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SERVICEMAN'S LOG
Rocking Raucous Retro Roland Repair
Dave Thompson
I’m trying to stay positive despite the world falling apart around my
ears. Earthquakes, plagues, waves of misguided activists – they’re all
conspiring to ruin what’s left of our idyllic way of life. At least customers
still occasionally find their way to me, with devices that sometimes can
still be repaired; in this case, a throwback to the 1980s. And that’s just
fine with me, because they knew how to build fixable gear back then.
Items Covered This Month
• Rocking Roland repair
• Samsung aircon repair
• Fixing LED light fittings
• Repairing a water heater and
•
•
•
key-fob
Multiple LED downlight failures
Repairing a TV with constantly
decreasing audio levels
Fixing outdoor lighting
*Dave Thompson runs PC Anytime
in Christchurch, NZ.
Website: www.pcanytime.co.nz
Email: dave<at>pcanytime.co.nz
siliconchip.com.au
W
e live in ‘interesting times’. The
pandemic is disrupting lives, if
not directly through infections, then
by hammering businesses through the
collateral damage of lockdowns, and
a drop in people being able to go out
and buy goods and services. The economic toll is becoming increasingly
apparent and harming us all.
There is also significant lobbying
going on from all manner of crackpot pressure groups trying to make
everyone’s lives worse. They might
not see it that way, but there’s no
escaping the reality. I get the feeling
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that so many policies these days are
not being thought through, especially
with politicians now taking advice
from school kids rather than listening
to the experts.
In the electronics world, I’ve been
worried about how getting older is
affecting my ability to do fine repair
work, but I also have all the above in
the back of my mind, which doesn’t
help my state of mind.
Work, while sparse, is still coming
in. Recently, a Roland Juno DX2 keyboard came into the shop accompanied
by its owner. It had simply stopped
August 2021 61
working. Not only were there no dulcet tones one usually associates with a Juno, there was nothing at all. No
lights, no power.
These vintage 80s-era keyboards are now quite sought
after for their genuine ‘analog’ retro sound, so its owner
very much wanted it to be fixed. I told him that, in theory, everything was fixable – if not by me then by someone with more experience – and it all really depended
on how deep his pockets were.
As with many musicians, it turns out his pockets were
not very deep at all! Quite shallow, in fact. I advised
him that I would assess it and then let him know what
was ailing the machine, and it would be up to him as to
whether he wanted to carry on. But it was also up to me
as to when to pull the pin on any given job, which is part
of our serviceman’s creed. He agreed.
He had already done some of the work in taking all the
screws out from the bottom and cracking the case open,
so that saved me some time.
He could get this thing apart so easily because he didn’t
have any of those stupid security fasteners to deal with.
Manufacturers back then were usually sensible, making
products that were able and meant to be repaired, with
any proprietary spares usually available from dealers (for
a good while at least). The electronic components used
throughout were often available from any good local electronics store.
Access to the circuit boards was usually good as well,
with no break-away plastic clips or similar impediments
restricting any attempts at repairs. I liked that philosophy
then, and I like it now.
Dead on arrival
Testing this thing was also simple. I plugged in the supplied power lead and hit the “On” button. Result: nada.
Zilch. Bupkis. Nothing.
The first thing to do was to test the power supply. Many
a repair has come unstuck because the serviceman overlooks the patently obvious; that the lead or power supply
has failed. It’s easy to do, and I’ve done it myself many
times, being too keen to roll up my sleeves and get stuck
into a job. One must temper one’s urge to get into it and
test the obvious first.
In this case, the power lead is likely as old as the
machine, and without knowing its history, it could very
well have fatigued and failed. The obvious test is to unplug
it from the keyboard and stick a couple of multimeter
probes into it in a way that I could wiggle it around and
ring it out without electrocuting myself.
This I did, and I got a healthy 240-odd volts AC no
matter what I subjected the cable to. So I was happy that
it was OK.
The next step was to plug the cable back into the keyboard and test some points in the power supply circuit
board. This was separate from the rest of the circuitry and
easy to spot, given the transformer, capacitors, diodes and
associated leads connecting to it. I love this older hardware; everything is so obvious as to what it does.
A quick probe around the board showed that mains
potential was going into the transformer but not coming
out. This is quite unusual; transformers are one of the
most basic of all electronic components and for one to
fail is, in my experience, quite rare. I mean, if there’s a
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lightning strike or other huge power anomaly, then yes, a
transformer can burn out, but in ‘normal’ use, it is unusual.
A transformer is essentially just two coils of insulated
wire wound onto a soft-iron core; how those coils are
arranged determines what type of transformer it is.
In the Dominions and other areas where 220-240V is
the norm, the primary and secondary windings will be
different than in the USA and other territories where the
mains voltage is 110-115V. If a device is intended to be
used in either location, it will often have two 110-120V
primaries that can be connected in series for 220-240V
operation or in parallel for 110-120V operation.
This is one reason why many modern appliances (computers, printers etc) have a separate power supply; the
basic machine runs on the same internal voltages, it is
just the supply that differs. Of course, these days, most
of those switchmode supplies can run off a wide range
of voltages, like 90-250V AC, so they are suitable for use
worldwide.
Obviously, if there is a frequency-dependent component in the device (that is, it needs the 50Hz or 60Hz signal as a reference to operate), the internal power supply
will vary between countries. In this case, however, the
Juno was designed to be used in this part of the world,
with 220-240V AC mains.
I removed the power supply board, a simple operation
with only four PK-style screws holding it down, and then
desoldered the transformer leads from the board. With the
board resting safely on the chassis, I used my non-Variacbranded Variac to slowly apply AC voltage to the circuit
downstream from the (now removed) transformer.
With my multimeter probes attached to the board’s outputs, I expected to see whatever DC voltages the board
was designed to provide. Sadly, I got nothing; perhaps
there was more to this than I thought. While I’d need the
right transformer, I might also have to see what else was
damaged before I could resurrect the Juno.
I had hoped I might get lucky, but usually, by the time
a transformer blows, there is a lot more collateral damage due to unusually high secondary voltages being produced as it fails. Even though there is a fuse, by the time
that blows, a lot of harm can already be done. I might still
have many more problems to sort out, but I would have
to replace this transformer to find out.
The appeals of retro
Did I mention I love working on older stuff like this?
Each section of the keyboard’s functions sits on a separate
circuit board. The VCO (voltage controlled oscillator), VCF
(voltage controller filter) and the VCA (voltage controlled
amplifier) sections are all separate. The same goes for the
keyboard processor, signal processing and audio amplifier sections. If one section fails, a new (or repaired) PCB
can simply be installed, and regular operation resumes.
This philosophy is unlike how modern instruments are
produced, where everything is typically on one big circuit board with propriety COB (chip-on-board) ICs and
no spares available from the manufacturer. Even worse,
no circuit diagrams generally are provided, whether you
are a repair agent or not.
If something goes wrong, you usually have to chuck the
whole thing away (into a landfill) and pay an exorbitant
price for an entire new keyboard, as the cost of repair is
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so high. Nowadays, it seems to be all about IP (‘intellectual property’) protection and making hyper-consumable
products with almost zero ability to repair.
Back then, for better or worse, they used standard parts
and standard (if increasingly clever) circuitry to achieve
what they wanted to do. Foreign powers with commercial aspirations often hijacked these designs, calling the
resulting device something else, but essentially cloning
and copying the original company’s design.
Affected manufacturers responded by making it increasingly difficult to reverse-engineer their products, usually by using proprietary parts and making spare parts or
components and replacement circuit boards increasingly
unavailable, meaning repair was simply not an option.
No wonder people are up in arms about huge increases
in e-waste and the rise of built-in obsolescence!
I’m actually with them. This is just wrong, and while
it might be great for IP protection, I don’t think it’s the
best way forward.
However, as our Juno 2 has discrete components on
separate boards, it is a veritable dream for a serviceman
like myself to fix.
So it seemed that the problem with this machine was
in the power supply board. I was hoping that if I could
resolve this, the rest of it should still be OK. But like any
good mystery, I wouldn’t know until I got the power supply board working.
I do know that many of these older analog ICs were
pretty hardy devices in their day, so the lack of any obvious burned-black spots on the other PCBs, holes in chips
or that distinctive stink of burnt electrical components
was a good sign. I was reasonably sure that once I got the
power supply board working, the rest of it would start
up again and start producing sounds. Fingers crossed!
To be thorough, I should test every component on the
power supply board. That’s not too onerous a task, to be
frank, because there is not much on it. There is a diode
rectifier array, two relays, a regulator, a few capacitors
and a fuse.
The fuse had not blown, so that usually indicates a lack
of shorts. The regulator is a standard 78XX type, and the
capacitors and diodes are all common components. All
are clearly marked, as is the PCB assembly. To really save
the planet, modern manufacturers should take a hint from
the way this keyboard is manufactured.
My first check was to measure the transformer’s output, and I got nothing, indicating that at least one of the
windings was open-circuit.
Fortunately, the transformer has a part number on it, but
a quick Google search found nothing relating to it. The great
news is I have a commercial transformer-winding machine.
The bad news is that I would have to dig it out of storage in
my garage to use it, and that idea wasn’t appealing at all.
The good news is that I got about a hundred miscellaneous transformers when I bought the winding machine,
but the bad news is I’d have to trawl through those transformers to find a suitable replacement for this one. The
good news is that I didn’t have to! I had a Jaycar replacement in the drawer that would not only fit, it would also
be suitable electrically. That really is excellent news...
This was not so surprising, as all I really needed was
a mains transformer with a 12V AC output with a reasonable current capacity, and those are a dollar a dozen.
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August 2021 63
Removing the old one was simple, and
replacing it almost too easy. Surely this
repair couldn’t be this straightforward.
Once I had replaced that, I powered
the machine on and... nothing. I knew
this was too good to be true.
I now had 12V AC, but nothing past
the diode array. Out the board came
again, and this time I replaced the
existing diodes with four 1N4001s.
Desoldering these old boards can be
tricky, but I have to say I love the smell
of that old solder; it brings back many
memories. I replaced all the diodes,
and for good measure, the regulator as
well while everything was out.
After reassembly, I hit the power
button with expectations of it all working – and it did! The display and all
the lights lit up as they should. With an
amp plugged in, I hit a few notes and
was rewarded with that warm, mellow, smooth, rich, laid-back, melodious, euphonious analog sound. Thank
goodness for that!
While I likely could have fixed other
parts of the circuit if necessary, I was
glad that I didn’t have to work my way
through it all. The time involved alone
would have deterred the owner, and he
likely would have bailed on the project. At least now I could tell him that
he would probably have many more
years of use from this beautiful vintage keyboard.
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He was over the moon, and although
he said he thought it would be an “easy
fix”, he doesn’t know the half of it.
Samsung air conditioner repair
N. K., of Kedron, Qld likes to wield
a soldering iron to repair written-off
devices. It’s part of his hobby, and he
enjoys the challenge of solving mysteries and saving a lot of money at the
same time. In some cases, there is a lot
to gain and little to lose...
This one was brought to me by my
son. His friends, a young couple with
small children, had their air conditioner written off by the repairman
in the middle of Brisbane’s hot and
humid summer. It was an old Samsung
split system, and apparently, replacement boards are no longer available.
They could ill afford the $2700
quoted for a new system, so my son
generously offered to take the boards
so he (meaning me) could check them
at the component level. So I could not
test them in operation. The boards
were the indoor and outdoor unit
power supplies, the display board and
the controller board, hosting the main
microcontroller and several other
surface-mounted ICs.
The repairman said he found dead
geckos on both power supply boards
and blamed them for the failure. I
found evidence of fried gecko on both
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boards, but the marks were confined
to the mains areas of the boards. So
I doubted that was the real problem.
They reported no lights on the indicator panel and the system was completely unresponsive.
I figured that if the problem was
with the outdoor power supply, or anything else outdoors, the indoor indicator lights should still come on. The
outdoor unit is a linear supply with
a conventional transformer followed
by a four diode rectifier bridge. The
fuse was intact. It’s only used to power
relays anyway, and the diodes tested
OK. There are no Mosfets, so I was
confident the problem was elsewhere.
I looked briefly at the indoor indicator board and saw nothing visually
wrong. There was not much I could
have fixed there anyway, so I put it
aside. Likewise, the complex controller board looked intact. So I dismissed
it as both unlikely and too hard.
That left just the indoor power supply board. Its fuse was also intact. It is a
switchmode power supply with 230V
AC directly rectified to 325V DC. The
rectifier bridge checked OK with my
multimeter, as did the 400V electrolytic filter capacitor. Tracing the tracks
on the board, this fed a TNY266PN offline switcher IC, with Mosfet switches
to chop the DC into the primary of the
step-down transformer.
The secondary, low voltage side
of the transformer went to a single
half-wave schottky rectifier diode
followed by filter capacitors and a
small KA78L05AZ linear 5V regulator. There were other components, but
they either checked out OK or did not
look like suspects.
Testing the schottky rectifier diode
hit pay dirt. It was short circuit. However, without expensive test gear, I am
always suspicious of the black magic
lurking in switchmode supplies.
You can never tell if something else
failed first, damaging the diode, or if
the diode failed and took other components with it. In any case, I never
trust the Mosfets in a failed switchmode power supply.
That TNY266 could have refused to
power up due to a sensed low impedance on the primary of the transformer,
caused by the shorted diode on the
secondary. This, coupled with my
overall suspicion about failing Mosfets, led me to replace the TNY266 as
well. I could not tell if the KA78L05
5V DC regulator had been damaged by
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the failed rectifier diode, so I decided
to replace it too.
The replacement components only
cost a few dollars, plus $25 for shipping. I could not find an equivalent
axial lead schottky diode, so I used a
surface-mount equivalent, soldered to
two posts on the board.
It was all a gamble, but when my son
reinstalled the boards and reconnected
the power, the air conditioner sprang
to life and started doing its job. So I had
the thrill of the hunt, the satisfaction
of success, and a suitably impressed
son. This also resulted in a very grateful couple and a disappointed air conditioner salesman.
Fixing LED light fittings
J. N., of Mt Maunganui, New Zealand, had a go at fixing light fittings
with failed individual LEDs...
I had to replace an outdoor light
because it had become too corroded
and the housing was letting water in.
Fortunately, I had a spare replacement
Arlec ABL003 LED unit on hand.
After installation, all went well for
about three weeks until the light failed.
As I am a retired technician and it was
out of warranty, I decided to see if it
could be repaired. After removing the
cover, nothing seemed out of place, so
I removed the unit to my workbench.
I discovered that it had 18 LEDs in
series, powered by an AC-to-DC converter.
I applied power and verified that it
was producing a reasonable DC voltage. Next, I tested the LEDs and found
that two were faulty (marked with red
arrows in the photo below). I couldn’t
be bothered replacing them even if I
could find replacements. Then I realised that I could simply short out the
two faulty LEDs by applying solder
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across them. Upon reapplying power,
bingo, the light worked!
To be on the safe side, I decided to
add a 2.2kW resistor in series with the
LEDs to reduce the current through the
remaining LEDs to a similar level as
it would have been with all of them
installed.
After a soak test of 48 hours, I reinstalled the light which is still working
well after two months.
Repairing a small water heater
and a faulty key-fob
K. D., of Chermside, Qld, had to make
two repairs recently, both of which
involved fabricating new parts. In both
cases, those new parts are far superior
to the failed ones that they replaced…
I was asked to look at a small unit
that heats water to about 40°C and circulates it through a mat. Made thirty
years ago, the device had initially been
used to keep premature babies warm.
It had long been made obsolete from
that job and repurposed for use in the
laboratory. The complaint was that the
unit wasn’t heating the mat.
There were four likely points of
failure: the element, the control electronics, the pump or the plumbing.
Looking at my notes, I had previously replaced the cartridge heater in
this unit.
The original element was 3/8-inch
(9.5mm) in diameter, and the only
replacement I could get with suitable electrical ratings was 10mm in
diameter. That necessitated the careful reaming of the thin-walled pocket
the element fitted into with a chucking reamer.
To quickly check the element and
control electronics, I measured the
power consumption of the unit. I
found that the element was clearly
Australia’s electronics magazine
being cycled on and off by the control electronics. That meant that the
failure was most likely in the pump
or the plumbing.
I disconnected the hoses, and the
lack of flow or suction confirmed that
the pumping system or plumbing was
at fault. Water drained passively from
the hose connections, though, indicating that there wasn’t a major blockage
in the piping. That left the pump itself
as the likely culprit.
With the cover removed, I could feel
that the rotor of the pump motor was
turning, so the impeller had to be the
source of the problem. Splitting the
integrated pump/heater block required
complete disassembly of the unit. All
I found in the pump chamber was a
protruding shaft. There was simply
no impeller to be seen!
I did find, however, lots of tiny
pieces of Bakelite or phenolic material in the chamber and the water passages. Reassembling these like a jigsaw
gave me a flat piece ~40mm x 4.5mm
and about 0.8mm thick. It was a very
simple impeller that must have been
attached to a flat on the shaft with a
couple of spots of glue.
I thought of various ways to replace
the impeller, such as making one from
a brass shim or PCB material either
glued or soldered to the shaft. Then I
realised that I could 3D print a better
impeller that would be a press fit and
held in position by the flat section on
the shaft.
I quickly drew a simple design in
a 3D modelling package and sent the
file off to a colleague for printing. A
few days later, I had an impeller ready
to fit. It was a snug press fit onto the
shaft and turned freely in the pump
chamber. When reassembled, the
unit pumped far better than anyone
remembered.
The next repair began when I
watched a friend unlock her 2001
Toyota Camry with the key and not
the key-fob remote control she usually used. Some questioning led to
the explanation that a water bottle
had leaked in her bag some days earlier, flooding the remote which had
stopped working.
It was apparent how the water had
gotten in as the rubberised button had
perished and fallen out several years
ago, leaving a large opening through
which the small PCB-mounted switch
could be operated directly.
Looking into the hole, I could see
August 2021 65
several surface-mount components
with white corrosion on their leads. I
pressed the button a couple of dozen
times, and the car responded twice, so
I thought it would be worth attempting a repair.
The remote was obviously never
intended to be serviced, as the case
was glued together. Some leverage
split the case at the join, revealing an
oval PCB containing all the components, including a soldered-in coin
cell. Most of the corrosion was near
the button and was easily removed
with a fibreglass pencil.
I then washed the board with isopropyl alcohol. After a couple of days
drying in the sun, the car responded to
every press of the button. I masked the
switch with tape and gave the board
a generous coat of Electrolube HPA
conformal coating in case of future
water ingress.
Next, I had to make a new button. I
covered the outside of the hole with
tape and filled the recess from inside
with Dow Corning 3140 conformal
silicone. Once cured, and after some
trimming with a scalpel, I had a pliable
button thoroughly sealed to the case.
That left re-joining the case itself. I
chose not to glue it, in case I ever had
to change the battery. Instead, I used
Permatex Form-a-Gasket compound
to adhere the case halves together
with a watertight joint. The remote
has worked for many months, with
the homebrew button and case joint
still in place.
Multiple LED downlight failures
R. H., of Ferntree Gully, Vic, must
have been busy fixing LED downlights
as he has had quite a few fail, as he
relates...
I was prompted to write this by the
LED lamp repair story (Serviceman’s
Log; May 2020, page 51). I replaced all
our ceiling lights with 12W multi-LED
lights of two different brands. Over the
last two years we have had sweltering
summers, and this appeared to precipitate failures in these lamps.
Also, when I installed the first lot
of three LED lights in the kitchen, I
found that we could not watch TV
due to interference. I put about six
ferrite rings on each light power cable;
that reduced the interference so we
could at least watch most TV channels. I ended up shifting the antenna
to another side of the house using RG6
quad-shield coax.
I then installed another two lights
in the dining room, and the second
bedroom (my office). I put six or so
snap-on ferrite rings on each of the
mains power cables again, but still
got interference! I can only watch TV
with the lights off.
As these two rooms were in line
with my aerial and the Mt Dandenong transmitter, I had to do another
antenna shift; this time positioned
so the antenna points away from the
house. I also added a masthead amplifier to improve the S/N ratio. We can
now watch TV with the lights on.
When the weather gets really hot
(around 40°C), the roof cavity gets to
nearly 60°C, and the LED lamps measure 40°C+ on their faces. Initially,
one LED in the group of a dozen or
so LEDs in each offending light will
flicker annoyingly on/off.
Fortunately, at the time of our LED
light installation, I purchased an extra
spare LED lamp per room. As all the
new lights have been fitted with a GPO
power point in the roof loft, it was easy
enough for me to swap the failing lamp
for one of my spares.
With multiple lamp failures, rather
than throw them away, I have been
able to swap good LEDs from a failed
unit onto another failed unit to make
it work properly again. For our seven
installed multi-LED lights, I have
changed about 20 individual LEDs on
the 120mm aluminium platter.
After marking and disassembling
the faulty lamp and identifying the
LED polarity, I get out my mini gas
flame torch. With the 2cm flame burning vertically, I hold the LED platter
with pliers and place the faulty LED
above the flame.
After about five seconds, I can lift
off the faulty LED with tweezers and
repeat the same to retrieve a good
LED from a spare (wrecked) LED
light. Again noting the polarity of the
replacement LED, I put it where the
faulty LED was removed, heat it again
with the gas flame (from the reverse
side) and the LED will ‘magically slip’
into place using the existing solder.
If you look carefully at the LED
array photos (mine shown below, and
the one published in the May issue),
the faulty LED has a black spot. Pretty
much every faulty LED I have found
suffers from this black arcing spot. The
string of series LEDs fails at the point
of the weakest LED, and once it has
gone open-circuit, the whole string
won’t work.
The only other fault I have encountered with these LED lights (and with
CFLs) is the 2.2µF (sometimes 4.7µF)
400V electrolytic capacitor having a
swollen top. Replacing that capacitor
usually fixes it.
Repairing a TV with persistent
lowering of audio levels
L. J. C., of Forest Hill, Vic, has a story
about an electronic fault that had an
unusual cause, leading to a very frustrating intermittent fault...
In 1965 my father in law, who lived
Burnt spot
on faulty LED
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in a Victorian country town, bought a
new TV. I don’t recall the brand, but it
was Australian made. It worked well
for a few weeks, then developed an
annoying fault.
While you were watching it, the
audio level would slowly decrease,
so you would have to get up and turn
the volume up. This would continue,
so you had to keep turning the volume
up periodically until eventually, it was
at full volume.
After a while, presumably due to a
power line spike when a motor turned
on or off (eg, a fridge), the fault would
disappear, so you had to jump up and
turn the volume down! Then, after a
few minutes, the cycle repeated; it was
most annoying.
He had the shop’s TV technician try
to fix it a few times, but he never succeeded. Eventually, the set went out of
warranty, so I asked him if he would
like me to fix it. He agreed.
I removed the rear cover; in those
days TVs had a circuit diagram conveniently pasted inside. It was essentially a valve TV, but it had transistor
audio IF and audio output amps.
I was a telephone technician, and
my boss had recovered an old TV chassis from the rubbish tip, so I inserted
the audio IF and output amp valves in
and connected a speaker to use it as
a signal tracer. I connected the input
of the signal tracer’s audio amp to the
input to the set’s audio amp. I then
switched the set on, and waited for
the volume to decrease.
I determined that the fault was in
the audio IF stage since the level coming from both speakers decreased. But
when I attempted to measure the collector voltage on the first IF transistor, the transient caused the volume
to leap back to the original level.
Frustrating!
I reasoned that the fault might be
temperature sensitive, so I put a radiator at the back of the TV to warm up
the components (my mother-in-law
was not impressed). When the volume eventually reduced, it remained
low while I made the measurements.
I connected the input of the signal
tracer’s IF amp to the collector of the
first IF transistor and found that the
audio level coming from the signal
tracer’s speaker was also low.
Looking at the circuit, I noticed that
the IF coil was tuned by a 560pF plastic film capacitor. In those days, plastic
film capacitors were cylindrical. They
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The internals of a
typical garden LED
light.
were made by rolling plastic dielectric
films with the conducting films, with a
pigtail wire emerging from both ends.
I concluded that the connection
between one of the pigtail wires and
the respective metal film was faulty, ie,
there was a thin film of oxide between
the wire and the metal.
When the set was switched on, the
transients broke down the insulating
film, so the volume was normal. But,
as the cap warmed, the insulating film
started to reform; thus, the capacitance became smaller, hence gradually
detuning the IF stage.
But when a transient occurred,
either from the mains or me attempting to make a measurement, the insulating film broke down. It became a
good Ohmic connection for a while
until the insulation started to reform.
The gradual detuning by the IF amp
reduced the signal level going into the
next stage and the FM discriminator,
thus reducing the volume.
I replaced the capacitor with a new
one and thus solved the problem.
Fixing simple outdoor lighting
F. F. C., of Sydney, NSW likes disassembling broken things and investigating the build quality, finding and
fixing problems etc. The subject of this
current letter is those cheap outdoor
solar lights that are known to fail frequently...
These lights are attractive for garden areas, outdoor steps etc because
you don’t need to run any wiring to
them, and of course, the low cost is
the other attraction.
The problem is that they never seem
Australia’s electronics magazine
to last very long.
That low cost means that it’s tempting to throw them away when they
stop working and buy another one. But
often, the fix is quite simple. Opening
them up is usually not too difficult,
and all you will find inside is a solar
panel, a battery, one or more LEDs and
a small control board with a handful
of components. The ‘battery’ is often
a single 18650 Li-ion cell (nominally
around 3.7V).
If you need a circuit diagram, use
your favourite search engine to look
up the part code printed or etched into
the main chip. As you can see from
the photo above, there are only three
parts on the tiny PCB. One of the components is a commonly found 4-pin
part in a SIL package.
If one of these lights fails within
the first year or so, the most common
cause is corrosion of the battery contacts. While the housing should theoretically be sealed, moisture might still
make its way inside, and the contacts
will quickly become rusty. That will
prevent the battery from charging. Of
course, the battery itself can fail over
time, but it usually lasts a few years
under normal conditions.
Another possible failure point is in
the wiring to the solar panel, which
can be quite fragile. Keep that in mind
when you disassemble and reassemble the light to fix it. You could fix the
original problem and create a new one
if you fracture those connections!
The circuitry is so simple that it is
unlikely to fail. If it does, you can generally swap the board from another
light with a different failure.
SC
August 2021 67
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