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SERVICEMAN’S LOG
A mixed bag of odds, sods, ends and bobs
Dave Thompson
It’s sometimes a bit of a curse when people around the neighbourhood
discover that I can do repairs on electronics and anything else vaguely
related. I’ve had my fair share of food processors, heaters, amplifiers and
CD players turn up just through word-of-mouth referrals.
Don’t get me wrong; I welcome anything as a challenge. However, while
sometimes the results are positive, that
isn’t always the case.
Recently, I had an 80s-era Phillips
CD player through the workshop.
This thing was likely audiophile quality back in the day, and the price tag
(still stuck to the top) confirmed that
at $3500 Kiwi bucks, you’d have to be
a serious audio guy to buy it.
I don’t think – aside from a house
or a car – I’ve ever paid that much
money for anything! Some of my old
audio gear and guitars were getting
up there in price, but 3.5 big ones for
a CD player? Not for me!
Anyway, this player had a problem.
It would no longer open, and I got the
impression the owner was more interested in getting the CD out of it than
an actual repair. As with most older
devices, getting any spares for it – like
another CD player module – would be
problematic.
I told him what I tell most people in this situation:
I’d open it up and
have a look, and
if I can do
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anything with it, I will; but if I can’t,
well, that’s all there is to it.
The machine was built like an external masonry water closet. Where one
screw would suffice, they used three.
All the plastic parts were also clipped
onto the steel chassis. They certainly
knew how to make stuff back then!
None of this glue-the-two-halvestogether and throw-it-away-if-something-goes-wrong business.
One thing they didn’t do was round
off the stamped chassis edges. Not
only was this unit really heavy but the
exposed metal edges were like guillotines. As I’ve been caught before, slicing my hands open on poorly-finished
metal fittings, I knew this time to be
extremely careful how I handled it.
I once picked up a heavy amplifier
case and the sharp-edged chassis cut
into all my middle knuckles. I couldn’t
hold anything for weeks, which is a
major pain in the rear (among other
body parts). Lesson learned!
I disassembled this CD player and
when I got inside it, I discovered that
the CD module was like nothing I’d
seen before. I was hoping that it
would at least be similar to the
modern-day units you get for
computers, DVD players and
stereos, but no, it was completely different.
Even the connections
to it looked proprietary.
Although the module
was clearly labelled with
part numbers, as usual,
I couldn’t find any relatable information on the
web about it; no service
manuals or circuits for it
anywhere. I also searched
the likes of eBay and other
auction sites to no avail.
I went back to the
Australia’s electronics magazine
machine and looked to see if I could
pinpoint what was actually going on
with it. On power-up, the CD player
just sat there hunting, as if looking
for a disc. It wouldn’t open as it was
working, and that’s all it did. Disc in
or not, it just sat there looking.
I suspected the laser had failed, and
that’s what the rest of it was waiting
for – the laser to report a disc was
present, then it could complete booting and carry on.
I have dozens of laser modules
removed from CD and DVD drives;
perhaps I could adapt one of these to
this drive? Once again, it was all so
different, and the laser module itself
was a heavy-duty thing that looked
like even a hammer wouldn’t touch it.
I couldn’t even see the laser diode as it
was embedded well inside the carrier.
I could possibly get the old one out,
but only using drills and such, so that
wasn’t going to fly.
Part of being a service or repair guy
is knowing when to pull the pin on a
job, and for me, this was that point. I
had the disc out; all I had to do was
manually turn the drive door pulley
while there was no power present,
opening the drawer bit by bit until I
could move it all the way out.
I reassembled the thing and, against
all hope, tried it again, just in case
the drawer would open and the thing
would magically work. But no, it was,
as far as I was concerned, end-of-life. I
suggested to the owner that he might
get more success from an established
repair agent, who might have spares
that would get it working, but he
agreed that it had its day and it was
time for a new one.
At least I got the disc out of it.
The next odd job
Another neighbour arrived out of
siliconchip.com.au
Items Covered This Month
• A mixed bag of odds, sods,
•
•
ends and bobs
Fixing the motor in a burnt-out
clothes dryer
A Kriesler radio and its
capacitor firework
*Dave Thompson runs PC Anytime
in Christchurch, NZ.
Website: www.pcanytime.co.nz
Email: dave<at>pcanytime.co.nz
the blue and asked if I knew anything
about trailer lights. He’d recently
had his trailer refurbished, with new
incandescent taillights and an LED
number-plate light and some of the
cabling replaced. But some of those
lights had already stopped working
properly. Could I take a look?
I suggested he should take it back to
the people who’d refurbished it, but
he said he already had several times,
and they couldn’t find a fault in their
work and weren’t prepared to spend
any more time on it. I thought that was
a bit rich, but the guy was clearly troubled by it, so I said I’d have a look over
it and see what I could do.
This was a standard trailer; nothing
flash, just the sort of thing you’d fill
up with rubbish or soil of a weekend
and do a garden or dump run or similar. The lights and lenses all looked
relatively new, as expected, but when
hooked up to his car, he had no tail
lights, and a brand-new LED numberplate light also didn’t work.
The indicators did work, so that was
something.
The first thing I did was hook the
trailer up to our own car; I wanted
to rule out problems with his car’s
fuses, power leads and trailer plug.
Even though they are pretty hardy,
trailer plugs can get a real hammering, and people can accidentally drop
the trailer hitch onto the plug when
moving the thing around, crushing it
between the hitch and the road.
However, once hooked up to our car,
I got the same result as he did, indicating some kind of fault in the trailer
wiring itself.
This isn’t exactly rocket surgery;
it’s basically a big tow-able wheelbarrow, but the inclusion of a wiring loom
apparently elevates it to another level.
In New Zealand, we use a heavyduty plug with seven contacts, and
this plug hooks into a handy socket
mounted on the car once the trailer
is connected. I imagine it is the same
connector used worldwide, but I don’t
know for sure. Once connected, the
indicators, brake lights and any other
ancillary lights hooked into the system should ideally mirror the actions
of the various rear lights on the car.
My first step was to measure the
voltages from the car’s socket and
check that no shorts or high-resistance
joints were dropping the voltage.
When I turned the lights or indicators
on, or applied the brakes, I read the
expected 12V (or near as reasonable)
at all the correct pins.
While colours for trailer wiring are
supposed to be standardised, and most
trailers are wired up correctly, there
are plenty out there – perhaps built
before the standards came in – with
non-standard cabling.
The wiring on this particular trailer
was not standard, which made things a
bit trickier. But due to the open nature
of the plugs and sockets, one can readily deduce what coloured wire connects to what part of the circuit.
And there’s another problem; ringing out a trailer loom with one person
is tricky; I don’t have a three-metre arm
span, nor do I have one of those tools
for measuring connectivity in longer
wiring looms.
I ended up just using a small jumper
lead with alligator clips at each end
and connected one clip to a good
clean spot on the trailer chassis and
the other clip to each pin in turn at the
connector end. I then used my multimeter with the buzzer function set to
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December 2021 69
span the ground and ‘live’ connections at the other end.
It’s a bit of a faff walking backwards and forwards to set
the clips, but with only seven big pins, it’s easy enough
to do. I got identical results to the car-plugged-in tests,
as expected.
I took the non-working incandescent bulbs out of their
sockets and tested them with the meter as well – all were
fine, but I wanted to be thorough. Too many times, I’ve
jumped the gun and had to backtrack over some silly
missed problem like a blown light globe.
Chasing a cable fault
It appeared there was a lack of connectivity somewhere along the loom that connects the trailer socket to
the lamps. The question was where. Two cables made up
the loom on this trailer; both ran down a natural channel
formed under the right-hand chassis rail before splitting
at the right-rear light, and a single cable ran across the
rear underside of the trailer and up to the left-hand light.
Both were four-wire cables about the size of a standard
mains lead and were strapped – some very tightly – using
cable ties both together and to the chassis rails.
Detecting breaks in longer cables is a bit of an art in
itself, and while there are many methods using special
tools and Wheatstone bridge-based machines and the like,
I checked them using a ‘quick and dirty’ method.
Using the jumper cable and multimeter once again, I connected one of my many dental picks to the non-grounded
multimeter lead. I could then simply pierce the cable insulation and measure continuity along the length of the main
cables, shifting the ground lead as I went along the loom.
There’s a certain amount of educated guessing as to
where the wires run within the insulation, and one could
argue it exposes the inner wires to the elements. Still, the
pick is so fine, and most trailer connections are exposed
to the weather anyway, I didn’t see it as a problem. The
main problem is the dental pick is dangerously sharp, so I
had to take care not to miss the cable and find my fingers!
At one of the tight cable tie points, I lost connection
with the white wire in the bundle. This wire was terminated at the right-rear lamp, where it was split off using
one of those plastic-coated inline crimp connectors to one
wire leading to the LED number plate light.
There was another similar connector for the second
LED wire. That could explain why this wasn’t going
either. That whole rear section of the loom was covered in
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poorly-applied insulation tape, which I consider unsuitable for wiring sitting out in the weather. I’d have to re-do
all that once I worked my way down there.
I clipped the cable ties all along the loom down to the
section where I thought it might be broken and marked that
area with a bit of tape to avoid losing my place. I removed
the cables from the right-rear light assembly and pulled
them back through the chassis rail so I could easily get
to the dodgy section. This would also make it easier to
add proper heatshrink tubing where needed eventually.
I was a bit surprised to find that the wiring simply enters
the body of the taillights through a largeish hole in the
backplate. In my opinion, this is a design flaw; as the lights
hang directly behind the wheels, they can fill up with water
and road grime flung up from the tyre through that hole.
Now for the tricky part, peeling away the insulation
around the fault. I didn’t want to replace the whole loom
from front to back but would do so if push came to shove.
I’ve in-lined joints before, and that shouldn’t be too much
of a problem on a low-voltage system.
I carefully split the insulation on either side of the suspected fault with the tip of a craft knife about 5cm along
the ‘grain’ of the cable, being very careful not to carve
anything else inside. Now having access to the crushed
section, I could move the other three wires out of the way
and check the white wire.
I simply pulled on it a little, and a small section of insulation stretched, telling me the wire inside had parted
company. I snipped it at that point and, sure enough, cut
only through the plastic.
Of course, if I stripped back the insulation and simply
re-soldered this wire together, it would be shorter than the
others, creating a messy join. Instead, I stripped it back
on each side and installed some heatshrink tubing before
using a brass ferrule to make up the length difference.
A thorough crimp had it back to size without a lot of
bulk, and after shrinking the tubing over the ferrule with
a heat gun, I fed suitable large-sized self-amalgamating
heatshrink tape down to cover that area of the loom. Once
again, the heat gun had the tube down to size, and the
amalgamation would see it well-sealed in there.
Almost there
With that area done, I went back to the rear end. I fed
the loom roughly back into place and reconnected everything back to the light assembly. I wanted to test it before
I went any further.
This time, when it was all plugged in, I got brake lights
and tail lights but, frustratingly, still no number plate
light. Looking at the mess of how it had been connected
into the loom, there was no wonder. Once again, I got
the multimeter out, and while I had voltage to the point
of the connectors that split the loom off to the LED, I got
nothing after them.
Hopefully, all I’d need to do is replace those inline connectors to get it working because the LED assembly had
been riveted to the tailgate, and I didn’t want to have to
drill those big rivets out. They had already cracked the
plastic housing and I was reluctant to cause any more
trauma to it.
The people who had installed the LED had left plenty
of cable length, so chopping out the connectors wouldn’t
be a problem. I soldered those wires back together (after
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siliconchip.com.au
installing suitable heatshrink) and, when tested, it all
worked properly. I then took the loom back out and fitted more heatshrink tape – all this would tidy up that
insulation-tape mess.
Now when everything was reconnected and appropriately cable-tied, the lights worked a treat, and the wiring
installation looked a whole lot better. Job done!
I wonder why the original installers couldn’t figure it
out. You don’t have to be Wile E. Coyote, super-genius...
Fixing the motor in a burnt-out clothes dryer
A. L. S., of Turramurra, NSW had to take a guess at what
had failed so he could order a replacement part before
he’d disassembled the failed unit. His guess was close
enough to result in a successful repair...
Returning home one day, my wife came running out to
greet me with “there’s been a disaster!” Our 5kg Simpson
clothes dryer (39S500M) had stopped working and had
emitted clouds of smoke, setting off the smoke alarm and
filling the house with an evil smell!
The smell from this dead dryer was slightly different
from the usual burnt-out transformer smell that I was
familiar with. It had the odour of a stale ashtray. My wife
said it smelled like a car had done a burnout in the house,
but I put it all down to the type of insulation enamel.
My wife thought it was best to throw the dryer away
because it was over 20 years old, and I agreed. But when I
checked out the reviews of the newer high-tech programmable model, several reviewers gave it only two stars, and
a couple of buyers regretted buying it. That’s because it
has a sensor that is supposed to detect lower humidity
and shuts down the “program” when it sees fit.
The problem is that if the user disagrees with the decision of the dryer, they can’t dry the clothes for five or ten
minutes more if the items are still damp! My wife also
preferred the old-fashion timer and was very adept at setting the timer for various items.
So I suggested that I have a go at fixing it because I was
sure it was a burnt-out motor, and there were plenty of
second-hand and re-conditioned replacements available
online at reasonable prices. I could also find plenty of
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December 2021 71
other replacement parts such as drive
belts, timers and odds and sods, which
made me think that this model was
infinitely repairable!
She agreed but did not want me to
pull it apart yet to avoid a mess in
the laundry. So I took a gamble and
bought what looked like a pretty good
used motor (part #0214377106) for $69
online, which arrived after about two
weeks. I tested it on the bench with a
temporary AC mains supply, and it
seemed very strong and noiseless, so
it was time to operate and replace the
faulty one.
Before I could remove and dismantle
the dryer, the kindly next-door neighbour (who enjoys working out at the
local gym) helped me pull it off the
wall. I then set about removing the
screws from the back panel and took
off the small nut which held the drying drum in place.
Inside, I found three connectors: one
for the incoming mains, one for the
motor, and one for the heating element.
These are tricky because they are hard
to access; the sheet metal was really
sharp, and my wrists were in danger
of being slashed. It didn’t help that the
wires were very short, and there was
a narrow gap between the connectors
and the edges of the back panel.
I used thick leather gloves to help
separate them, and then I could
remove the back panel.
I then removed the drive belt from
the motor assembly and extracted
the big drying drum for cleaning and
inspection. The guts were full of dust
and lint, so I vacuumed it out to see
where all the screws were. I could just
see some burnt lint around the motor
capacitor. I used a 6.5mm socket on an
extended shaft to remove all the screws
holding the motor in place.
The fan and shrouding had to be
unbolted at the same time. Finally, it
all came out, and I was able to see that
the capacitor which was bolted to the
motor had a cavernous hole (which
was definitely not an inspection hole),
and it had oozed molten metal all over
the motor. The 8μF 450VAC rated
capacitor had overheated and spilt its
guts (shown below)!
That explained the smell; a burning capacitor smells different to burnt
windings. There was a thermal cutout, but this was mounted beside the
motor on a piece of tin. Since the motor
itself had not overheated, the full
mains voltage remained active across
the capacitor. Luckily, my wife had
switched it off as soon as the smoke
alarm activated; otherwise, it could
have started a fire.
Fortunately, the new second-hand
motor was identical to the old one
and also had the 8μF 450V capacitor
attached, which looked very fresh. So I
replaced both the motor and capacitor.
Before everything could be reassembled, I filled a bucket with the lint I
removed! My wife is very particular
and empties the external filter assembly before every drying cycle. Obviously, that was not enough to prevent
a huge buildup over 20 years. Perhaps
this contributed to the demise of the
This 8μF capacitor
had overheated and
leaked all over the motor.
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motor capacitor; the rear ventilation
slots were blocked, so there was no
air cooling.
Cleaning it up took me quite a few
hours; I had to use a hose to wash the
separated parts, allow them to dry and
then reassemble them carefully. The
motor bolted into place easily enough,
and I threaded the belt arrangement by
holding the tensioning spring back.
You need to settle the belt onto the
drum by rotating the motor by hand
for at least two drum rotations before
applying power; otherwise, it will
instantly throw it off.
Satisfied that all was good, I plugged
in the repaired dryer, stood well back
and set it going. It operated noiselessly and smoothly, and my wife and
I watched it for a few minutes just like
a new TV set. We were very happy that
we had saved a few hundred bucks getting our dryer back in action!
A Kriesler radio and its aluminium
capacitor firework
R. M., of Scotsdale, WA heard a
knock at the door, and it was his mate
Kevin, holding something that looked
like a spent firecracker. It wasn’t,
though...
“I got this really good looking old
radiogram, got it working, and it suddenly went bang! And I found this
inside!” said Kevin.
It did look a lot like a demised firework. About 12mm in diameter and
50mm long, tightly wrapped paper
and foil, with one end showing definite signs of having exploded.
When I realised the foil was aluminium, it clicked. I was holding the
guts of an old high-voltage electrolytic capacitor. Having been retired
for years, it had objected to suddenly
being hit with volts and responded
appropriately. A bit of leakage current, a buildup of heat and pressure,
and bang’s your uncle.
I offered to take a look at the radio,
and it shows up the next day. It was a
nice looking unit, a classic mid-20thcentury Kriesler in excellent condition. Someone had been taking very
good care of it – I caught a whiff of
furniture polish. Lifting up the lid,
there was the large glass dial with an
imposing array of knobs, and a record
changer in a recess to the left.
The cabinet was OK, but the innards
might not match. Removing the
Masonite back and a couple of long
screws loosened the top part of the
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deck, the dial swung up and released
the chassis. I wriggled it out and onto
the bench. I’d forgotten how heavy
these things were! The top looked
clean with no apparent damage, but
underneath was another story...
Within the usual tangle of pointto-point wiring, there was the empty
aluminium can of an axial electrolytic.
The end cap had been blasted away
and hung forlornly from its solder tag.
The once-liquid part of the contents
was a grey goo sprayed all over the
inside of the chassis. Luckily, it was
facing away from most of the circuitry
and expended its venom into a basically unpopulated corner.
One thing that had copped the lot
was the red active mains power lead.
The rubber insulation had decomposed over the years, and it was
stripped bare.
The only reason it wasn’t shorting
was that it was reasonably stiff and
well-anchored. With judicious use of
compressed air and a toothbrush, the
chassis cleaned up nicely. All the rest
of the circuitry looked good.
I decided to make some quick
checks to see if it was safe to proceed. I
plugged it into a Variac and cautiously
upped the volts. No smoke appeared,
and the dial lights and all the six valve
filaments lit up. I managed to connect
one speaker and got a lot of hum, but
also recognisable audio.
One pleasant surprise was a copy of
the circuit diagram stuck to the back
panel. It was a bit faded and discoloured. Editor’s note: we have supplied
another scanned version of this circuit.
There were four filter caps on the
high-voltage lines with their values
clearly marked. 32μF, 50μF, 16μF and
8μF. The local electronic suppliers
didn’t stock caps rated at 400V, but
element14 did, so I ordered all four
online.
Next, it was time to replace that
damaged power lead. Kev had thoughtfully looped up the slack lead and
secured it with a cable tie. It seemed
a bit long, and the plug looked modern, as did that end of the cable. I cut
the tie and unwound the full length of
the power cord, or should I say cords.
The old cord was joined to a new one
by a suspicious large insulation-tape-
covered bump.
Taking off the tape revealed a terminal block with just two joiners: Active
and Neutral. There was no Earth connection because the extra length of
cable was twin flex, with a three-pin
plug but no green/yellow striped wire!
This resulted in Kevin receiving a stern
lecture on electrical safety.
With the new capacitors fitted, it
was time for the big test. I switched it
on and wait for the old electronics to
build up steam, then I got a glorious
burst of ABC radio.
I thought I’d better check the record
player next. The complicated autochanger mechanism looked clean, and
the bits moved freely, so I dug out an
old 78 RPM disc and put that on the
turntable. After lowering the pickup,
there was a rush of snap, crackle and
pop followed by music. But only
through one speaker.
I checked the balance control, but
it was centred. Only one speaker was
working now, but with the radio, both
had given their best.
An inspection of the ceramic cartridge told the tale – decomposing
rubber again. The little flexible bridge
that joins the stylus to the left and
right piezoelectric elements had rotted badly and completely lost one leg.
According to the label, the radiogram was made in 1965. What’s the
chance of finding a new cartridge
for that? Actually, it was easy; a bit
of checking around and I found a
replacement. It cost $70, but I now
had two-channel mono.
To make sure nothing else was going
to blow up, I left the radio running
for a day. There were no problems,
so the nostalgia box went back to a
happy Kev.
The capacitors cost around $40, so
for just over a hundred bucks, he was
happily grooving along to the sweet
sounds of his extensive collection of
SC
records.
The circuit for the Kriesler 11-98
manufactured in 1965, scanned from Philip
Leahy’s HRSA Circuit Book 5.
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