team of school pupils for
an early science-fair project.
However, that device used switches,
potentiometers and analog meters to
calculate and display basic mathematical functions.
While it worked, it was underwhelming, and didn’t win any prizes. It did demonstrate the basic principles that all modern computers run
on though (royalty cheques accepted!).
The biggest issue was reading those inherently inaccurate analog meters and
trying to analyse the results of our calculations. It would have been so much
easier if we’d had a digital readout.
That is why I was so impressed with
that HP calculator; tap in your figures,
press a button and there it was; even
the dimmest among us could read directly from the display.
Shortly after that, I saw my first
digital watch. These so-called “moon
watches” were unbelievably modern
and a much sought-after accessory.
At the press of a tiny button, the time
(and day and date in some versions)
was displayed on a miniature red LED
array for around five seconds before
going dark.
This was a trade-off between functionality and battery life; the tiny
‘watch’ batteries of the day would
soon run out, so the time was only displayed briefly at a press of the button.
These watches were so über-cool that
everyone who saw one immediately
desired one, though not many could
afford them in the early days.
Nobody really wanted to wear those
old-timey analog Rolex, Citizen and
Seiko watches anymore; all that mattered was having a timepiece with a
sleek stainless-steel body and a mysterious LED display!
As time went on (LOL!), prices fell,
especially with the advent of back-lit
liquid crystal displays, whose powersaving properties and increased functionality made moon watches old-hat
almost overnight.
But those early LED watches are
now a sought-after item, with the hipster crowd especially prepared to pay
big money for original models. The
sad fact is that many of those old-style
LED displays are now so weak as to be
unreadable because (like me) time has
robbed them of their glamour.
Analog vs digital:
this time it’s personal
From an electronics measurement
point of view, digital displays were
regarded as revolutionary. Way back
when, I only used analog meters because that was all that was widely
available.
Those of a certain age will recall
those large, heavy Bakelite Avo-style
multimeters (and their clones) that
cornered the market in the 60s, 70s
and 80s, before the likes of Fluke and
others popularised the digital multimeter, driving analog meters increasingly out of fashion.
On the face of it, having a digital
meter made sense. For one, you could
read the exact value on the display, so
there was no misinterpretation of the
results, or pesky parallax errors. And
you could see it in the dark, which
alone was bordering on voodoo to
many servicemen.
Many digital meters also featured
a ‘hold’ function, meaning you could
measure in cramped quarters and extricate yourself before checking the
results on the meter. This was something just not possible with the analog
meters of the time.
This is what they call progress.
However, there were problems. Digital displays require actual reading. Pilots, for example, don’t need to know
their exact exhaust gas temperature;
they just need to know the needle is
in the right place and a quick glance
tells them all they need to know. Reading EGT on a digital readout takes time
and breaks concentration.
It takes me longer to note my car’s
speed on a digital speedo than an
analog dial, requiring me to take my
eyes off the road for longer.
Editor’s note: I find the exact opposite to be true, despite using analog
speedometers exclusively for almost
20 years before getting a car with a
digital readout.
These days, I often find myself using my analog multimeters, but it also
depends on the task in-hand. I’m lucky
to have options, because I’ve built up
a collection of both analog and digital
types over the years.
And given that I can buy a digital
multimeter for just a few bucks that
(on paper at least) matches the specs
of any multi-hundred dollar analog
model of just a decade ago, there is
no excuse not to own more than one.
Items Covered This Month
•
•
•
•
•
Decisions and hard choices
Yamaha amplifier and Simmons
subwoofer repair
Battery replacement for tablet
Vox valve guitar amp repair
Mitsubishi aircon repair
*Dave Thompson runs PC Anytime
in Christchurch, NZ.
Website: www.pcanytime.co.nz
Email: dave<at>pcanytime.co.nz
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Australia’s electronics magazine
siliconchip.com.au
For one project, it was cheaper for
me to buy two digital multimeters
from the local electronics store than
to buy dedicated volt and ammeters.
And if I am only reading the battery
voltage under the bonnet of the car,
or using the continuity beep function
to ring out a cable loom, I don’t need
anything as fancy or as inconvenient
as those bulky, olde-worlde movingcoil models anyway.
However, like many service people,
I still love my analog multimeters!
Disaster strikes
I only bring this up because the other
day I was moving an amplifier chassis
around my workshop and as I picked it
up from my (admittedly overcrowded)
workbench, I accidentally snagged one
of the leads of my oldest and dearest
multimeter.
Not realising I was caught up, I
dragged the meter off the bench and
it fell and hit the barely-carpeted concrete floor of my shop with a sickening
crunch. Yikes!
This particular meter has a nice
leather case, and while you’d think
that this might help save it, alas, no.
While not appearing physically damaged, the meter’s needle now sat fixed
at a weird angle at around 30% of the
scale, and wouldn’t move when the
meter was lightly shaken from side
to side.
This is a classic sign the meter’s armature had either been shocked free
of the pivots it usually sits in, or was
just broken. It wasn’t looking good.
Many people would just shrug their
shoulders, throw the meter in the bin
and get another one out of the drawer,
but you know me; if this wasn’t repairable I might consider chucking it, but
until I ran out of options, binning it
wasn’t going to be one of them.
The first thing I did was undress
it. The leather case might look authentically vintage, but it didn’t do
much to prevent the meter from getting clobbered. Then again, perhaps
things might have been worse if it
didn’t have any protection at all. Ah,
yet another philosophical question
to ponder!
I quickly removed the few screws
that held the back on. No pointless
anti-tamper fasteners here, just good,
old-fashioned self-tapping screws.
There were two batteries inside,
one PP3 and one AA. This slightly
surprised me; while I am obviously
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aware these things have batteries,
this meter is at least 30 years old and
I can’t recall ever replacing them! I’d
take the opportunity to do that now,
but first I’d need to get the meter working again.
The PCB was held in with another
couple of screws, and with those out,
only the front panel knobs prevented
it from being lifted straight out. The
knobs popped off without too much
effort.
The four main connectors, what
I call banana sockets (but are also
known as 4mm connectors) were hardwired to the PCB and came out with it
as an assembly.
I de-soldered the few flying leads
connecting the batteries and meter,
but I was careful to leave the rotary
switch components sitting in the top
cover, as there are lots of small bits
and bobs that make up the switch and
these are easily lost.
I’d made this mistake before years
ago, creating a lot of extra work for myself, so I was prepared for it this time.
I took a digital photograph of the positions of all those bits before removing them and putting them aside in a
parts tray.
I was now left with the plastic top
‘half’ of the body and the meter assembly. The clear plastic meter facia
simply pried off with some gentle persuasion applied to the slots provided.
From this point, I had to be ultracareful, as the meter movement was
now totally exposed and I didn’t want
to damage it further. The white meter face was also vulnerable to contamination with dirt, fingerprints and
wayward tools, and any mistakes at
this point would really decrease my
chances of a good outcome.
Analog meter 101
This movement is what is known
as a moving-coil meter, and they are
used in many indicator and measurement roles. Their operational theory
is simple; a soft iron armature, with
a needle attached and a coil of wire
wrapped around it, is suspended
within the magnetic fields of a permanent magnet.
When a current is applied to the
coil through two tiny counter-wound
hairsprings (which also assist with
meter damping), a rotational force is
created proportional to that current.
The amount the needle deflects is then
apparent against a scaled meter face.
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October 2020 63
The trick is making the armature
as friction-free as possible, increasing sensitivity, and in really goodquality meters this means mounting
the pointed ends of the armature into
jewels embedded in the meter frame.
Mechanical wristwatches also commonly use this technique.
Cheaper devices use either bronze
or steel bushings to do the same thing,
and usually work just as well; the only
downside being they may not last as
long without adjustment.
In this case, one end of the armature’s mounts is adjustable via a setscrew, which also fine-tunes the ‘endfloat’ of the assembly, and correct adjustment means an almost friction-free
movement.
End-float is usually set at the factory, then sealed with a dab of paint.
This adjustment lasts (hopefully) a
lifetime. Most meters also have a zeroadjustment screw accessible from the
outside that engages and alters the armature spring tension, allowing a null
balance point to be set.
I thought the armature might have
simply been jolted out of its mounts
by the fall, which would explain the
cock-eyed angle the needle was sitting at, and the lack of free movement.
Visual inspection under magnification
confirmed this was the case.
The only way to replace the armature into its mounts was to back off
the top adjustment screw until I had
enough room to reposition the pointed ends back into the bearings. I could
then re-set the end-float for maximum
free movement without any play.
I backed off the set-screw by breaking the paint seal and gently coaxed
the armature back into place with
tweezers, a job made trickier by the
springs, as they tried to pull the armature in different directions.
I managed to position it, tightened
the screw and carefully adjusted it.
However, the needle still read half-way
up the scale, and the zero-adjuster had
minimal effect.
With the armature in place, the
movement should have been free to
find its natural balance against the
spring tension, and would be adjustable with the mechanical zeroset screw. However, the needle was
still ‘sticky’ and moved erratically, so
something else was going on.
Another inspection showed the outer coil of the bottom hair-spring was
wrapped around one of the tiny, sol64
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dered coil connections. It wasn’t going
to move freely if that spring was impaired, so with two pairs of tweezers,
I gingerly extracted the spring from
the obstruction.
This is trickier than you might think,
as these coil springs are extremely
thin and fragile, and any kink or other
anomaly would alter its tension and
would prevent the meter from ever being accurate.
Luckily, I managed to unhook it,
and the needle immediately fell back
into place. With a sigh of relief, I reassembled everything and checked calibration against some known values.
I used a 50W reference resistor and a
regulated 5V output from a power supply, and after some adjustment, both
results were close enough.
Disaster averted, and my favourite
analog meter lives for another day!
Yamaha AX-300 amplifier and
Simmons S-10W subwoofer repair
R. W., of Lismore, NSW took a punt
on buying some cheap old audio gear
in the hope that he could fix any problems that might crop up due to its age.
As it turns out, his confidence was not
misplaced…
Motivated by letters in Silicon Chip
on repairing older hifi amplifiers, I
Australia’s electronics magazine
kept an eye on an internet auction site
with a view to obtaining a decent amplifier and a small subwoofer. Eventually, I bought a 1980s Yamaha 30W
per channel amplifier and a 100W subwoofer with an odd 10-inch driver for
a bargain-basement price.
The vendor of the amplifier stated
that one should not expect it to perform as it did when new, but I was not
perturbed as it cost less than $50 and
could use the case if it was a write-off.
After performing some safety
checks, I powered up the amplifier
and sampled its performance. What a
disappointment! It had quite a lot of
hum in both channels, the volume pot
was noisy, and the sound could best
be described as “thin” – lacking in fidelity and dynamic range.
On removing the cover, the innards
were relatively clean but 6000µF power supply filter capacitors had noticeable bulging. I was unable to obtain a
schematic for the amp but decided to
take a punt and replace the caps and
see how things went from there.
As it happens, Altronics sell similarly sized electrolytics rated at 10,000µF,
so I decided to mail-order some. The
cost was well below their minimum
for mail order, so I decided to change
every electrolytic capacitor in the amp.
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On powering up with the new caps,
the hum had completely disappeared,
and the performance was probably as
good as new.
Some contact cleaner for the pot and
a new coat of satin black paint on the
cover, and it was like new. I remember being impressed with the Yamaha
amps in the 80s and this one was no
different now.
A few days later, the subwoofer arrived. It had clearly been stored somewhere damp, as there was mould residue on the driver, the case and the
grille. This was easily cleaned off,
and the enclosure was then immaculate. Powering the speaker with nothing connected and I was greeted with
– yes, you guessed it – hum!
Removing the integral amplifier
again showed bulging filter electros
in the power supply with a value of
10,000µF that were the same physical
size as the ones from Altronics. Two
more of these fixed the hum issue, so
I set the system up with my TV.
On switch-on, after the speaker
protection relay engaged on the subwoofer, I was yet again greeted by hum!
This had to be an Earth loop as both
the sub and the Yamaha amp were
quiet when separated. The AX-300
has a shielded power transformer but
is supplied with a two-pin mains plug
and had an Earth binding post for use
with a turntable.
The sub has a 3-wire IEC power input socket. I made a 3-pin mains plug
with just a green wire connected to
the Earth pin, and I connected the
other end to the binding post on the
amplifier.
The hum disappeared, so it was definitely an Earthing problem! So I replaced the amplifier’s power cord with
a 3-wire mains lead, properly secured
and Earthed.
For less than the cost of a soundbar, I had obtained a sound system
that would blow any of them out of
the water, and saved some old but still
useful pieces of equipment from the
scrap heap.
I’ve been using a Samsung Galaxy S
10.5 tablet for a few years now. Lately,
I noticed that its screen was bulging
in the middle and it had come loose
from the frame.
I immediately realised that the battery must be failing. I’ve seen this happen to other devices, so I knew it was
time to replace the battery.
Before I started working on my tablet, I found a good video on replacing
the battery in this particular tablet on
YouTube. Watching that, I picked up
some useful tips.
The first thing to do was to remove
the back of the tablet to access the
battery. This proved to be somewhat
tricky, as the back had not been removed previously, but with some effort and a couple of phone repair tools,
I was able to remove the back and gain
access to the battery.
With the back removed, I could see
just how badly the battery was bulging. I was also able to press the screen
back into place. I was hoping that the
screen had survived being bent; I later determined that it had not suffered
any damage from being bent away
from the frame.
Removing the battery is fairly easy;
it just entails disconnecting two ribbon cables and the battery connector,
then undoing the four screws that hold
the battery in place. I was going to or-
der a new battery via eBay; but first I
thought I would try the battery from
another identical tablet I had, to see if
it was still usable. The other tablet’s
battery charging circuitry had failed,
and I couldn’t fix it, so it was a suitable donor.
Because this battery had been flat
for months, I was concerned that it
might not charge, but decided to install it anyway and give it a go. After
moving it from one tablet to the other, I reconnected the ribbon cables,
plugged in the charger and left it for
several hours. I occasionally checked
it to see whether it was charging.
The charge indicator sat on 0% for
quite some time, leading me to think
that it wasn’t going to charge. Eventually, it went up to 2%, which was a
good sign. It took a long time to charge
the battery fully, but it did reach 100%.
The next thing would be to see if it
retained its charge, after being flat for
months.
I checked it the next morning, and
it was still 100% charged, so it looked
like the battery was still viable. I was
a bit concerned when I noticed that
there was a “no go” symbol next to the
battery charge indicator on the screen.
But I thought this might be because the
back was off, so I refitted it.
Now that the back was on, the “no
go” symbol was no longer present, so
The bulging case of the Samsung tablet is shown above, with the battery shown
below.
Samsung tablet battery
replacement
B. P., of Dundathu, Qld has become
quite adept at keeping old electronics going. This time, he noticed a
quite worrying symptom in his tablet and luckily, had a ‘donor’ device
which provided the parts he needed
to fix it...
siliconchip.com.au
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October 2020 65
that confirmed that the assumption
was correct.
Often when a lithium-ion battery is
flat for some time, it will no longer accept a charge. Whether this battery’s
bad start to life will come back to haunt
it in the future remains to be seen, but
for the moment at least, it seems that
it’s still good.
I tried fitting the damaged battery
into the other tablet with the faulty
charging circuitry, but it wouldn’t
switch on, and I noticed some parts
of it getting very hot, so that tablet is
only useful for spare parts now.
Regardless, this was another repair
that ended up not costing me anything,
thanks to having access to the defunct
tablet for spares.
These batteries are around $25-30
on eBay, so they aren’t that expensive,
but it was nice to be able to complete
the repair at no cost. I hope to get a
lot more use from this tablet before it
becomes obsolete.
Vox valve guitar amplifier repair
S. W., of Fulham Gardens, SA had
to guess at the values of some burnt
components to repair a guitar amplifier. While it turns out that the values he chose weren’t the same as the
originals, they must have been close
enough as the repaired amplifier
worked well enough...
Some time ago, I was asked by a
family member to repair a Vox AC4TVH 4W valve guitar amplifier that was
inadvertently operated without the
speaker connected. Apparently, the
user was unaware that this amplifier
does not have a built-in speaker, and
should only be used with an external
speaker plugged in.
After removing the amplifier module from the case, I observed that heat
stress on several resistors had caused
their values to become unreadable.
High-voltage supply fuse FS2 was
also blown. I checked the audio output transformer and found it to be OK.
I then powered up the amp and
found that the mains transformer secondary voltage was acceptable, and the
filaments of the two valves were alight.
Hence the two major components appeared to be undamaged. Great!
Further testing revealed that three of
the heat-stressed resistors were opencircuit. I was unable to find a circuit
on the web to identify their values.
Therefore, I saw no alternative except to trace out the circuit of the module using some valve circuit theory
from decades past. This resulted in the
circuit diagram shown here where R5,
R17 and R24 (highlighted in red) were
the open-circuit resistors.
Using basic circuit theory, I selected a value of 180W for R5 to allow the
EL84 to self-bias at about 8V with an
anode current of around 50mA, and
820W for R17 and R24, to keep the anode and screen voltages for the EL84
below 300V when operating.
Once the resistors were replaced, I
soon discovered that the major problem was an internal short between the
screen and grid of the EL84. With a
new tube in place, the amplifier fired
up as expected. The only problem was
that the power output was only about
3.8W across a resistive 15W load before amplitude limiting set in.
I contemplated lowering the value
of R17 and R24 to increase the available power to 4W. However, the owner was not concerned about the lower
power level and was just happy to get
the working amplifier back.
As I was working on it, I noticed
signs that the amplifier had some problems in the past. For example, blown
fuse FS2 was labelled 200mA, while
the value written on the circuit board
was 125mA.
This may indicate that sometime
in the past FS2 was replaced with the
higher-rated fuse. Possibly, this was
The full circuit diagram for the Vox AC4TVH valve-based guitar amplifier, which was found online.
66
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Australia’s electronics magazine
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done as a quick fix for an intermittent short in the EL84. One can only
speculate!
Some time later, while I was searching the web for information on singleended valve amplifiers, I came across
a full circuit diagram of the AC4TVH.
In this circuit, R17 and R24 are shown
as 220W while R5 is 180W. So I got R5
right, but went a bit high on R17 and
R24, hence the slightly reduced output power.
Mitsubishi aircon repair
D. S., of Maryborough, Qld took a
look at an aircon that had been deemed
unrepairable by a professional. And
guess what, he managed to fix it with
just a bit of effort and a less than a dollar’s worth of parts. Sadly, this is far
from an uncommon story...
Air conditioners, in both vehicles
and homes, usually come up for repairs and service during summer. So,
I wasn’t surprised when I got a phone
call from a friend in January asking if
I could take a look at his home aircon.
I was told that a service agent had
already looked at the system but had
told the owner that the mainboard had
been destroyed by gecko urine, and
that replacement mainboards were not
available, so the whole system would
have to be replaced.
I thought there must be a cheaper way to fix it, so I switched off the
power and took off the covers. Many
covers... I have to admit, the chances
of a gecko getting into the enclosure
which held the circuit boards seemed
slim with all the covers in place.
Upon initial visual inspection,
I found no physical damage, so I
grabbed my drivers again. After rechecking to ensure the power was off, I
disconnected the mainboard, marking
all the various connectors and taking
photos on my phone to ensure that I
could reassemble it later.
15 minutes later, I had the mainboard out. A much closer inspection
showed nothing of interest, no damage, no swollen electros, no burnt-out
transistors, nothing! I searched the rear
of the board, checking for dry or broken solder joints.
The board did have a few heat marks
and discolouration on it from thermal stress, but removing and checking the affected components, I found
no problems.
It’s a Mitsubishi split system aircon,
and these units are very well made.
siliconchip.com.au
The boards are fully marked with all
components types, values and test
voltages silkscreened to the board, so
it was a pleasure to find everything as
it should be.
So I refitted the board, plugged everything back in and turned it on. The
head unit lit up like it should for about
five seconds, then shut down again.
The condenser section was doing the
same. The main condenser fan started
up and ran for about two minutes before shutting down, but the compressor did nothing.
I searched the internet hoping to
find that this unit had on-board diagnostics and it did. However, we
could not locate the remote to press
the appropriate buttons to get any
fault codes.
After further checking, I noticed
that the mainboard switched mains
to the various mains components, but
the control circuitry ran from 24V DC,
12V DC and 9V DC rails. The mainboard did not have any form of power
step-down circuitry, so where were the
logic supplies coming from?
I removed the mainboard again and
discovered another board hidden beneath it, inside its own plastic enclosure. Another 15 minutes of fiddling
finally got it out. Close inspection revealed several leaking electros and
quite a bit of corrosion across this
smaller board.
Replacing the leaky electros and
cleaning up the mess was easy. All the
caps were common value, high-temperature through-hole components.
I also found the remains of a very
small signal diode that had virtually
rotted away. I had to guess its type as
the corrosion had also destroyed that
part of the silkscreen.
I used a 1N4007 type rated at 1000V,
1A. This power board supplied the
various DC rails to the mainboard via
a small relay, so I reasoned that this
was a good choice.
I also found a tiny ceramic capacitor
fitted across two wires of a five-wire
connector. I backtraced this small harness back to the mainboard where it
connected to the processor chip. The
power board had several ICs controlling the various switchmode sections,
along with the usual opto-isolators,
SMD transistors and various other surface mount components.
This harness carried control data to
and from the mainboard to the power board, although I could not locate
any other information on its function
online.
I cleaned up the corrosion, re-drilled
the through-holes and concentrated on
the remains of this small capacitor. It’s
difficult to clean off corrosion without
removing the markings, but after some
very gentle wiping, I found the value
104 marked. Thus it was a 100nF capacitor, which I had in my parts box.
After replacing that capacitor, I began to reassemble the various boards.
That’s when I found that the corrosion
on the small harness had eaten through
one of the conductors. I have heard
many times that “it just fell off in my
hand”. Well, this time it really did!
I cut off the damaged section of cable, reattached the connector and refitted the board into its hiding place.
The mainboard went back without a
hitch, and I plugged all the wiring back
into their clips.
On went the power; no bangs or
puffs of smoke occurred so I flicked
the manual off/on switch on the head
unit and it sprang to life.
After 30 minutes, I refitted the external covers and gave my friends the
good news. There was some bad news;
he would need a new remote control,
but at $65, that was going to be a lot
cheaper than a whole new system!
Another air conditioner saved from
landfill; it was almost chucked out because a service technician could not
be bothered to diagnose it fully. I have
no idea which fault or faults were actually stopping it from working, but
I have always been a firm believer in
fixing that which can be fixed!
SC
Servicing Stories Wanted
Do you have any good servicing stories that you would like to share in The Serviceman column in SILICON CHIP? If so, why not send those stories in to us? In doesn’t
matter what the story is about as long as it’s in some way related to the electronics or electrical industries, to computers or even to car electronics.
We pay for all contributions published but please note that your material must
be original. Send your contribution by email to: editor<at>siliconchip.com.au
Please be sure to include your full name and address details.
Australia’s electronics magazine
October 2020 67
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