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SERVICEMAN'S LOG
I hope the purists won’t spit their dummies
Dave Thompson
I love a good restoration; it’s great when old gear is kept working into
the 21st century in original condition. But sometimes that just isn’t
possible, and it’s a good enough result to get something working again
while keeping it looking original. So what did I do that will get certain
knickers in a twist? Read on to find out...
As I mentioned last month, all
these lockdowns are (generally) bad
for business, but they do give us time
to do those jobs that were waiting for
the shipment of round tuits to arrive.
One of these jobs is a 1940s Gulbransen valve radio a friend had given me
a while ago to check over. It has been
sitting in a corner of my workshop
gathering dust for a while, simply because it looked like a huge mountain
to climb.
This is one of those large mantel radios with an oak-veneered timber case.
It has a gently-glowing dial displaying
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Silicon Chip
the many short and long-wave bands
available at the time, a nifty ‘magic-eye’
tuning indicator and a sizeable built-in
speaker, all giving it a typically warm
valve radio sound and aesthetic.
The problem with this radio is it
had been stored in an outside shed for
the last 40 years, and the moisture has
really gotten into it. The timber finish
has cracked, faded and lifted in places, and the fawn-coloured grille-cloth
and paper speaker cone now almost
Australia’s electronics magazine
Items Covered This Month
•
•
•
•
The week old vintage
The self-made (repair)man
Yamaha E303 keyboard repair
Peak Instruments component
analyser repair
*Dave Thompson runs PC Anytime
in Christchurch, NZ.
Website: www.pcanytime.co.nz
Email: dave<at>pcanytime.co.nz
siliconchip.com.au
non-existent (possibly due to rodents
or other critters chewing on them).
Worse still, the metal chassis and
internals are so corroded they are – in
my opinion anyway – beyond reasonable repair.
The guys from the Vintage Radio
section of this magazine will likely
scoff at this assessment. It seems that
anything is restorable and/or worth restoring to them! I’m imagining them
right in their beautiful, wood-panelled office with Venetian blinds, stippled-glass windows, walls of filing
cabinets and not a computer screen
in sight, scoffing away.
But keep in mind that I’m new to
this vintage stuff, and I don’t want to
start a job that I can’t finish!
For me, the problems arise when I
quote to the customer the huge amount
(including many labour hours) it
would take for me to restore this radio to health. Someone – a specialist
restorer perhaps – might be able to do
it less-expensively, and I put this to
him as an option.
He (rightly) had a minor coronary
when I told him how much I would
charge, and told me in no uncertain
terms it simply isn’t worth that kind of
money to him. I surmised as much, as
I’ve been down this road many times
before. People assume it’s just a lick of
paint, a few lines of code, or the push
of a button that fixes their prized possession; but we know it’s much more
involved.
That said, he did say this radio was
owned by a favourite relative whom
he used to visit as a child, and so it
has much sentimental value. It would
also be great to get it going again. So
what could I do?
Unless someone really wanted to
put the time and love (and money)
into this radio, I wouldn’t consider it
a viable restoration project. For one,
Collier and Beale (made locally under license from Gulbransen and distributed by HW Clarke) likely made
many hundreds, if not thousands, of
this radio model back in the 1940s. So
it probably isn’t all that special, aside
from the obvious sentimental value
to my client.
By now, I imagine dedicated restorers/collectors are frothing at the mouth
at what I’m saying. But I suspect the
vast majority of these have ended up
in refuse tips all over the country.
The tuning gang is seized, the valves
have simply gone, and the chassis is
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so rusted it would need stripping and
mechanical restoration, I’m just not up
for it; at least, not without being paid
handsomely.
Consider that the wiring, the valve
sockets and every other electronic
component would likely need replacing. While I have a reasonably extensive collection of new, old stock (NOS)
and salvaged parts from old valve and
early transistor radios and amplifiers, I
just don’t have what this radio needs.
So I’d need to spend time sourcing and
purchasing those parts before I could
even get stuck into the restoration.
The woodwork wouldn’t be a problem for me, given my proclivity for
working with timber, and I suppose the
metalwork restoration wouldn’t be too
onerous either when it comes down to
it. But if the customer doesn’t want to
spend the money, what am I supposed
to do? Sadly, working for the sheer
love of it doesn’t pay the bills, and I
just can’t do that these days.
The customer then came up with the
idea of replacing the guts with modern components, keeping the radio’s
outward aesthetic but using the likes
of modern amplifiers and tuners. He
asked me if it would be possible to
combine modules that he’d seen advertised on eBay and AliExpress to
do this, and I agreed it should work,
and would cost a lot less than a full
restoration job.
He was OK with this option, so I did
some research and ordered some inexpensive modules and a suitable speaker from our Chinese friends. While I
waited for them to arrive, I set about
tidying up the cabinet.
I will be keeping everything I remove (the chassis etc) in its original
condition, just in case the customer
wants to do a complete restoration later. I won’t be altering anything externally to maintain the radio’s authentic
look, other than to re-finish the timber
bits and pieces. I only say this to deflect any blowback I’ll be getting from
the vintage radio mafia!
Gutting it and cleaning it up
The first thing I had to do was remove everything from the case. This
involved just a few screws and unplugging a few interconnecting wires. Obviously, I was very careful in keeping
the integrity of the original parts, but
in the end, I needed to get it all out so
I could work on the case.
Veneer is a tricky material. It looks
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April 2021 47
fantastic, but is just a hyper-thin layer
of some more-expensive timber laminated (glued) onto a cheaper timber
underneath. Better-quality radios and
stereograms were made out of solid,
furniture-grade timbers like oak, walnut and elm. But sadly, not this one.
Veneer is usually so thin that any
damage to it, such as a hole worn
through it, renders the rest of it pretty
useless. Patching it often looks awful,
unless you are very skilled, know what
you are doing and have a selection
of similar veneers on-hand. I am not
skilled at veneer repairs, don’t know
what I’m doing and don’t have any
suitable materials on-hand, so that’s
three strikes and out for me.
Fortunately, in/on this case, the veneer had simply lifted and cracked a
little here and there, most likely due
to moisture dissolving the glue that
held it down in the first place. So I
thought that it might not be too challenging to repair.
There was the odd chip, probably
where something had fallen onto the
radio while it was stored in the shed,
but these dings were all small. So I
thought I’d be able to get away with
merely soaking and re-gluing the veneer down, sanding it all lightly and
then re-oiling the whole thing with
Danish oil.
It actually turned out quite well, given the age and damage and my lack of
skills in this area, and once it was oiled
and I applied a couple of clear coats of
lacquer, it looked very nice and still
maintained a realistic vintage vibe.
The other problem that I had to solve
was the dial glass. The magic-eye tuning indicator is mounted in the middle of it, and it is connected to the
rest of the old electronics via a flying
lead/valve socket arrangement. The
glass was quite dirty, and many of the
screen-printed station markings were
a bit worse for wear. I was unsure how
to clean it without damaging it further.
I started with soap and water, then
progressed to methylated spirits with
a very careful application in one hidden corner to make sure it wouldn’t
wipe the whole thing totally clean. The
outside surface was no problem; just
soap and water cleaned off all the accumulated dust and grime quite well.
I managed to remove most of the
dirt from the inside – the printed side
– without damaging any more of the
station information. We’d not be using
any of it now anyway, but I wanted to
retain the radio’s original look.
Now for the fun bit
The modules and speaker I ordered
arrived not long after finishing the
case. I purchased an 8W amplifier
module, an FM tuner module and a
Bluetooth receiver that could be connected to a smartphone, complete with
a small remote control. Grand total:
$29. You just couldn’t make any of
this hardware for the money.
The speaker I bought is a 5-inch,
20W multi-range model that would
happily handle anything the amp
would throw at it, for just $11.
The most expensive part I had to
buy was the replacement grille cloth.
While there were more modern-looking cloths available, I wanted a traditional look, so I had to buy a square
meter of it, expecting to use just a third
of that. No matter; what I don’t use will
go in my parts bins for another project.
Fitting all this gubbins into the
case was the next challenge. Once I
removed the chassis, there was nothing left to mount anything on. And I
still needed to sort out a light to shine
through the old dial gauge to give the
appearance of a soft-glowing bulb.
First, I needed to mount the new
speaker, which had a completely different footprint from the old one. I
made up a thin, custom timber insert with the correctly-sized hole cut
into it, and tacked it directly to the
old speaker-mounting facia. I then removed the old grille cloth, squeezed
the new one in around the sides,
and stapled it after pulling it taut. It
looked almost original, and I was quite
pleased with it.
Next, I’d need a power supply for
everything. The modules required ei-
Servicing Stories Wanted
Do you have any good servicing stories that you would like to share in The Serviceman
column? If so, why not send those stories in to us?
We pay for all contributions published but please note that your material must
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Please be sure to include your full name and address details.
48
Silicon Chip
Australia’s electronics magazine
ther 5V or 12V, so it wouldn’t be too
difficult. I thought about purchasing
a power supply module at the same
time as the others, but fortunately, I’d
already bought a suitable one a few
years ago for another project and had
never used it. It would do nicely here.
The only extra component to add
was a power transformer, and as I have
about 200 of the things lying around after buying a transformer-winding machine a while back, it didn’t take me
long to find one to do the job.
The amplifier would require the
most power, with the Bluetooth module and tuner lapping up the remainder. I mounted the transformer directly
to the bottom of the timber case with
a couple of wood screws. Inter-wiring
was done using standard light-gauge
cables, routed and tied-wrapped into
place.
The mains lead was simply clamped
into place (to proper specifications)
and run directly out from the back of
the box. The FM antenna was routed
around the inside of the case. Our FM
reception here is generally OK, so this
ad-hoc aerial should suffice.
I used stand-offs and long screws
to mount the other modules to the inside sides of the case close to where
they needed to be. They all use terminal blocks for interconnections which
made things simple, and P-clamps and
cable ties kept everything looking nice
and neat.
Tuning was the next challenge. The
various FM modules available online
are tuned with either a remote control, a manual up/down push-button
or rotary tuning using a potentiometer. Many of these modules come with
comprehensive LED displays, none of
which my customer was keen on.
A vintage-looking radio with an LED
display chopped into the front isn’t
that appealing. We decided that, since
he usually tuned into a single station,
he would forgo any gaudy displays
and just manually tune it, hopefully
using something resembling the original knob, if possible.
Volume control was similarly problematic; many of the modules used a
digital volume adjustment system. But
in choosing an amplifier module that
used an old-fashioned pot, that made
my job much easier. All I had to do was
remove the pot from the module and,
using suitable flying leads, connect it
via an adaptor to the case where the
original volume pot used to be.
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April 2021
2021 49
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The original knob obviously
wouldn’t fit the new pot, so I turned
up a simple brass adapter so it could fit
onto the much smaller shaft of the new
volume control. I did the same thing
with the ‘tuning’ pot, and a new rotary
on/off switch that mimicked the originals. It actually all ended up looking
very stock-standard, and the customer was happy with how it presented.
A bit of solder here and there had
the speaker and other ancillaries connected up, and it was ready to test. It
worked very well, especially as he is
a ‘set-and-forget’ user.
The only thing left was the dark dial.
Obviously, I couldn’t tee up the new
tuning with the old manual dial-cord
system or magic-eye, but he wasn’t worried about that. What would make a difference is the glow from the old dial. To
this end, I simply rigged up a couple of
orange LEDs and, after a bit of experimentation, adjusted the series resistors
to provide a convincing soft glow.
I could have gone for blue or something a bit more modern, but instead
tried to maintain the vintage look of
the original radio.
All in all, it ended up looking OK
and working very well, and as a bonus,
he can stream music from his phone
if he desires. The sound is excellent
and the volume punchy, so all in all,
it was a good solution to the problem.
Another happy camper!
The self-made (repair)man
S. G. of Mildura, Vic had a frustrating time chasing a fault which seemingly he had caused, but he still can’t
figure out how...
You might laugh at my story, but
you wouldn’t if it happened to you!
I just spent over a week trying to
repair one of my stuff-ups. A couple
of weeks ago, I purchased an amateur
band radio for the 2m and 70cm bands.
This was going to replace the 2m radio that I had in the back of my Pajero ever since I first got my license. It
also involved installing a new antenna on the bullbar, where the old UHF
CB antenna used to live.
I moved the UHF antenna to the side
of the bonnet and mounted it with a
special Z bracket, so the bonnet will
still close. This works fine, and so does
the new VHF/UHF antenna for the new
radio. The only thing that I had left to
do was to drill a hole in the firewall,
right next to the cable feeding 12V to
the caravan.
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Silicon Chip
This cable is also used to supply a
6-way fuse block so I can run fridges from the auxiliary battery, as well
as the CB radio and the new amateur
band radio.
I used a 25mm hole saw and a short
length of 25mm flexible conduit to act
as a gland through the firewall. I took
care in drilling the new hole, as there
are several wires in the area that go off
in all directions on the inside of the
firewall. Yes, I did check before drilling the hole, but still managed to take
out the interior lights, the digital clock
and the hazard and turn indicators!
First, I decided to check the fuse.
The Pajero has two fuse boxes, with
one in the engine compartment that
houses the fuse for the hazard lights.
The second fuse block is under the
dash and requires removing the trim
piece around the steering column just
to gain access. The clock and interior
lights are both on the same fuse, and I
fixed them by replacing the fuse.
The hazards are fed from two power
sources, one permanent power (from
the fuse block in the engine compartment) and the other is the accessories
circuit fuse block under the dash. This
is so that the hazards will work independently of the ignition key. Pressing the hazard button changes over the
power feed from accessories to permanent power.
This hazard switch also links both
the right and the left blinker circuits so
that all the lights flash at once.
After more head scratching, I
checked more fuses. I pulled the
Australia’s electronics magazine
blinker fuse (not easy due to the poor
access) but it appeared OK. Next on the
list was the blinker can itself. The only
way I could think of to check whether it was faulty was to try replacing it.
I then had the idea to bypass the
blinker can, which involved fitting a
small link wire between the B and the
L pins on the socket. I now had all of
the hazard lights and blinker lights
working.
At this point, it looked like I would
have to pull the whole dash apart just
to gain access to the wiring loom. I took
out the gauges, speedo and tacho cluster, just to see if I could find any damaged wiring, but it was impossible to
see properly behind the dash. I even
tried to feel for damage to the wiring
back there, but if I found it, how would
I repair it? It looked like the Pajero was
built around the wiring loom!
After some further checking of the
blinker can, though, I struck gold. This
was a three-pin can (some have just
two pins), and on checking the can
in my workshop, I determined that
the third pin was a ground and was
needed as it is an electronic type and
has a constant flash rate, independent
of the lamps.
Tracing around the blinker can socket, I soon found that while power was
present, there was no ground return. I
ended up cutting the ground wire from
the socket, soldering on a new ground
wire and attaching it to the chassis.
It still didn’t work, so I called it a
day. On Monday morning, I popped
into a local shop and bought a new can.
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After fitting it, my hazards and blinders worked – I breathed a sigh of relief!
I don’t know how the blinker can
failed; there is not much in it in terms
of electronics. It just looks like a 555
timer driving a small relay. Anyway,
I don’t care, it all works now!
Yamaha E303 keyboard repair
J. K. of Castlecrag, NSW spent a long
time tracking down a problem in his
keyboard, but at least the fix cost virtually nothing once he had diagnosed
the fault...
I purchased a Yamaha E303 electronic keyboard about 10 years ago,
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second-hand, for about $300. It is an
excellent learning tool, and had been
enjoyed by my grandchildren almost
every time they visit.
A few years ago, the highest note
(high C) stopped sounding. Since I
seldom used it, I didn’t do anything
about it. Actually, that key plays an
important role in one of the resets,
but I did not need it for that purpose.
In the last couple of months, several
more keys stopped sounding. I jumped
online and found the service manual,
but it did no more than show how to
disassemble the unit.
Disassembly is fairly intuitive, but
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removing the keys to expose the pressure pads was not obvious. Luckily,
the manual provided some pictures
which showed how to do it.
There are 61 keys in total. Each is
sounded by two carbon sticks contacting the pads on the keyboard, completing a circuit.
The E303 is a touch-sensitive piano,
so the harder the key is pressed, the
louder the note. This happens because
of the resistance of the carbon sticks
on the pads changes with pressure.
A very common problem is dirt on
the pads or the carbon sticks. Spilling
coffee or sticky drinks on the keyboard
April 2021 51
will cause significant problems, but
cleaning the carbon sticks and the pads
(with isopropyl alcohol) did not help.
So I had to check that the connections
between the keyboard and the control
unit were solid.
That is a very tedious job which required tracing voltages through the
connecting sockets and onto the keyboard. The control unit (DMLCD in the
service manual) provides 3.3V to the
two keyboard circuit boards 61L and
61H via multi-cable leads 1 and 2 (see
the accompanying diagram). I traced
the +3.3V DC supplied to CN831 on the
DMLCD board, at pins 1, 4, 5, 8, 9, & 12.
The 3.3V supply is referenced to
Earth as it appears on the control
boards, but there is no cable carrying
the Earth connection. Instead, pin 7
of CN833 is about -0.2V referenced to
Earth and that translates to +3.095V on
each of the pins mentioned above. All
the voltages were present and correct.
I had hoped that the service manual
or Yamaha themselves would give me
some leads, but they stated that they
do not get involved in repairs, and refer all such enquires to their “Service
Agents”. Strangely, the Service Agent
for the Sydney area is located beyond
Windsor.
Each pad serving a note consists
of two contacts which are “connected” by the carbon sticks when a key
is depressed. Each contact on the circuit board connects through a diode to
other pads, then connects to the control unit. Its a very clever system, because just twelve or so leads convey
information about which of 61 keys
has been pressed and whether two or
more keys are involved.
The diagram shown on the previous page is part of the left-hand keyboard circuit board 61L. The squiggly
lines are the contact pads, two for each
note. So it became a job of tracing all
of the 122 diode connections back to
the control board.
That’s when I found five copper
tracks with no continuity. Some kind
of corrosion or stress had broken the
links. The tracks are very fragile, so
even a small amount of corrosion
could break them. I considered spraying the boards with a conformal coating, but the risk of some spray getting
on to the contact pads discouraged that
idea. If more connections break in future, I will know what to do.
Luckily, the fix was relatively easy;
I just soldered a short length of wire
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between each of the diodes with a
failed connection. After doing that for
the five tracks, all of the failed keys
came to life!
I expect that a very experienced
technician would recognise the problem quickly and would simply replace
the two (low and high) keyboard PCBs,
61L and 61H, with a component cost
of about $100 plus the time of swapping the new boards in.
Doing what I did – tracing the problem – took about 30 hours which
would have cost about $2000-3000 at
standard labour rates. Which is why,
these days, most repairs are not made
at the component level, and instead,
the boards are simply swapped. I think
the control board for this keyboard
costs about $350 – more than I paid
for the whole thing!
Repairing the Peak of test
instruments
P. B. of Kaitaia, New Zealand had
given up trying to repair a piece of test
equipment, but then when he went to
take another look, a solution presented itself...
I am a retired service technician.
Some 20 years ago, I decided that a
Peak semiconductor component analyser would greatly assist my servicing
work despite its relatively high price. I
took extra care to ensure that I did not
connect it to any live equipment, and
that any capacitors were discharged
before using it.
At some stage in its life, the
self-analysis check it does on startup came up with a fault code. Sadly,
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the user manual gives no information
on what the codes signify. Looking
at Peak’s site, I rapidly concluded
that returning it to the UK for service would cost more than purchasing a new one.
Dave Thompson recently mentioned
his Peak instrument in a Serviceman’s
Log column (March 2021; siliconchip.
com.au/Article/14784), which jogged
my memory. I decided to have a look
at it again and started by replacing the
battery. However, as I went to remove
the battery, I became aware of what
seemed to be a dry joint where the negative battery spring terminated on the
board. It looked dull grey and pitted.
Ancient memory then stirred into
life, of a discussion with a serviceman
in the area some years back, of a similar fault of another piece of batterypowered equipment where the negative wire had dropped off.
The consensus was that it was a
common occurrence on aging batterypowered equipment, only affecting the
negative terminal.
Sure enough, a hot soldering iron
and a shiny solder joint later, the analyser sprang into normal operation.
I wonder if this is a form of electrolysis. Three different metals are
in contact: the plating on the battery
spring clip, the copper PCB track and
the solder.
With the passage of time and current
passing through it, the solder joint deteriorated. The voltage drop was not
enough to stop the self-analysis or the
display working, but it was sufficient
SC
to trigger the fault code.
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