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SERVICEMAN'S LOG
I’ve repaired planes before, but never tanks
Dave Thompson
Some jobs require a great deal of patience and involve plenty of
introspection. Did I do the right thing? When is the right time to call
it quits? This is one such story, illustrating the pitfalls of my life as a
serviceman.
In the years that I have been The
Serviceman, I have tried to keep this
column from being too computerrepair centric, mainly because computers are quite boring to many of the
service people who read this magazine.
However (there’s always a however!), a repair I’ve had on the boil for
almost a year now illustrates just how
fickle the business can be, and how
much we rely on others to do their jobs
properly to have a successful outcome.
I’d call this one a cautionary tale.
It all started a long, long time ago
in a galaxy far, far away (not really!)
when a regular customer brought me
a machine I was already very familiar
with; a Dell Alienware M18X gaming
laptop. The Alienware range of Dell
laptop computers is well-known for
their blistering performance. Therefore, they are a very sought-after
machine within the gaming fraternity
(and sometimes ‘power users’ too).
As with any high-performance
laptop, all this muscle doesn’t come
cheap. My client bought his Alienware laptop in the USA when he was
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travelling there some years ago. Even
though it was ‘on special’ at the time,
he still paid around $US6,000 for it,
a staggering sum of money for a laptop at the time.
It’s luggable, all right
$US6,000 buys a lot of hardware,
and this Dell is no exception. The
computer boasted the likes of twin
accelerated (and upgradeable) graphics cards, dual RAIDed hard drives
and a high-definition 17-inch screen,
a relative rarity at the time.
To call this machine a ‘laptop’ is
perhaps a bit disingenuous; it’s built
like a tank. I certainly wouldn’t want
to carry it around with me and plop it
on my lap, given it weighs around 8kg.
It is more of a ‘desktop replacement’
computer, intended to sit in one place
most of the time, not be lugged around
as one would a more ‘typical’ laptop.
To give this some context, I took a
standard Acer laptop with me on a trip
to Europe a few years back, and by the
third week of our travels, I was so sick
of carrying it around I was seriously
Australia’s electronics magazine
Items Covered This Month
• Servicing is often a tankless job
• Pool pump filtration system
•
•
failure
Replacing shorted schottky
diodes
Fault-finding an audio level
meter kit by ETI
*Dave Thompson runs PC Anytime
in Christchurch, NZ.
Website: www.pcanytime.co.nz
Email: dave<at>pcanytime.co.nz
ready to drop it in a rubbish bin at
Frankfurt airport.
I can see the advantages of tablets!
Even with a nice laptop bag, it was
such a hassle to take everywhere with
us. That’s even ignoring how much
of a pain it was to take it through the
customs checks in European airports,
where customs officers seem to assume
that every laptop is a disguised bomb.
I almost ditched our laptop due to its
weight and size, and in fact, I ended up
leaving it in Croatia, where we spent
most of our time over there, rather than
lugging it back with us.
That was an everyday laptop with
a then-standard 15-inch screen; this
Alienware thing I had in the workshop
weighed at least three times as much,
and the ‘bag’ that came with it looked
(and felt) more like a shoulder-borne
suitcase than a laptop bag. So, it’s a
very large and well-appointed gaming laptop intended (I assume) to be
sat on a desk and not moved unless
absolutely necessary.
I’ve worked on this machine before,
mainly to rectify the odd software/
operating system glitch or similar
small-fry stuff. Nothing too serious.
July 2021 91
But then the owner brought it in one
day last year with a problem; he’d lost
video output, but just before that, the
hard disks could no longer be ‘seen’
by the computer, and he was having
that old chestnut “disk boot failure”
message.
A crash course in RAID
While a common enough message
with standard machines, the fact he
had two hard drives in a RAID configuration made this a little more atypical, and not a good sign. RAID stands
for either “redundant array of independent drives” or “redundant array
of inexpensive disks”, depending on
whom you ask.
RAID is not just a fly spray; it is a
range of configurations used by computer people to ‘gang up’ hard drives.
A server machine, for example, might
spread its data storage over several
separate disks, or ‘mirror’ data over
many disks, so not all their eggs are
in one basket.
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The theory goes that if one hard
disk fails (as they are wont to do), the
others should still have a copy of the
data and business can continue until
the faulty drive is replaced (usually
via a hot-swappable drive bay).
The whole RAID thing is way
beyond the scope of this column; needless to say, the way the twin hard disks
in this machine were configured meant
that data reads and writes were split
between the two disks (known as striping), and this makes for excellent performance. The read speeds approach
twice that of a single drive.
Many gaming machines use this
type of RAID configuration, but the biggest disadvantage is that if one drive
fails, everything screeches to a halt,
and all the data is gone (unless it has
been backed up which is, of course,
always a good idea).
I feared the worst when the guy
brought the machine in. My first
assumption was that one of the drives
had failed and all we’d have to do is
Australia’s electronics magazine
kiss his data goodbye, provide a new
drive and reinstall Windows and his
software and games on a rebuilt RAID.
But no, there was something else afoot.
A regrettable decision
It turned out that he’d taken the
machine to another repair guy first.
This often happens with servicemen,
and there is nothing much we can
do about it. Customers can take their
devices anywhere they want, and
while it might sting a bit, such is the
life of a serviceman.
I’ve moved from several different
parts of town over the years, sometimes due to the quakes and sometimes
just because we moved house. While
some customers will follow me, some
will not, and I understand completely.
I certainly don’t begrudge people’s
decisions to go somewhere else; they
might not be happy with my work, or,
like in this case, they might live a fair
way out of town. While once my workshop was a lot closer to him, it is now
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much further away. He ended up taking this machine to a more local guy
rather than trudge all the way across
the city.
The problem is that the local guy
mustn’t have been very careful because
as he pulled the hard drive assembly
(consisting of the two hard drives)
from the motherboard, he tore the flexible PCB ‘strap’ that connected the twin
drives to the computer.
Not only did the strap tear, leaving
part of it behind still trapped in the
socket, but he’d also yanked on the
connector on the motherboard, which
looked to have come unseated, damaging the tracks and rendering the board
basically useless.
He’d simply put it all back together
(there is an easily-removed and
replaced cover that exposes all this
stuff) and given it back to my guy
claiming it was ‘dead’. He brought it
to me for a second opinion and, after
my diagnosis, was more than a little
miffed at being charged $150 by this
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other guy essentially to wreck his
machine. I said I’d see what I could do.
It turns out that I couldn’t do much.
Spares for these ultra-performance laptops are not readily available, especially those of this age. Dell couldn’t
help, so it was down to me searching
the second-hand market for parts.
Sourcing new parts
The first challenge was finding a
suitable hard drive connector. As it
turned out, AliExpress had plenty
of vendors selling the part, and
even though it was pretty expensive
($US65), I promptly ordered one while
I got on with the rest of it.
The vendor I bought it from had several other Alienware parts listed, so I
bookmarked that page just in case. The
part arrived six weeks later, but it was
the wrong one. They’d sent me one for
a three hard disk array; while I initially
thought perhaps I’d be able to use two
of the connectors, the connection to the
motherboard was very different.
Australia’s electronics magazine
This is the most frustrating thing
about buying from China; if they sent
the part shown in the product picture
and the specs below it (which we all
tend to buy from), it would be fine. As
it was, this part was useless. After the
usual to and fro dealing with the vendor, they sent another one, the right
part this time.
In the meantime, I was trying to remedy the broken socket on the board.
This is one of those PCB-mounted
sockets with a flip-down ‘bar’ that,
when toggled to the top, locks the flexible connector in once it is fully seated.
The other guy had simply pulled the
strap out, breaking the connector, tearing the flexible strap and, by the looks
of it, lifting some PCB tracks. This
wouldn’t be easy to fix.
While the sockets are available from
the usual suspects, I had no means of
repairing something like this. I didn’t
know how deep the damage went, and
I could spend hours trying to resolve
this for no good outcome. I bit the
July 2021 93
Helping to put you in Control
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Input accepts thermocouples J, K,R,S, T and
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PTC Digital ON/OFF Temp Controller
DIN rail mount thermostat with included PTC
sensor on 1.5m m lead. Configurable for a huge
range of heating and cooling applications. 230
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SKU: EEC-010
Price: $98.95 ea
Ursalink 4G SMS Controller
The UC1414 has 2 digit inputs and 2 relay outputs. SMS
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Price: $228.76 ea 20% off!
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Accepts 4~20mA, 0~10Vdc, is visible 50m
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10cm High digits. Alarm relay and 230VAC
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SKU: FMI-100
Price: $1099.95 ea
Touchscreen Room Controller
SRI-70-BAC Touchscreen Room Controller are attractive flush
mounted BACnet MS/TP controllers with a
large colour intuitive 3.5” touchscreen for
viewing the system status and modifying the
settings.
SKU: SXS-240
Price: $306.90 ea
For Wholesale prices
Contact Ocean Controls
Ph: (03) 9708 2390
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Prices are subjected to change without notice.
94
Silicon Chip
bullet and told my client that he needed another motherboard if this thing was going to run again.
He was actually fine with this, and asked if we could
take the opportunity to upgrade the video cards for better
performance. I checked with the vendor I’d been dealing
with, and he’d listed a couple of uprated graphics cards.
Not cheap at several hundred bucks each, but the client
agreed, so I ordered them along with a used motherboard.
The spending on this job was getting huge, so I hoped
what we got from overseas would be fit for purpose. I also
requested a progress payment, something I very rarely
do. But as the bill for parts was already nearing a grand,
I thought it prudent. The bottom line was that my client
loved this special machine and wanted it to work again;
as a serviceman, this is always my goal as well.
All we could do now was wait for the parts to arrive.
Given that the pandemic had just started and flights were
on and off, it took several months for the parts to arrive.
When they did, it was the video cards first, then eventually the motherboard turned up.
Many vendors post a video of the parts working on the
test bench, possibly to ensure there was no comeback if
something didn’t work. In this case, the vendor didn’t
show anything. I received the board, well-packaged, and
assembled the machine.
Not a good sign
When I fired it up, I had no video, which was the client’s original problem when he took it to the other guy.
No matter what I tried, I couldn’t get any video output.
The built-in HDMI port had nothing, with or without the
twin removable video cards installed. Something was off.
As was typical, dealing with these guys in China was
problematic. I’d spent many hundreds of dollars but
couldn’t get a straight answer. The board looked to be
faulty, and I arranged to send it back; a not inexpensive
task. Another month or two went by waiting for them to
receive the board.
They did get it, which was a miracle, as I’ve sent several things back over the years and not one has arrived at
the address provided by the vendor. I didn’t hold much
hope for this shipment either.
To be fair, it did arrive, and the vendor sent another
motherboard, which took the usual two months to get
here. My client was extremely patient, and hats off to him
for being so understanding. My hands were tied; there is
not much I can do in situations like this. Given the pandemic and the fact that the usual lines for parts are closed
or delayed, we didn’t have many options.
The new board duly arrived. Again, I reassembled the
machine and installed the graphics cards and other bits
and bobs. I left the top of the case off so that I could see
what was going on. On power-up, there was a puff of
smoke; it came from one of the video cards. My heart sank.
Now I didn’t know whether the graphics cards were faulty
or the motherboard. Perhaps the last one had been OK too?
This was a chicken and egg situation. I’d need knowngood graphics cards to test the motherboard, or a knowngood board to test the graphics cards. As it stood, I didn’t
know what was good and what wasn’t, and I’d possibly
just toasted a $500 motherboard. The serviceman’s lot
is not always easy, and in this case, things were turning
from bad to worse. What do I do now?
Australia’s electronics magazine
siliconchip.com.au
What I did was pull the plug. I’d gone about as far as I
could with this job. It was just under 12 months that I’d
had it in bits on the bench. I dreaded calling my client
and telling him the news, but I had to anyway. It’s the way
of the serviceman. Knowing when to pull the plug on a
dead-end job is something we all have to learn.
If we don’t know that point, we’ll end up wasting time
and money on something that isn’t achievable. He was
surprisingly OK with it and quite philosophical. He was
aware of the ups and downs of buying from overseas,
and I’d made it clear along the way that we were buying
second-hand parts, and things might not work out.
He’d purchased another machine in the meantime,
so at least he was up and running. While he had a lot of
sentimental affection for this old Alienware machine, he
accepted that sometimes it just isn’t feasible to carry on.
He was also happy to pay the costs of the hardware
I’d purchased. I didn’t add anything to those costs, and
donated my time (he was a loyal client). I just wrote off
the rest as one of those things that happens to a serviceman now and then when a job turns sour.
As a result of this long-time saga, I wound up with some
of the hardware. Whether I can move it on or use it anywhere is in the hands of the computer Gods.
I did transfer his data and photos to his new machine
(again not charged for), and he was happy, even though
his beloved Alienware laptop was dead. I was relieved
that we’d found a middle path and that he had everything
salvageable from the old machine.
Whether I will see him again, I don’t know. I did my
best, and if he wants to take his new machine elsewhere,
so be it. I’m not in business to lose money or clients, but
sometimes things just don’t work out, and external forces
can make or break a job. Whatever happens, life goes on,
and the next phone call could be a great job or a real challenge. That’s the life of a serviceman.
Pool pump filtration system failure
A. H. of Attwood, Vic, had a recent problem involving
some rain and a lot of mud. The problem continued with
the inability of his pool’s filtration system to cope, leaving
him with a pool pump that needed a repair...
While away on business, it rained what can only be
described as mud at home. This rain-mud turned our pool
into a murky red-brown colour. For reasons unknown to
me at the time, the pool filtration system didn’t cope. Fast
forward a few days, and when I had my first chance to
look at the pool, it was now a most unpleasant red-browngreen colour, and the bottom couldn’t be seen.
Obviously, something fairly serious had gone wrong
with the filtration system. Checking revealed the Chromatalyser complaining that there was no water flow for
it to carry out sampling for Chlorine/PH levels. This was
strange, as the system is fully automatic, injecting acid
as required as well as controlling a Chlorinator to adjust
chlorine levels.
Overriding the system and turning on the filtration
pump revealed a distinct lack of motor noise and an
“Err64” message. This pump is a 9-star energy efficient
variable speed Hayward Tristar model SP3215VS and is
an absolute beaut when it works. The pump operating
manual revealed that “Err64” is apparently an “Internal
Short Circuit Failure”.
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Australia’s electronics magazine
July 2021 95
This sounded pretty ominous,
although Hayward’s cure for this fault
was to turn it off and back on, which
of course didn’t help. So I was now
up that well-known creek without a
suitable motive implement.
A weather forecast of 30-40°C for
the next few days, with the wife and
kids insisting that they would need to
use the pool, meant that I had to fix it
immediately, if not sooner. So I was
forced to shell out over 1500 Aussie
dollarydoos for a replacement pump.
With the new pump installed and
running, the pool returned to normal
crystal clear water within a day or so.
With that crisis averted, my attention
turned to the old pump turned doorstop.
Hayward pumps are very serviceable and easy to fix, but the electric
motors that drive the pumps are not.
In fact, there is no parts breakdown
for the motor assembly at all, just the
pump section.
My admittedly limited knowledge
on variable-speed drives made me
think that the power switching module, or similar, would most likely be
the culprit. So I commenced ripping
the control box that was mounted on
top of the motor apart.
This revealed a circuit board with
many components on it, but no
power switching module. Inspection
revealed a few connectors going into
the bowels of the motor, where another
circuit board was located.
While playing around with this top
board, something went “pfzzzt”, and
the motor was completely dead. No
display, no “Err64”, nothing.
This top board appears to be a power
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Silicon Chip
filter/power factor correction/high
voltage DC supply/soft-start device. It
magically creates over 300V DC which
is sent to the lower board. A 12V DC
supply rail is returned to the top board
for power as well as some switching
signals for the soft-start relay. So it
was time to gain access to the motor
internals.
Unfortunately, the manufacturer of
the motor had used those stupid headsnaps-off-when-correctly-torqued
type of bolts, which meant that they
couldn’t be undone. A hacksaw made
short work of that, and the motor split
apart to reveal its secrets.
I checked the motor windings and
found no problems, so my attention
turned to the internal circuit board.
I expected to see a spectacular mess,
but no, the board was remarkably clean
with no noticeable damage.
Unbolting it from the housing and
turning it over revealed a “Dual Inline
Intelligent Power Module” (IGCM15F60GA). Sure enough, desoldering
and resistance-checking this module
revealed a short circuit between the
“Motor V-Phase Output” pin and the
“V-phase Low Side Emitter” pin. So it
looked like my hunch was right.
Further troubleshooting on the
top board revealed a low resistance
between Vcc and the S-GND pin on
the power factor corrector SMD IC
(L4981BD). This was dragging the
12V DC rail down and shutting down
the whole pump. Removing this IC
returned the pump to its original “Err64” condition.
I had nothing to lose,
so I placed an order for a
new IC, power module and
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some bolts. A week later, the parts
arrived, were soldered into place and
the motor roughly slapped together for
testing. At power-on, I was rewarded
with the sweet sound of a motor spinning up to 3000RPM. Success!
I reassembled the whole kit and
kaboodle after a careful inspection of
all the pump seals etc. I checked it for
faults with my PATS tester (all good!)
and reinstalled it into the filtration
system for testing, where it has now
worked for three weeks with no faults.
For a total cost of around 30 bucks,
I now have a working spare pump. I
will probably never need it, but Murphy’s Law dictates that if I sell it, the
next day the operating pump will
cark it, and I’ll have to come up with
another $1500...
Replacing shorted schottky
diodes in equipment
R. S. of Fig Tree Pocket, Qld, has a
couple of servicing stories, one about
parts he has found to fail frequently,
and another about turning two dud
devices into one good one...
I am finding many failed 200V
schottky rectifier diodes in equipment that I am repairing. Hopefully,
the manufacturing process for these
diodes has been improved since these
ones were made.
Samsung monitors can have a
shorted MR5200 (5A, 200V) in the
power supply. There are two of these
diodes in parallel. Sometimes one will
siliconchip.com.au
short out, stopping the monitor from
working.
Ryobi battery chargers (BCL14181H)
also have two MR5200 in parallel, and
one can short out. These chargers can
also have a shorted P-channel FET
(which feeds the charging current into
the battery pack).
The Dyson charging plugpack
(Salom Model 17350-05) can have a
shorted MR2200 (2A, 200V). You can
crack these plugpacks open in a vice.
Strangely, these have three output
connections: 0V, 16.75V and 24.35V.
The other Dyson plug pack (Model
205720-05) has only two connections,
0V and 26.1V.
Dyson DC35 motors are a brushless
DC motor, with a permanent magnet
rotor driven by coils on the stator, powered by two half-bridges. The rotor has
only one bearing at the fan end. As
there is no bearing at the motor end to
centre the rotor in the stator, mechanical inaccuracy can cause the rotor to
rub on the stator. The motor then just
buzzes but does not turn.
To get the plastic back off the motor,
hold that part in a vice, and then grab
the rest and pull. I found this worked
better than trying to pry it off, which
damages the plastic.
The first motor I came across was
rubbing, and it was difficult to centre. Sometimes it would work, and
then it would not. The second motor
had a fault on the drive board with
one of the components sending up
a wisp of smoke. So I took the drive
board (which includes the stator) from
the first motor, and put it in the second motor.
The two large capacitors on the
drive board have glue on their tops and
must be pried loose. You only have to
resolder the power connections. This
was successful, resulting in one good
motor. I noticed the second motor was
better mechanically than the first, with
larger mounting screws for the board,
so the design may have been modified
during production.
The adjacent photo is the power
supply board for a Dell U2414Mb
monitor, showing yet another example of a shorted schottky diode fault.
The 150V, 8A SB8150 used for D702
at left had failed; I replaced it with a
5A, 200V rated SR5200.
Editor’s notes: 200V is at the high
end for schottky diodes, which more
commonly are rated for a PIV in the
range of 20-100V. So perhaps they are
siliconchip.com.au
The power supply board for a Dell U2414Mb monitor which shows an
example of a shorted schottky diode circled in yellow.
pushing the process to its limits, resulting in more failures in service. As for
the Dyson plugpack with two output
voltages, perhaps this suits two different vacuum models with different
battery voltages.
Fault-finding an ETI LED audio
level meter kit
N. B. of Wollongong, NSW, ran into
a problem putting together a kit when
he had built several others of the same
type successfully. The solution turned
out to be simple, but hard to believe...
Over the years, I have assembled
several kits of the ETI Bargraph LED
audio level meter. The kits cost about
$33.00 and took about half an hour to
assemble. They all worked well, except
the most recent one which I assembled
some years ago. It wouldn’t work, so I
put it aside and forgot it till recently.
I then needed an audio level meter
for a project, so out it came. I checked
and rechecked everything, and it all
Australia’s electronics magazine
seemed fine, but it still didn’t work.
Signal was getting to the processing IC; all voltages were as expected.
I had a spare processor, so I fitted it,
expecting it to work. It still didn’t. I
then did a diode check on the display
bar with its 10 coloured rectangular
LEDs, seven green and three red. They
all checked out OK.
Out of desperation, I decided to
compare the LED bar assembly on
the board with a new one which I had
recently bought. The bar is a preassembled commercial unit. To my amazement, I discovered that the LEDs were
all inserted in the escutcheon bar the
wrong way around!
I desoldered the whole thing and
found that I could coax the LEDs out
of the escutcheon bar with a pair of
longnose pliers. I refitted them the
right way around, resoldered the bar
to the PCB and hey presto, it worked!
I must confess that I felt a great victory
in finding that fault.
SC
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