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SERVICEMAN'S LOG
A feline-themed cautionary tale
Dave Thompson
Cats can be quite difficult to manage, especially if they each need
specialised food. With modern tech you now have devices like a
microchip pet feeder, which allow only certain cats access to a particular
food/medicine bowl. However, there’s always a caveat with allencompassing one-trick problem solvers.
Items Covered This Month
•
•
•
Do (not) feed the cat
Tektronix TDS744A oscilloscope
repair
Restoring an electronic organ
*Dave Thompson runs PC Anytime
in Christchurch, NZ.
Website: www.pcanytime.co.nz
Email: dave<at>pcanytime.co.nz
It’s no secret we own a few cats (or
should I say that we serve a few cats?).
I have mentioned them before in this
column.
One of the problems with having
multiple cats is that they are very much
individual characters, with their own
preferences for food and attention. So
it is hard to implement a strategy for
one cat without affecting the others.
For example, one of our cats has allergies to something in the soil around
our cat run. Every spring, these allergies flare up, but the other two cats
aren’t affected at all. Having to dish
out special food or medication to one
cat and not the others can be a lesson
in frustration, as they all graze on each
others’ food.
So when we saw an advertisement for “Microchip Pet Feeders”,
we thought it might be the answer to
our problems. Our cats are all microchipped within a few weeks of birth (as
all pets should be). Having the ability
to allow one cat to feed from a particular food/medicine bowl while the others have no access is very appealing.
That is exactly what these devices
claim in their advertising bumf; apparently, you can program access for
up to 30 individual animals into each
feeder using their unique microchip ID
tag. In our situation, we only needed
to register the one cat to it.
To shop online or not
We ordered one of these units online, and it duly arrived on the doorstep. I’m a modern guy; I like this ‘new’
way of buying products; not because
I’m lazy, but these days one tries to
avoid going out of the house (if one is
even allowed!).
Clearly, online shopping is boom46
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Australia’s electronics magazine
ing at the moment. I have to wonder
whether many people will go back to
the ‘old ways’ even when restrictions
are lifted. Who wants to deal with the
hassle of driving to a shopping centre,
finding a parking space and pushing
your way through crowds to the shop,
only to be disappointed that what you
want isn’t even in stock?
It’s quite convenient just to have
stuff show up at your door a couple of
days after clicking some buttons on the
computer, and overall it doesn’t cost
that much more since you are saving
on petrol, stress and (perhaps more
importantly) time.
However, there are still problems
with this approach. If you know what
you want, or have used the products
before, or they are the sort of items you
can buy based on specifications (like
a lot of electronic devices), it’s perfect
because you know exactly what you
are getting. But online shopping isn’t
that suitable for buying the likes of
clothes or shoes, for example.
Unless you have gone to a bricksand-mortar store to try on the same
product beforehand, and know it fits,
buying these things over the Internet
can be fraught with problems. What
if it doesn’t fit? You are then in a position where you have to go through
the hassle of contacting the vendor,
returning the item, and possibly paying the return shipping costs.
That can mean that your item ends
up costing you more than if you had
just gone down to the store and purchased it in the first place. At worst,
you have no usable product and are out
of pocket for all the related expenses.
Defects and warranty returns can
also be a can of worms. Some online
sellers are great about returns, such as
siliconchip.com.au
most Amazon sellers and local computer stores. But I have experienced
vendors who start ‘ducking and diving’ and trying to place the onus on the
supplier or manufacturer, not wanting
to accept the return themselves.
High-street stores are bound by all
manner of consumer laws to protect
customers, but an online store might
be located off-shore and so all that legal responsibility goes out the window.
What happens then?
Trying to outwit the cats
Anyway, back to our new microchip feeder. We liked it so much we
purchased another, and although we
bought it from a different source, it
is the same brand. The cats seem to
love them, and weren’t as put off by
the movement of the lid or the small
amount of mechanical noise they make
when opening and closing as we initially thought.
However, cats are inherently very
crafty and intelligent animals. The
first feeder we purchased kept our alpha male out for a while, but he soon
learned that in the few seconds it takes
for the bowl door to close once the registered cat has left it, he can swoop in
and hoover a large amount of any leftover food before the door slowly closes
on him. Clever!
The door-close-after-eating timing is
variable, to a degree, via a three-position slide-switch (short, medium and
long delay). But even on the shortest
setting, there are a few seconds the
contents of the bowl are vulnerable
to pilfering.
Our A1 male soon made good use
of this potential design flaw by sitting very close nearby and swooping
siliconchip.com.au
when the registered cat leaves. I told
you they were clever!
Other than that, the device does
what it says. There is a food bowl
buried under a horizontally-closing
bi-folded trap door. Once this door is
closed, there is no way for the cat to
actively lift the door to access the food
or get to it in any way (and they try,
believe me!).
The door design is smart too; it cannot be opened by simply hooking a
claw (or finger) under the split centre
section and pulling upward, as the
motor’s mechanical lever assembly
and natural friction/resistance holds
it firmly shut.
It could probably be forced open
with enough force, but cats aren’t
strong enough (at least in the manner
Australia’s electronics magazine
required) to achieve that.
It’s a good system; it works well and
is quite robust. They have obviously
put much thought into the design.
There is a kind of plastic halo over
the whole thing, and the cat must stick
their head and neck through this to
access the food (most microchips are
inserted between the pets’ shoulderblades and are thus in the right place
to trigger the device).
That is probably the biggest aspect
any pet would have to get used to. This
halo obviously has the antenna for the
microchip reader inside it. If the pet is
not microchipped, a tag is supplied in
the box, and this simple RFID disc can
be attached to a pet’s collar and used
instead of an embedded chip.
As soon as the pet comes close to the
February 2021 47
feeder, the sensor picks up the chip/
tag, identifies it and either allows or
denies access. If the chip/tag ID is recognised, the door sequence starts. One
LED flashes and the motor runs to open
the door. Once the pet withdraws its
head from the hoop, after the pre-set
door-close time, the motor runs back
the other way to close the hatch.
While relatively simple, it’s a system that’s quite tricky to implement
in a low-voltage (6V) battery-powered
package.
There is no provision for a mains
supply, which in my opinion is a major
design flaw. Batteries are expensive,
wasteful and don’t typically last that
long, and these units require pricey alkaline types for ‘optimal’ performance.
An AC power option would have been
a valuable addition.
A turn for the worse
However – there is always a however when a serviceman is involved
– last week, the first feeder we purchased started misbehaving, with the
door not operating correctly.
According to the user manual, the
indicator LED should flash red once
every few seconds when the batteries
get low, but that wasn’t happening, so
I assumed it wasn’t a power problem.
I changed the four C-sized cells for
new alkaline ones to be sure, but the
problems persisted. The door would
not open fully, or then it would open
fully but then not close properly.
I removed the batteries and tested
them with my multimeter, just to satisfy my nagging doubts. Of course, we
all know this is not a complete indication of actual battery state anyway, but
in lieu of a proper battery tester, a basic voltage test does tell me if they are
getting past their best. All measured
well over 1.5V, so I was reasonably
confident the batteries were still OK.
Things got worse over the next 24
hours, with the door often refusing
to open at all. This feeder has several
buttons that can be used to either program the pet ID, set times or open the
door manually. Usually, a press of the
manual door button would open the
hatch straight away, but this became
increasingly erratic. Something had
to be done.
And this is where the whole online
shopping system can start to break
down.
I tried to find somebody to contact on the original purchase site for
48
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a warranty claim, and it turned out it
is almost impossible to reach anyone
there. The 0800 number (a free-calling
toll number here in NZ) didn’t go anywhere, giving me only a pre-recorded
message stating they ‘couldn’t take my
call’, but at the same time providing
no option for leaving a message. Great!
There was also an e-mail form,
complete with one of those annoying
CAPTCHAs, but when I filled it in
and clicked the Submit button, I got a
page-not-found fault, along with the
claim that the message could not be
delivered. Excellent!
This is increasingly the case with
online sellers. They just don’t have
any real customer service. Call me oldfashioned, but it makes much more
sense to pay a little more and go to an
actual store, where any potential problems can soon be ironed out without
all this faffing about.
Or maybe someone can open an online shop with slightly higher prices,
where you can actually contact someone for help. I know it’s a crazy idea,
but it just might work!
But none of that helped me now. The
only thing left to do was to open it up
and have a look. And I also have another feeder to compare this one to, so
what could possibly go wrong?
Disclaimer: I am not a certified
Microchip Pet Feeder serviceman, or
even a non-certified feeder serviceman. Just so we’re clear.
Four screws held the large moulded
plastic back frame on. Once those were
removed, the back split away cleanly,
exposing the wrapped-wire chip sensor antenna, the underside of the door
motor mechanism and a long, narrow,
single-sided PCB absolutely stacked
from one end to the other with surfacemounted components.
I was surprised at the complexity of
the circuitry and PCB, but then again,
I guess there’s a lot going on in there.
There was also a smaller ribbon-cable
connected button-board PCB near the
top rear of the unit, containing the
manual door and programming buttons. Other than that, it was all fresh
air inside.
Fortunately, and against type, none
of the component identification numbers had been obfuscated. I could see
there was an ARM microprocessor
mounted near the middle of the PCB
and several other support chips for it
surrounding that. At one end was the
power supply section and at the other,
Australia’s electronics magazine
the motor driver, which included an
array of what I assumed to be Mosfets
or similar.
The door motor appeared to be a
simple 6V DC motor – nothing special.
I unsoldered the two motor leads from
the PCB (handily black and red) and
used a benchtop power supply set to
6V to run it backwards and forwards.
It operated perfectly and smoothly,
so there was no mechanical reason it
would be jamming or misbehaving.
I wired it back in and used my power supply instead of batteries to power
up the unit; the door opened to full
travel and sat there trying to open further, with the motor ‘hunting’ slightly.
Something was obviously not right. I
was also not entirely sure how they
were relating the position of the motor and door assembly to the driver
circuit; how does it know when the
door is fully open or closed?
There are only two wires to the motor, so perhaps they are just sensing
drive current in the line when the door
won’t go any further and feed this information back to the micro to tell it
to stop driving.
I repositioned the door/motor manually back to closed, and powered on
again. Once again, the door opened fully and tried to go further. It didn’t seem
to matter where the motor was sitting;
it just tried to open up and keep going.
At this point, I realised there was little I could do. Without circuits, firmware or anything to work with, it was
becoming a waste of my time.
My cunning plan goes awry
I know what you’re thinking: I have
the other one! From a troubleshooting
point of view, there is nothing like having another working unit to compare to
a faulting one, so I went and brought
the working one out to the workshop.
Amazingly, though they looked
very, very similar, they were actually
completely different models. The PCB
was very different; the case moulding was different, and even the door
mechanism was different. So there was
nothing I could use from the working
one to relate to the non-working one.
Awesome!
All I could do at this point was button it all back up and go back to the
seller’s website, and try to look for a
way forward.
After making many approaches with
no luck, I ended up going directly to
the feeder manufacturer, and they were
siliconchip.com.au
very happy to help me out. However,
there are many hoops I now have to
jump through, and I’ll likely end up
having to ship this thing at my expense
overseas. It isn’t a small package.
This is not a great outcome, but better than nothing. In the meantime, we
bought yet another feeder to replace
this faulty model, and although we got
it at a knock-down price (compared to
the others), it does leave a bad taste
when online vendors don’t play by the
rules of civilised shopping.
I’m fully prepared to write this one
off, especially if it is going to cost too
much to rectify. Cynically, I’m sure
some of these online sellers take this
into account, because at some point, it
is just not worth the effort at the end of
the day. It’d be a shame, as they are an
excellent device and work very well.
As an interesting aside, there is another aspect to this repair. The PCB
inside the faulty feeder has a tiny
screen-printed message visible on the
top that reads:
“My name is Ozymandias. King of
Kings. Look upon my works oh ye
mighty, and despair.”
What a weird comment to add to
your feeder’s PCB design! It is obviously meant to be read by somebody.
At least it didn’t read “Help, I am being held inside an electronics manufacturing facility against my will!”.
So should I despair? No, service
work can be fascinating.
Tektronix TDS744A
oscilloscope repair
A. L. S. of Turramurra, NSW, fixed
his Tektronix TDS744A 500MHz
4-channel oscilloscope, but he had to
totally disassemble it to get to the root
of the fault, as he describes...
I purchased this scope secondhand some years ago, and it worked
perfectly until one day it refused to
boot. It just flashed the LEDs on the
front panel.
Looking through the service manual,
I could find no reference to this type
of fault. This manual was obviously
not designed for component-level repair because it had no circuit diagrams
or even a block diagram! It had diagnostic procedures to isolate faults to a
particular module, but it has to power
up first, so that was no help.
I immediately jumped to the conclusion that the power supply module was
the culprit, so I started searching for a
replacement or any information on it.
siliconchip.com.au
After trawling the net for some time,
I discovered many other faults which
are common to this model such as acquisition board failures, attenuator
failures and poor SMD electrolytic capacitors, but nothing on power supply
problems or any schematics.
One guy on YouTube had the same
flashing LEDs, but it was for an HP
spectrum analyser, and it required a
complex repair of the switchmode
power supply. I also found some very
good YouTube teardowns and repairs
of this model, and some useful tips.
They mentioned that there is an
internal “protection” switch which
can be accessed from the side panel
through a hole. Sometimes, switching this can bring the scope to life. I
switched it to protection mode, but
nothing happened.
So it was time to open it up and take
a look. I thought there might be some
visible evidence of burnt-out components, or perhaps it was just an internal fuse that had blown, or it just
needed a reset.
I always leave devices with highvoltage CRT power supplies alone for
at least a couple of days to allow everything to discharge, especially when
there is no available information on
exactly where the high voltage is!
After removing four screws at the
back, the rear panel and outer case
came apart with a light nudge from a
rubber mallet.
I removed two Tektronix “calibration is void if removed” stickers given
that the warranty period had expired
over a decade ago. This proved that
the instrument had not been opened or
messed about by the previous owner,
at least since its last calibration.
The internal layout was beautiful
and well-designed for servicing. Each
large PCB was easy to extract, starting with the one on top, which is the
processor/display board with eight
connectors.
After these were removed, plus a
small panel which has a Centronics
connector and an RS-232 connector,
the PCB slid out.
Next, there is a large aluminium protector board with a high-voltage warning. I had to remove several screws to
get that one out. I also had to gently
lever it out of a slot, as it was very stiff.
The power module was then exposed, so I removed it for a closer
look. It was a pretty heavy board with
a fairly standard switchmode architecture, capable of delivering all the low
voltages for the scope.
There were signs of overheating
stress, but there were no immediately
apparent shorts or problems, and all
the electrolytics checked out fine incircuit. The inability to boot made it
impossible to check the voltages given in the manual, so I had to look into
other possibilities.
I couldn’t find any power modules
or identical ‘parts’ scopes for sale,
except for a few scopes that probably had failed power supplies. But
further research indicated that the
TDS684A (1GHz, 5GS/s model) and
the TDS784A (1GHz, 4GS/s model)
have identical power modules and
identical processor/display modules,
so I took another look.
I found one broken TDS684A for
sale, which showed some activity on
a very damaged and dull CRT screen. I
therefore deduced it must have a functional power module, so I bought it for
around $350.
The bad screen wasn’t a huge worry
because this model has a VGA output.
My idea was to swap the modules to
get my 500MHz scope working, and
maybe even repair the 1GHz scope
and get it working too!
The non-working 1GHz scope arrived after a couple of weeks, and I hurriedly checked it out, but it was worse
than the eBay seller’s photos led me to
believe. The raster and graticule were
folded over at the bottom of the screen.
Was there something wrong with the
power supply, or was the vertical amplifier or scan coil faulty? Would an
external monitor even work?
Also, the seller told me that he was
pretty sure that it was showing all four
traces, but there were no traces at all,
Servicing Stories Wanted
Do you have any good servicing stories that you would like to share in The Serviceman
column? If so, why not send those stories in to us?
We pay for all contributions published but please note that your material must
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Please be sure to include your full name and address details.
Australia’s electronics magazine
February 2021 49
so the acquisition board was probably kaput too! This appears to be a
common problem with this model.
It’s possible that the seller assembled
the whole scope out of junk modules
from previous repair jobs.
I decided to try swapping the power
module anyway – after all, it did boot
up. So I tore down the spare scope
and extracted the ‘good’ power supply
board. Because I was getting good at disassembly, I had it swapped in no time.
Then, after checking all the connectors
five times and cautiously plugged the
thing in, I stood back in anticipation of
sparks and blue flashes and pressed the
“on” button at arm’s length.
The LEDs were flashing again, and
no boot up at all! The fault must be
on one of the other modules; perhaps
the processor/display module. So I
swapped that too. Again, nothing, just
those darn flashing LEDs!
I noticed that on top of the processor module was a single 7-segment red
LED display, and it was flashing “8” in
time with the LEDs on the front panel.
I could find no mention of what this
means anywhere.
So, I thought I had better change
the acquisition board, which required
delving deeper because the screws into
the BNC attenuators were behind the
front control panel. The whole instrument had to be inverted because this
module is on the bottom.
The front plastic panel had to be
removed and this was supposed to
“snap off” (according to the manual),
but 20 years of grease, dust and grime
acted like an excellent glue, so I had
to use two screwdrivers in tyre-lever
fashion to ever-so-gently prise it off.
Of course, it cracked, but luckily the
crack was on the bottom, and it was
almost invisible.
Then I had to remove the BNC cover
along with the front control panel to
expose four screws which finally released the acquisition board. I smartly
swapped this, hoping it would cure the
boot problem at last. But no! I was still
getting the LED light show.
What next? Deep inside the bowels of the instrument, there are several PCBs which are stacked like a
house of cards, inside a three-sided
metal box. From this emanated myriad wires connecting the cathode ray
tube (CRT) and the EHT tripler, along
with the scan coil drivers and output
transistors and some ICs.
There was also a large processor
IC, and I was horrified to see that the
EHT cable had touched this, leaving
black soot on it, but it was all part of
the design to squeeze everything into
a tiny space. The CRT and its associated scan coils, rear PCB and correction magnets were also squeezed into
this box.
This was all that was left, so the fault
must be there somewhere, mustn’t it?
I was beginning to doubt my ability to
fix the two scopes, but I had already
committed enough cash to motivate
me to continue.
The next step was to inspect this
daunting mess, so I disconnected everything, taking care to note where all
the wires went. I disconnected all the
cables and connectors except for the
EHT lead, which was blocked by the
thick aluminium chassis.
So the CRT had to come out, but first,
more stuff had to be removed such as
the softkeys, which were mounted on
a thin metal bezel, and also the floppy
disk drive.
Then, very gently, I pulled out the
CRT to the limit of the high voltage
cable, about 4cm out of its housing. I
was only just able to remove it from
the tube by lifting the rubber insulator on the side of the tube and lightly
squeezing the prongs with a medical
clamp to release it.
I made sure it was fully discharged
by shorting these metal prongs to the
chassis. Fortunately, the two-day safety discharge period I had allowed had
done its job.
I have some old-world experience
with TV repair, so I was extra careful
not to knock the skinny end of the tube
because that is the weakest part. I also
wore safety glasses because if these
things are broken, they can implode
and fling glass everywhere.
I held it with all the delicacy of
a newborn baby and stacked it face
down in a cardboard box and set it
aside away from harm.
Now the whole instrument was
stripped down to the bone (as shown
at lower left), and all that was left was
the box of components with the highly
suspect board.
Several electrolytics had to be bent
out of the way to access the screws
which needed to come out. Some of
the electrolytics completely blocked
the screwdriver access. I don’t know
why they didn’t measure the electrolytics before they allocated the screw
positions.
Despite having removed the screws,
the assembly just wouldn’t come out.
It would not fit through the gap left
The Tektronix oscilloscope was taken apart to determine
the suspect components/boards.
►
Some burnt and shorted tracks were found on the
EHT module around the TIP30C driver transistor and
associated electros.
50
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Australia’s electronics magazine
siliconchip.com.au
by the CRT, but by twisting it on its
long axis and angling it in a certain
position, it finally came out like one
of those kids’ puzzle games.
On the EHT module, I found some
burnt and shorted tracks around the
TIP30C driver transistor and its associated electrolytic capacitor (shown
opposite at lower right).
This was not visible from the top,
and the cause was not immediately evident until I removed a capacitor and
a transistor. This short had obviously
caused an overload, shutting down the
whole instrument.
I repeated the extraction of the EHT
assembly on the very cannibalised
TDS684 1GHz scope, leaving it as a
bare chassis. By this time, I had become very proficient with these techniques, and the extraction took just
five minutes. I mounted up the suspect
“spare” EHT module in my scope and
inserted the original CRT to see what
would happen.
Well, it finally booted but as you
might have guessed, that wasn’t the
end of my problems! The raster and
colour display were unexpectedly
good, but I could not get a trace, and
that meant that the substitute acquisition board was bad.
Now I had to retrace my steps and
put the original acquisition board back
in, which proved pretty easy because I
had so much practice. After I restored
this board I got a trace, but the gremlins
had multiplied, and error messages
plastered themselves over the screen.
Retracing my footsteps, I restored
the original processor/display module and waited for the boot-up, which
takes about a minute. I thought I was
dreaming as everything worked perfectly; the self-test passed the display
was steady, and it even came up with
my last settings!
The only downside was that the
brightness was a little lower than it
had been; that can be improved with
the internal brightness adjustment, but
I had just about had it, so that would
have to wait for another time.
If I can get the 1GHz acquisition
board going, I can extend the scope’s
bandwidth from 500MHz to 1GHz, so
I will have a go at that later. For now,
I just want to enjoy my once again
working scope!
Restoring an electronic organ
K. V. of Kallangur, Qld, has put some
time and effort into restoring electronsiliconchip.com.au
ic organs, which are sought after these
days, and quite valuable...
Some years ago, my wife and I were
given an old Hammond “Grandee”
electronic organ. My wife can play
quite well, but I can only fiddle with
something electrical. The organ was on
the way to the dump, beyond repair –
but I was given first choice!
I eventually got it all working thanks
to a gentleman in Sydney, who obtained a service manual for me. This
was a big help because one circuit
board was missing. Apart from that,
the cabinet had been home to a family of mice for some years, leaving
quite a mess!
My son helped me make up a new
circuit board, and after a big cleanup, it
all came to life. One of the first things I
had to do was to add a speaker switchon delay to alleviate the loud thumps.
Electronics Australia published a
letter I wrote about these repairs back
in 1997. Most of the problems we have
had over the last 20 odd years have
been because of poor contact in the
many plug-in connections. It is good
to be able to remove a circuit board to
check by unplugging it, but generally,
there is nothing wrong with it. Clean
the contacts, a little wipe with Vaseline, plug it in and it goes!
One problem that took 20 years to
track down was that the hum level was
higher than it should be. I had changed
all the electrolytics in the power supply with very little improvement. The
hum level on the two amplifiers was
below Hammond’s specified level, so
I left it at that.
The connections to the organ from
the power supply and amplifiers were
by two 15-pin plugs. I never did like
them. If they were wriggled, they made
scratchy noises in the speakers.
Pluggable terminal blocks looked
to be the answer. These plugs carried
a mixture of various DC voltages, signal voltages and mains voltages. The
modifications involved a fair bit of
work, but it was worth it. While I had
the chassis out, I thought I might as
well change the Leslie speaker plug
to a pluggable terminal too.
The Hammond drawing on the Leslie speaker shows six wires, two for
the speaker and two each for the highspeed and low-speed motors. But this
organ had five wires, not six!
When this organ was built, someone
decided to save a bit of wire (about
800mm), because all the returns were
Australia’s electronics magazine
February 2021 51
terminated off the one Earth bar on the
chassis – but they added another 6-pin
plug and socket at the Leslie speaker end. I decided to wire it up as per
Hammond’s drawings and delete the
extra 6-pin plug. It was superfluous.
When the organ was put back together, everything worked OK. My
wife played a few tunes and was quite
happy with it. That annoying hum
level had gone!
I sketched out the connections of the
Leslie speaker showing how they were
and how they should be. The tremolo
speaker return connected to the fast
motor return, which is always running, then through two doubtful plug
contacts to the common Earth bar. The
tremolo speaker had every chance of
picking up some 50Hz current, producing the hum.
52
Silicon Chip
Sometimes the designers’ plans are
not always carried out on the workshop floor, but the organ worked – so
out it goes to be sold! All the soldering in the Hammond was excellent
and I never had any trouble with dry
soldered joints.
That reminds me of another organ
I had to repair, a Baldwin “Fanfare”
built in 1977. It had been sitting idle
for years, and it too had become the
residence of mice. That meant another
big cleanup, checking and replacing
corroded contacts. When it was ready,
I connected it to a variac and slowly
increased the voltage in stages. At full
voltage, most of the organ worked.
About this time, a service manual arrived from W. D. Greenhill & Co in England, so I was able to check the power
supply. I found that only one section
Australia’s electronics magazine
was within tolerance. I removed the
power supply to the workbench, replaced the electrolytic capacitors and
one open-circuit transistor. All voltages
were set within the ±3% as specified.
When it was replaced in the organ,
the -12V supply was down to -7.5V,
and clearly overloaded. A bit of circuit tracing revealed that the -15V and
-12V supplies were crossed over in a
plug. The organ worked much better
after correcting this error. This is another case of an original fault that was
‘allowed through’ because most of the
instrument worked!
I did eventually get this organ all
working after tracking down numerous faults, corroded connectors, poor
solder joints and some faulty ICs, as
well as fitting a delay relay to the
speakers.
SC
siliconchip.com.au
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