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SERVICEMAN'S LOG
One good turn deserves another
Dave Thompson
A client turned up at the workshop the other day with what I would
consider the perfect job for me. This bloke is a known audio ‘nut’ in my
old circle of friends. Although I hadn’t heard from him for many years,
he had tracked me down because he finally decided to fix up a few of the
‘vintage’ items in his vast collection of 70s and 80s audio gear.
I say ‘my circle of friends’, but I
didn’t really know him; I had met him
briefly, and knew of him by reputation
back when I was a young jobbing musician. He played bass guitar in one of
the many bands I used to cross paths
with while grinding out gigs on the local pub circuit.
He was known for being right into
his audio gear, so in lieu of any real
information available to us at the time
(no internet in those days), we often
bowed to his supposedly superior
knowledge in subjects related to sound
reinforcement and instrument amplification. For better or worse, he was a
fount of knowledge at the time; I had
to learn this stuff somewhere, right?
For those intent on writing off my
experiences, put those burning torches and pitchforks down; I admit I was
never a ‘rock star’ but I did play in
touring bands for many years, and one
picks up pertinent knowledge along
the way.
While I might not know what
amplifier and speaker combination works best in your man-cave/
lounge room, I could suggest what
sound reinforcement hardware
you would choose if you wanted to sonically light up a 500-seat
theatre!
My point is that we all knew this
bloke as an audio purist, and while we
somewhat blundered on with our typically low-fi stage gear, he was the one
who was really into the specifications
and minutiae of the speakers and amplification that were being used back
then. While I hesitate to label anyone
I’ve ever known as an ‘audiophile’, he
was probably as close as I ever came
to meeting one.
Not that he was in any way one of
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these guys who proclaims that those
$500-per-metre, plutonium-enriched
gold and copper alloy speaker cables
as the only thing to use for a home
stereo setup. Or that one had to have
thousands of dollars’ worth of audio
hardware to have a good sound; he was
just really into his audio hardware.
Many of us likely know (or have
known) someone like this, to varying
degrees. I’ve met guys over the years
who insist that speaker cabinets need
to be mounted on Kryptonium-alloy
Australia’s electronics magazine
Items Covered This Month
•
•
•
Acoustic research turntables
PA system repair
HP5100 frequency synthesiser
repair
*Dave Thompson runs PC Anytime
in Christchurch, NZ.
Website: www.pcanytime.co.nz
Email: dave<at>pcanytime.co.nz
January 2021 61
needles embedded into unicorn-horn
substrate on an isolated, rubber-floored
room to really appreciate the sound of
their stereos.
And all this will have to be powered through some rare and obscure
Class ABCDEFGHIJK+ amplifier that
costs more than a small house. The
marketing bumf of the time laid it on
pretty thick, having us believe that
unless one has this type of system, it
simply wasn’t worth even firing up
the turntable.
This is obviously not the case, but I
gave up trying to convince anyone of
this a long time ago. To me, whatever
sounds good to me is the best system,
regardless of specs and cost.
It seems my old friend has mellowed a bit; maybe because of age and
wisdom, but likely also because his
now-wife doesn’t share his passion
for spending money on expensive audio gear. That said, he still uses and
swears by his many 70s and 80s highend amplifiers and turntables.
I only mention this because when
he called the other day, and after the
usual 30-minute, three-decade catchup conversation, he arranged to bring
in a couple of his Acoustic Research
(AR) turntables for me to have a look
at and see what I could do with. After
that is the promise of some more juicy
gear to work on. Life could be worse!
You turn me right ’round
Most people realise that anything
with words like ‘research’ or ‘labs’ in
the brand name must be excellent, and
therefore expensive; and back in the
day, in New Zealand, these Acoustic
Research ES-1s were.
They weren’t insanely expensive,
like the Mitchell Transcriptor turntable (featured in the movie A Clockwork
Orange), or the Oracle Delphi MK1,
both of which could be had here for the
price of a small car (minus tonearm,
of course, which they assumed you
would want to add yourself anyway).
But they were still relatively pricey
none-the-less.
The customer duly arrived with a
couple of banana boxes full of bits
and pieces, and I could see my work
would be cut out for me. One box contained one AR ES-1 turntable, which
was the most complete, but this had a
damaged drive motor and spindle assembly, which made the drive spool
wobble like crazy when powered up.
Even if I could get a belt to hang
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onto it, playing any records would
be pointless and sound reproduction
would suffer badly.
The second box contained a turntable identical to the first, but which
had seen better days. While it still
powered on and the motor ran, the
veneered timber case was in a very
sorry state, and the power indicator
lamp was not working. This one was
also missing several pieces, such as a
tonearm, the tonearm mounting plate
and most alarmingly, the rectangular
clear Perspex cover.
The cover hinges were still attached
to the base, but the cover was nowhere
to be found. It transpired that this particular table had been bequeathed to
the current owner after the previous
owner had passed away; a sorry situation to be sure, but at least the turntable wasn’t just thrown into the garbage by the grieving family.
So, in summary, I had to repair two
Acoustic Research ES-1 turntables;
one was complete but had a wobbly
drive capstan, and the other was minus
a lid, tonearm and altogether incomplete and to be honest, a bit of a mess.
This was no problem for a serviceman like me, though! If he wanted to
pay me to restore these two beautiful
machines, I’d be more than happy to
oblige. However, I’m sure you see the
predicament; often, when servicemen start talking about the money involved, getting vintage devices back
to rude health can suddenly become
a lot less urgent!
I quoted the guy, and he was more
than happy to pay. Darn! I knew I
should have charged more!
Australia’s electronics magazine
Suspect #1
I tackled the most complete one first.
That entailed removing the platen,
which is simply held in by gravity, the
drive belt, and the eight screws that
held the cast metal plate to the timber
chassis, the fibre-board floor underneath the turntable (which is held on
with the four rubber feet screws) and
desoldering the wires that go from the
drive motor to the small circuit board.
The tonearm cables just go straight
through the mounting plate and out
through a cut-out in the fibre-board
floor to the amp, with just one small
plastic cable clip holding them in
place inside the box. Once these items
are removed, the whole mechanical assembly lifts clear, leaving what is essentially a timber box with a circuit
board and mains cable mounted to it.
Simple, to be sure, but very effective. The only problem with this one
was the bent drive shaft. God knows
how this happened, but it was severely
eccentric when running. Fortunately,
the customer had purchased a replacement motor from an internet auction
site, but hadn’t fitted it because he
couldn’t get the drive pulley off the
bent shaft.
This proved no real problem for
me, as I have the right tools for the job
(woohoo!). After removing the motor
(which required desoldering the two
motor power leads), I mounted it in
some jaws under my bench press and
gently pushed the pulley free.
I had to be careful because these pulleys are typically a cast alloy and are
very soft. It separated from the motor
shaft quite readily though, and I ran it
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on a temporary mandrel in my cordless drill to check its concentricity.
The pulley itself was fine. I simply
mounted it onto the replacement motor with some Loctite and replaced and
re-soldered it back to the drive plate.
On switch-on, it ran almost perfectly, although it required a few light taps
on the high side with a small rubber
mallet to get it running dead true.
Another problem with this turntable
was the drive spindle on the platen itself. The heavy platen sits and runs in
what appears to be a phosphor-bronze
bearing. It had excessive play, and I
suspected this to be due to the bearing
drying out. These types of bearings are
usually pressure- or vacuum-infused
with oil when manufactured, and last
for years, but this one was bone dry.
I don’t have a vacuum chamber (I
know, I know), so all I could do was
fill the bearing with oil and leave it
standing for a few days before removing the excess and trying the fit again.
This time it was better, and operation
was smooth and steady, but since I had
no instruments to measure wow and
flutter (I know, I know), I’d have to go
with what I had.
The owner would either have to
get that bushing replaced, or re-oiled,
or do some regular lubricating maintenance on it in the future; he didn’t
seem too worried about this prospect
when I mentioned it to him.
Suspect #2
That brought me to the next pile of
bits. It’s always nice to have a fullyfunctional version to compare with
when assembling parts, and this time
was no different. I put all the metalwork back together and laid everything
out in the case, and the only part missing was the tonearm mount.
I took some measurements from the
working version. The plate appeared
to have been made from some kind of
painted hardwood, so I fabricated one
from an oak offcut I had in my timber
bins. I bored the four countersunk
mounting holes around the periphery, but left the rest undrilled; how
and where the other holes go would
depend on what tonearm he wanted
to use.
I offered to do that for him when the
time comes, and said he would let me
know. After filling, sanding and painting it with a semi-gloss black lacquer, it
looked almost the same (and as good)
as the original.
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The same couldn’t be said for the
timber turntable case, though. It
looked like it had been left exposed to
the sun for many years, and all the dark
external veneer had peeled and flaked,
exposing the lighter timber beneath.
The only way to solve this was to
strip the veneer off and re-finish the
timber below. I used a coarse belt on
my belt sander to rip the old finish
off. While messy, it came off easily;
the trick is not taking any of the solid
timber underneath! I then used progressively finer paper on my recentlyrepaired 1/3-sheet sander to smooth
everything off.
A few coats of Danish oil brought
out the grain, and five coats of clear
lacquer resulted in a beautiful finish which was (luckily!) very close in
shade to the original model, so I was
happy with it. The customer was too,
when he saw it.
I didn’t have a Perspex cover for
it though, and couldn’t find one online. I contemplated making one from
scratch, but I didn’t have any plastic
heater/former/folder gear with which
to do it (I know, I know). Dad had all
that stuff, but I don’t know what happened to it.
The customer wasn’t too bothered;
he planned on putting the turntable
in a rack that had a top cover anyway,
so with his agreement I removed the
original lid hinges and plugged and
filled the holes left behind. I used
plugs of similar-coloured timber so
it wasn’t too obvious that it had been
done, though of course, if you looked
closely you could see it.
However, it was on the rear of the
case so the repair would be out of view
for the most part.
The next challenge was the indicator light. These turntables have a simple on/off switch mounted on the top
(under the plastic hood) that switches the motor, well, on and off. When
on, a pinpoint of orange light shows
through about halfway down the front
of the case and directly underneath the
power switch.
It is quite bright, so I wasn’t sure
exactly what was being used. Whatever it was had been glued or embedded into the timber on the inside of
the case, and someone in the past had
tried to remove it by simply pulling on
the connecting wires. They had parted
company, and I could see what looked
like the bottom of a peanut bulb stuck
in the hole.
Australia’s electronics magazine
Cautious use of a dental pick from
the inside of the case soon had the
lamp out, and it turned out to be a peculiarly-shaped neon bulb with a pinpoint at the tip, which is the part of it
I could see from the outside.
I have a good selection of neons
collected over the years, but I didn’t
have anything like this. I decided to
use a light-emitting diode instead, and
the customer was OK with this. The
problem was that the neon ran from a
160V AC feed from the circuit board (as
measured across the broken-off leads),
and I think that’s a little high for LEDs,
and they prefer DC too.
I installed a high-voltage full bridge
rectifier across the circuit board contacts which gave me a DC voltage I
could use for the LED. I calculated
I’d need a resistor of around 15kW to
drive the LED from this supply without blowing it. After installing the
LED into the hole and soldering everything up, I tentatively plugged it in
and switched on.
The LED was a little dim, so I
dropped the resistance to 13kW, and
that did the trick. After running it for
half an hour on the bench, nothing
became overly hot or emitted smoke.
The effect from the outside of the case
was almost the same as the neon, so I
was happy with it.
After insulating everything with
heatshrink tubing and tacking the
LED into the chassis with a small dot
of epoxy, I assembled everything into
the case and buttoned it up with new
rubber feet.
This turntable suffered the same
problem of excessive play in the platen spindle, so I did the oil bath trick
again, and that sorted it out. After fitting
a new belt the customer had supplied,
and trying out the drive system, I was
happy with the way it was running.
The final job was to re-attach the AR
badge lying in the bottom of the box to
the correct location on the front of the
case, and it was the job done!
PA system repair
R. J., of Laingholm, NZ found out
what happens when amateurs and
barely competent ‘professionals’ have
a go at installing or fixing a large PA
system. The result wasn’t pretty, so
he had to spend some time cleaning
up the mess...
My main focus is in broadcast studios, but I do get to work at theatres
and festivals and have a fair bit of
January 2021 63
equipment that needs maintaining, so
service jobs are part of the portfolio.
In the ‘good old days’, a band or
performer would turn up at a venue
with a sound system of variable quality
and crank it up to 11. But times have
changed, and most venues now have
good sound systems and some control
over the volume. Bands have been replaced in some places by a DJ who
can play any one of several thousand
songs, making it even more important
to have a quality sound system.
I have an acquaintance who runs a
performing artist booking business,
and before he books performers, he
checks out each venue. At one venue, he found the system to be terrible.
The owner who recently purchased
the business claims the system cannot
be that bad because it cost $50,000;
that was its value on the books when
he took over the business. So I was
called in.
It was a restaurant/sports bar/dance
floor and verandah in an industrial
area building which looked like it had
been a warehouse or a workshop. The
restaurant and bar fit-outs were well
done. The stage is bigger than most,
and at one time, the venue had been
fitted with an excellent system which
was well worth the stated value when
new.
The only fault I could see in the layout was the positioning of the speakers above the stage. They are mounted
behind the front line and close enough
to a back wall to cause feedback problems. The shock came when I was
shown the equipment rack, in a nonventilated office at the back.
It seems that the venue had some
sort of problem with the system which
caused a number of the original amplifiers to fail. The cost to have someone come and fix it was deemed too
much. It seems one of the regular clients of the bar said he could fix these
things. He got it going again by taking
out the non-performing amplifiers and
replacing them with domestic stereo
amplifiers!
The original amplifiers disappeared,
along with that patron...
The system was in a state of chaos
and disrepair. The owner wanted to
stage the repair process because his
venue had fallen on hard times, and
costs have to be managed as the owner
re-invents the place to meet the current market. This suited me as I could
do it as a fill-in job.
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This system has a DBX Zone Pro
controller which can switch any one
of six sources to one of six zones. It
was not switching as expected, and
randomly dropping the level to various outputs. Fortunately, the agent is
Jands who have a local office and some
very competent people. There is no
field service. The DBX needs to be assessed on a test bench, so I took it over.
Next day they phoned to report that
they’ve found the fault and that it is
fixable at a reasonable price. I have it
back in a day, armed with a warning
that the problem is definitely heatrelated. Not only is the rack in the least
ventilated part of a building, but there
is also a kitchen adjacent, so the ambient temperature is warm. The rack
is well-made and has four fans in the
top, none of which work.
We agreed this was an urgent matter,
so I sourced four fans. The mounting
screws were different, but with some
assistance from a specialist, the replacements went in. The original fans
seemed to have failed due to debris
falling through the vents.
I put the DBX back in with an air
gap above and below, and a warning to
the owner that if the temperature goes
up, we will have problems. I also purchased an external fan to assist with
airflow, and removed most of the junk
on top of the rack, which was blocking the airflow.
Reprogramming the DBX with the
supplied software was easy.
Working through the amplifier levels, I found that they were nowhere
near what the venue needs. The monster amplifier in the rack used for driving the subs had failed. It was a brand
no one knows and uses components
we can’t find. It seems to have been a
short-lived European import brand. I
contacted the company who did the
original install, but they were not
helpful.
One good thing about this system
was the speakers. They were a wellknown European brand, and they all
functioned properly. They all had
power-handling capabilities well
above anything we could deliver.
There were two line-level XLR leads
from the stage back to the DBX. Whenever someone plugged into them,
there was a huge hum. I was told that
it had been like this since the system
was put in.
On the stage, a mixer of indeterminate parentage was feeding audio to
Australia’s electronics magazine
the DBX. Replacing this with a small
Alesis ‘fixed’ the problem; the Alesis
line out is isolated from the local Earth.
But 99% of the visiting equipment is
not such a good design, so I would
have to come up with a better solution.
I located a couple of 600W:600W
transformers which have good audio
bandwidth. Don’t be fooled by the
cheap ones; they only go to 4kHz, and
the proper ones are not cheap. The
wall box on which the XLR sockets
are mounted has enough room for a
small PCB and the transformers, suitably wired and insulated. Now anyone can plug into the house and get
clean audio.
So the main job left was to upgrade
the amplifiers. We settled on a Class-D
Talon amplifier, which claims to deliver 2 x 450W. One was purchased to
see how it performs, and the result was
stunning. It has XLR inputs and can
be run in bridged mono mode. There
are two fans, and the unit is quiet and
runs relatively cool.
The owner was impressed and some
time later called me in, and we ordered
several more. Another afternoon’s
work, and we had a system which was
performing as well as ever.
I can’t believe the domestic stereo
amps lasted as long as they did. At
least one was cutting in and out on
one channel; likely, its power supply
was not up to 5+ years of 12 hours of
daily use. The other just had trouble
making steam. The two originally installed Aussie-made amplifiers are still
working. But there was one last problem remaining.
The venue has an AMS music system which streams music and video to
each client over a proprietary system
via an HP laptop computer. When this
system was installed, a ‘contractor’
was booked by AMS to run the cabling.
The cabling is not part of the rented
system, so its maintenance is the venue’s responsibility. From what I could
see, it had not been done properly.
One was run over Cat5 via a balun
which has one coaxial wire and a pair
of wires originally intended for feeding DC. There was another balun at the
end of the 40m cable with some RCA
connectors that had been grafted in
place of the original BNC connectors.
That it worked was more by chance
than design. The baluns were not designed for audio, resulting in significant losses of both low and high audio
frequencies. Cat5 has varying twists on
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its four pairs, and the only pair suitable for audio is blue/white (pins 4 &
5). Replacing this cabling was not an
option given the cost.
I tried to source some Cat5 audio baluns but had difficulty finding them. I
eventually got hold of some suitable
RJ45 termination. An hour or so and
we have an ‘improved’ cabling system
which delivers audio at high quality
over Cat5. Just why this was never run
with proper audio cable and terminated with XLRs or TRS jacks will never
be answered.
The venue now has a grunty music
system which was well tested over
the next weekend, and a reliable pub
quiz system which fills the place on
Tuesday nights.
HP5100 frequency synthesiser
repair
R. F., of McCrae, Vic wrote in to tell
us a little bit about how he got into
electronics (see the Mailbag section in
this issue). In that letter, he mentioned
that he was fixing up an HP5100 frequency synthesiser. Here are the details of what was wrong with it, and
how he fixed it…
My earliest recollection of a “fabulous” electronics device was on display at an open day for prospective
students in the old cream brick Electronic Engineering School at the UoM.
It was an HP524A digital counter set
up to measure the speed of a rotating
shaft. It could measure frequencies
up to 220MHz and weighed a massive 55kg.
It had digital readout columns of 10
digits per decade. Somehow, it was
very cool; one of my clock-building
friends still has one. Years later, as engineering students, we keenly appreciated the precision and superb construction of the Tektronix 547 oscilloscope – one of the most sought-after
instruments in our laboratory sessions.
Hewlett Packard made a nice range
of ‘scopes, but was more renowned
for their general and specialised test
equipment, which brings us to the devices needing repair.
Back when I was home-brewing amateur radio linear amplifiers for HF and
two-metre operation, I decided that I
needed an accurate, high-resolution
signal generator. I heard of an HP5100A
synthesiser available at a give-away
price, so I bought it.
However, it needed an HP5110B
synthesiser driver, and despite an exsiliconchip.com.au
haustive search via eBay and other
channels, I could only find the driver
as part of a pair; the other part was a
J02 HP5100B synthesiser.
The HP5100A could generate signals in 0.01Hz steps from 0.01Hz to
49.99999999MHz, whereas the J02
HP5100B generated signals in 1Hz
steps from 1Hz to 29.999999MHz. Fortunately, the HP5110B could simultaneously drive both synthesisers. So
I bought the second synthesiser and
driver as a package.
To cut a long story short, I installed
the two synthesisers, the driver, a
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modified HP5061A caesium-beam frequency standard, an HP5245L electronic counter and an HP6263B DC
power supply into – you guessed it –
a Hewlett Packard Systems equipment
rack. This massive collection of boatanchors weighs over 170 kg.
The caesium beam tube of the
HP5061A was unserviceable when I
bought the unit for $100 about 15 years
ago, but the unit had a highly-accurate
5MHz crystal oscillator in a temperature-regulated oven. So I stripped out
the caesium beam assembly and related parts and replaced them with a
January 2021 65
erating techniques all combine to produce exceptional performance.
But inevitably, a small proportion
of components do fail. Over the past
few years, the performance of my units
slowly deteriorated until I had no
choice but to delve into them.
Repairing the behemoths
modern GPS receiver and controller
to synchronise the oscillator.
The very stable 1MHz output from
the HP5061A is connected to the synthesisers, driver and counter to provide GPS-accurate synchronisation,
and consequently extremely accurate
and stable frequency synthesis and
measurement.
It still seems like a small miracle
that all this stuff can work so reliably
as a total package. There are thousands
of components in the fully solid-state
system, hundreds of discrete transis66
Silicon Chip
tors, and just a few integrated circuits.
Fortunately, the total power consumed
with all devices on-line is just over
200W, so heat – the enemy of long-term
reliability – is at a minimum.
Clearly, the original HP designers realised that component quality and assembly workmanship had to be of the
highest order to ensure a high MTBF
rating, and this is part of the ‘wow factor’ associated with these early behemoths. Gold plated circuit board traces
and pins, beautifully loomed cables,
modular construction and simple opAustralia’s electronics magazine
The front panel of the HP5100A
synthesiser has an array of 103 pushbuttons to select the desired frequency.
At the rear, it has 46 coax cables going
to the HP5110B driver.
A harmonic generator takes the output of the 1MHz master oscillator and
feeds them through a series of filters.
These produce signals with discrete
frequencies of 30-39 MHz (in steps of
1MHz), which are fed to 10 of the BNC
sockets on the rear panel.
Each of these signals is also divided
in decade dividers to produce 3.0-3.9
MHz signals which also go to rearpanel BNC sockets. A further three
signals at 1.0, 3.0, and 24.0 MHz are
generated as driver outputs. All output signals are extraordinarily stable
and spectrally pure.
An elaborate power supply produces voltages of +6.3V DC and -12.6V DC,
and is always on to supply the temperature-controlled oven of the 1MHz
master oscillator and the oscillator
circuitry. A DPDT toggle switch with
Standby and Operate positions supplies the rest of the driver electronics.
I discovered that this switch was
faulty, with a defect that I hadn’t previously encountered. The switch toggle operated and felt completely normal, but only one of its poles was actually switching, thereby leaving the
-12.6V supply disconnected from the
instrument in both standby and operate modes. A replacement switch
brought the driver back to life.
With the HP5110B driver working
again, the HP5100A synthesiser performed well, but the J02 HP5100B
stubbornly refused to generate an output signal.
This near-twin of the HP5100A is
not quite as complicated, having a reduced frequency range and lower resolution. “Only” 73 push-buttons are
required to cover this range and resolution. The output frequencies from
the synthesiser are all derived from
the single 1MHz precision oscillator
in the driver, and its 23 output signals.
The synthesiser outputs are produced through the processes of fresiliconchip.com.au
quency addition, subtraction, multiplication and division. The array of 73
push-button switches supply -12.6V to
a matrix of diode switches.
Each diode switch comprises one
silicon and two germanium diodes,
normally biased off by 6.3V applied
to the silicon device. The -12.6V overrides the 6.3V through a resistive network and turns on the germanium diodes, allowing an RF signal to pass
through the matrix with low loss and
negligible delay.
A full description of the synthesiser
is beyond the scope of this article, but
through an extremely ingenious combination of mixers, multipliers and dividers, the signals from the driver can
be synthesised into any frequency between 1Hz and 29.999999MHz.
The synthesiser function is implemented by a low-frequency section
(3.0 to 39.0MHz) and a UHF section
(370 to 390MHz). The latter section
is mounted on an internal sub-frame
which swings outwards from the instrument, to provide access to the various modules and their interconnecting
cables. All told, there are 25 modules,
many of them plug-ins, and 125 germanium PNP transistors.
Despite its complexity, troubleshooting the synthesiser is relatively straightforward. If a single module fails, the device produces no output signal. Locating the faulty module, and confirming
it is indeed at fault, is difficult; but access is easy, and all the modules contain discrete components (1964 was
before ICs had hit the market).
I reflected that even the transistor had only been invented 15 years
beforehand, yet the mainly germanium transistors in the instrument
were capable of reliable operation up
to 390MHz. That led me to the 39 to
390MHz multiplier module, which indeed was faulty. I found that a 2N2402
transistor had failed.
This PNP Ge device was rated at
18V maximum between emitter, base
or collector and had a transition frequency of 220MHz. The nearest equivalent in my parts bin was a 2N3906 Si
device, rated at 60V and with a transition frequency of 250MHz.
It seemed to be operating as a ClassC amplifier, and biasing differences between germanium and silicon devices
proved to be unimportant when its replacement with the 2N3906 brought
the module and the entire instrument
back to life.
SC
siliconchip.com.au
Australia’s electronics magazine
January 2021 67
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