This is only a preview of the June 2021 issue of Silicon Chip. You can view 37 of the 112 pages in the full issue, including the advertisments. For full access, purchase the issue for $10.00 or subscribe for access to the latest issues. Items relevant to "Advanced GPS Computer - Part 1":
Articles in this series:
Items relevant to "Recreating Arcade Pong":
Articles in this series:
Items relevant to "PIC Programming Helper":
Items relevant to "Programmable Hybrid Lab Supply with WiFi – Part 2":
Purchase a printed copy of this issue for $10.00. |
SERVICEMAN'S LOG
Trying to fix unbranded, generic equipment
Dave Thompson
The first step in sourcing spare parts for a faulty piece of equipment is
to take the manufacturer and model details and do some searching to
find out if the manufacturer or a third party has spare parts available.
But what do you do when there is no apparent manufacturer or model
number? Go on a wild goose chase, it seems...
Items Covered This Month
Sometimes a job comes through the
replacement tyre took many months to
workshop that is a bit out of left-field.
I’ll take a look at anything; if nothing
else, it’s all experience. Recently, I
received a call about an electric scooter
that had failed. This was one of these
‘friend of a client’ type deals, and I,
for one, appreciate such referrals. In
business, getting work this way sure
beats paying for expensive advertising.
This ‘scooter’ was a cheap import.
While this doesn’t necessarily indicate that it will be a tricky job, I’ve
been down this path too many times
before to assume it will be an easy
repair. According to the customer, in
the 18 months they’ve owned it, the
thing has spent more time off the road
than on it.
The tyres were the first
problem, with the rear
tyre blowing early on. It
was apparently paperthin and not fit for
our rough roads. A
siliconchip.com.au
source, and had to come from Europe.
Not an auspicious start! Then it simply stopped working.
The owner brought the scooter into
my workshop, and after the usual discussions about terms and conditions
and possible outcomes, I dug into it.
This isn’t one of those thin-line
electric scooters you see hipsters
riding all over town on. This model
is about the size of those mini-bikes
Honda used to make back in the 70s,
before the powers-that-be
decided they were too
dangerous for the
average citizen.
Australia’s electronics magazine
• Fixing generic equipment is
•
•
•
•
frustrating
Arlec battery charger repair
Fixing a 50in Panasonic TV
backlight
Failing capacitor in clothes iron
Mazda 3 aircon repair
*Dave Thompson runs PC Anytime
in Christchurch, NZ.
Website: www.pcanytime.co.nz
Email: dave<at>pcanytime.co.nz
June 2021 91
It has fat little 10-inch wheels, proper mudguards, apehanger handlebars and a comfortable padded seat. It’s more
like a small electric motorbike than a scooter.
The various controls also mimic a motorbike; a twist
throttle and front brake handle on the right, with back
brakes on the left grip. It has a headlight of sorts, a taillight, and a sturdy kickstand.
It is driven by a brushless electric motor integrated into
the rear wheel hub. A standard key lock switches it on
and off, and a small electronic display on the bars indicate the juice remaining and some other telemetry I haven’t been able to determine yet.
I know the display can show other items because if I
angle it to the light, I can see several other ‘icons’. My
guess is that this is a generic display and is used on many
other devices. This one is just wired to show the rider
whatever information this manufacturer wants us to know.
It’s all actually quite solid and well-made, but while
it’s a step up from those rental scooters, it isn’t really a
motorbike either. Still, it suited the owner’s requirements
of buzzing a relatively short distance to work and back
each day in relative comfort. Or would if it was working, anyway.
I would love to have a ride on it, being an avid motorbike rider myself (though not for a few years now), but
unfortunately, it wouldn’t move under its own steam.
While it powered on and the battery bar-graph style indicator on the handlebars showed plenty of herbs, twisting
the grip did nothing.
All the other electrics worked, which was a good sign.
Also, the guy (a skilled retired avionics engineer) who
referred this client to me had ‘run his Fluke’ over it, looking for things that could potentially go wrong, but he had
not found anything obvious.
He did re-terminate some of the connections to the controller in case there was something dodgy there, but the
problem remained. He figured it must be either a controller or motor fault, at which point he recommended that
the owner bring it all to me.
it isn’t all potted together with impenetrable goo, and the
numbers are still left on all the components, I likely won’t
find a circuit diagram for it anywhere.
Reverse engineering the controller to draw one up
would take hours of headaches and all with no guarantee anything would work anyway. What fun the serviceman’s life can be!
I then went with basic specs. I know the battery is a
48V Li-ion job, and it is easily removed after unplugging
the single heavy-duty ‘E’ connector. The battery at least
has all the specs printed on a label. Nothing else is identified, though.
The wiring to and from the various bits and bobs looks
to be colour-coded, though whether this code matches
anything else remained to be seen. The controller box
also appears quite well-made, from the outside at least.
It is a sizeable chunk of hollow, extruded and patterned
aluminium, with what appears to be integral heatsinking
along one side. It has shaped aluminium caps screwed on
at each end, using what appear to be ordinary PK screws.
All the cables pass through sealed holes in one end of
the controller, and the whole caboodle is stuffed into a
protected gap in the chassis, along with the battery, below
the seat and foot-well area. A key-operated moulded plastic panel covers it all up, and there are basic weather seals
along all exposed joints.
The controller must be at least partially working,
because if we insert the key and turn it on, we get the
battery-level indicators on the dash, and the lights and
other stuff works. If the motor had simply burned out, we
would get the same symptoms – lights but no action. It is
also possible that the motor-driver section of the controller has failed, but the rest of it is still working.
A frustrating search
After confirming the symptoms described above, the
next step was to try to identify this vehicle. It has no
brand name printed on it, nor does it have any part or
serial numbers anywhere. Par for the course.
A Google image search picked up a few similar bikes,
available from the likes of eBay, AliExpress and Banggood,
but nothing exactly like this one that could give me some
clues as to its identity. The company it was purchased
from 18 months ago were of little help either, having no
spares available.
My guess is that this is a generic bike, with various companies using the chassis, controllers and other bits and
pieces to make ‘their’ version of it. They then sell them
all off and move on to the next project.
This has pros and cons for me; if the controls and hardware are generic, I should be able to find similar (if not
necessarily identical) parts from any of these suppliers
who sell such hardware.
I’d have to drill a little deeper into the individual components and try to identify them.
I know what you’re thinking; fat chance! Even if I can
open the hefty extruded-aluminium controller box, and
92
Silicon Chip
Australia’s electronics magazine
siliconchip.com.au
Opening up the controller
So opening the controller up was my next step. Removing the controller is a bit of an act, because there are terminals and wiring going everywhere. There are four quite
heavy-duty main drive cables coming from the controller, and these terminate onto posts moulded into a large
hard-plastic block that keeps them all physically and
electrically separated, but close together in the same area.
These connections need to be undone with a socket
driver. The other wiring is generally a lighter gauge and utilises removable connectors (some installed by my friend,
some that look factory), making removing the controller
relatively straightforward.
The problem with the motor being potentially unserviceable is that I can’t easily test it. It is a brushless type,
so it needs a suitable controller to make it work. Just connecting it directly up to the battery isn’t going to make it
go, and in fact, would likely damage it.
Except for the different type of motor, this whole job
reminded me of a treadmill I repaired a while back. That
too powered on and showed lights, but had no motor drive.
The treadmill used a 12-130V DC motor, and I tested
this by hooking up a car battery to the motor’s red and
black wires. While it moved slowly at 12V, it at least
worked, which told me it was probably OK and the controller had likely failed.
That unit was ‘simply’ a DC speed controller; altering
the power level to the motor increased and decreased its
speed. These (for me, at least) are a bit easier to troubleshoot. In that instance, I replaced all the IGBT output
devices (which were blown), but I also sourced a new
controller board, just in case my repair failed. That repair
worked, so at least I now have a spare controller in case
it goes again.
There were more differences between that job and this
one, though. That board had part and model numbers
clearly printed on it, making it a doddle to find a replacement. Perhaps I’d be lucky here too?
With the controller sitting on the bench, I could more
easily remove the end caps and see if I could extract the
PCB from the interior. One long side of the board is taken
up with an array of what appear to be Mosfets, or perhaps
IGBTs. These all bolt directly to a piece of bar aluminium, and then this is bolted to one side of the controller
case with a smear of heatsink compound and four bolts.
These four bolts also had to be removed before I could
slide the board free. Once all the fasteners were out, the
board came out without any problems.
The first thing I noticed was how light-weight the componentry looked. That treadmill controller I worked on
was a hefty beast with a large external heatsink, and it
was mounted away from everything with lots of room for
cooling air. This little brushless driver, which admittedly
only has to cope with 48V, must be quite efficient given
the small size of everything.
Or, perhaps it is built down to a price, underrated and
too weenie for the size of the battery involved, which
might also explain why it isn’t working.
No obvious problems
A closer inspection revealed no burning, discolouration, overheated rails or any other obvious damage to the
board. There was also none of that acrid ‘electrical’ smell
siliconchip.com.au
Australia’s electronics magazine
June 2021 93
we’re all so familiar with that usually
indicates something is wrong. I didn’t
fancy pulling the very closely-packed
output transistors to test each one, so
I made do with trying to find part or
model numbers I could cross-reference. Nothing.
And while some components (quite
a few SMDs and the like) did have
visible numbers, a lot didn’t either. If
I could find a data sheet for the numbered ICs, there might be a reference
circuit I could check out.
Either way, I was stuck; I needed
a known-good controller to test the
motor, or a known-good motor to test
the controller.
Back to Google image searching.
After trying various search terms, I
began to see some familiar results.
I found plenty of controller boards,
but none looked exactly like this one.
There were also many different types,
with seven, nine and sometimes 12
output devices for the various sizes
and voltages of scooters, bikes and
batteries.
I had a lot better luck looking for
the entire controller itself. While it
also has no identifying labels, it did
look very similar to many of the image
search results. I narrowed things down
until I had pages of almost identical
controllers in the results. The cabling
on each was one of the few visible
differences between them, with the
controllers shown mainly having one
of three different configurations.
The controller I had looked to be a
widespread type, which was a welcome discovery. Another difference
was the physical size; controllers for
72V systems are far larger than their
48V counterparts, so again, I could
drill further down into what I was
looking for.
The surprising thing is that I was
expecting that even if I found one, the
controller would be stupidly expensive. That treadmill controller was
almost (but not quite) prohibitively
expensive, though I deemed it worth
it at the time to get one. The controller I found for the scooter is from AliExpress and costs just US$25, plus a
couple of bucks shipping.
I was gobsmacked. How can these
devices be made for such little money?
The fancy piece of aluminium extrusion it is all contained in must be
worth more than that by itself.
There were a few sub-types listed,
so I ordered the version intended for
a 48V electric vehicle with a brushless motor. It looked to have identical
connections and overall physical size
to the one I already had. Hopefully,
what arrives will be what was in the
product pictures; more than once, I’ve
purchased items from the product
description and received something
very different.
If all goes well, it will at least help
me determine whether the controller
or the motor is causing problems, and
the negligible cost can be wrapped up
into the assessment phase of the job
without significant financial outlay.
It is undoubtedly cheaper than
sourcing and buying a new motor/hub
assembly – which we might yet need
to do – but for now, it will tell us all
we need to know without throwing
good money after bad.
At the time of writing, I’m still waiting for the controller to arrive. Given
current world events, it’s no surprise
shipping is slow. I’ll let you know
what happens.
A happier ending
In the meantime, I got a call from
an out-of-town rep for a company that
provides exercise equipment for gyms
and retirement homes. He had a dead
machine in one of their spaces down
here and an open day the following
day. He wanted me to make an assessment or repair (if possible) of the controller board, which he would remove
and bring over, along with the external
power supply.
I agreed, and offered assistance if
he needed it. He didn’t; the controller
came out easily, and a fault was immediately apparent; a 47μF 35V SMD
electrolytic capacitor had exploded.
He brought the board to the workshop, and we agreed that I would swap
out the cap. If it blew again straight
away, he’d return the board to the
manufacturer for a replacement and
forgo the open day. I soldered in a new
cap, and we held our breath while we
powered up the board, watching as
the status lights lit up one by one. His
grin said it all.
He went back, reinstalled the board,
fired up the machine, and the open
day was a success. Sometimes we just
get lucky!
Arlec battery charger repair
B. C., of Dungog, NSW took some
time to refurbish an old Arlec battery
charger that had seen some rough use,
but it is now back into tip-top condition...
I got an Arlec PS439 30 Deluxe Battery Charger from the local recyclers
which wasn’t working. Also, the top
cover was in pretty rough condition; it
looked like it may have spent its former
life at a local motor garage. My friend
said he would clean it up and respray
94
Silicon Chip
Australia’s electronics magazine
siliconchip.com.au
the top after I got it working.
Removing this cover revealed an
accumulation of debris and also some
corrosion on the power transformer,
heatsinks and the control PCB. Careful use of a toothbrush, paintbrush and
solvent cleaned up most of the mess.
Scraping, followed by an application
of rust converter cleaned up the power
transformer laminations.
Fortunately, the front panel with the
ammeter, timer and switches had been
protected by the overhang of the top
cover, and only required light cleaning. I was then able to greatly improve
its external appearance using Nu Finish car polish on the case paintwork.
I then sent a technical request email
to Arlec in Melbourne and received
back two circuit diagrams, a control PCB layout drawing and a “current-control switch connections”
drawing. Interestingly, the drawings
were all done in 1983. Talk about the
thorough technical support for Australian made products!
This battery charger was a wellmanufactured product and was meant
to be foolproof to use. The charger
would only work if the battery had
some residual charge left in it and the
connection polarity was correct. There
are now plenty of modern chargers that
use a similar system.
Looking at the circuit diagram, I
discovered that there are two main
high-current secondary windings on
the power transformer. A rocker switch
selects the voltage to feed through a
rectifier block to charge either a 6V or
12V lead-acid battery. A large rotary
switch is then used to switch through
a series of voltage taps to give current
siliconchip.com.au
control of the output, as displayed on
the ammeter.
A timer gives the user a preset
charging time, to avoid battery overcharging, particularly on the higher
current settings. There is also an extra
transformer winding which gives a
regulated 12V rail to run the control
PCB electronics.
After some basic voltage checks, I
traced the fault to a lack of 12V at the
output of the series regulator. This
was because the TIP31C transistor
(mounted on a small heatsink) was
faulty. I also found that the BZX79C13
13V 0.5W zener diode controlling the
voltage at the TIP31C base had gone
short-circuit. Replacing these two
parts brought the Arlec charger back
to life.
I then connected it to a partially
charged car battery and set the timer
to complete the charging cycle. As
promised, my friend resprayed the
top cover to match the orange enamel
finish of the chassis. This charger now
sits proudly on a trolley in his garage.
Fixing the backlight in a 50in TV
P. M. of Christchurch, NZ, had a
badly-timed failure in a 50-inch LCD
TV. Luckily, he has quite a bit of TV
repair experience, so was able to tackle
the job...
As New Zealand was under “lockdown”, all businesses except essential services were closed, and everyone was told to stay at home. This
meant that the home TV had become
an essential entertainment and information device.
Two days in, and suddenly our
Panasonic 50in LCD in the lounge had
Australia’s electronics magazine
no picture. I have been trained to service TVs, but that was many decades
ago when TVs had CRTs. But it looked
like I had little choice under the circumstances, and attempted a repair.
I soon had the beast off the wall
and face-down on the kitchen table.
I removed the back, hoping to find
some sick-looking electrolytic capacitors which I could easily replace. I
was surprised to see how few electros
there were. None of them looked sick,
and all tested OK with my ESR meter.
I was surprised at how sparse the
interior was, with a power supply
board in the middle, a small video
board on the right, a backlight driver
board on the left and a display driver
board at the bottom.
The power supply rails all looked
good, but I was not so sure about the
backlight driver outputs. I managed to
find a manual online, but the driver
board was mainly SMD, and I didn’t
have high hopes about being able to
fix anything.
In the meantime, I put a 32in Panasonic from another room on the wall in
the lounge. After a day or so of squinting at it, I decided to have another look
at the 50in set.
Inside it, I noticed a label saying the
display was made by LG. I Googled
‘repair 50” LG TV’ and found several
hits on replacing the backlight LEDs.
It seems this is a common problem
with some models, made worse if the
user chooses a high brightness setting.
Gaining access to the backlight LEDs
involves removing the LCD panel from
the housing. In the Youtube video
(https://youtu.be/CHmHb-Dxx3Y),
the repairman used two suction cups
June 2021 95
attached to the front of the panel to lift
it out. Not having those suction cups
meant I probably couldn’t continue,
but then I remembered that we have
a handle in our shower which is held
on with suction cups (as shown in the
photo at lower left).
This handle was not ideal because
the cups are quite close together,
unlike the separate ones used in the
video. I attached it carefully to the
screen after removing the bezel, a
bunch of screws and two flat ribbon
cables. When I started lifting it, the
panel got a bit bendy at the ends, but
I managed to set it down safely.
There are three sheets of Mylar
that act as a diffuser to remove, and
beneath those are six rows of 10 LEDs
(as shown in the photo on page 95).
The LEDs are on strips of circuit board
which plug into a connecting circuit
board at the right-hand end. They
are wired in series, so with the aid of
my bench power supply set to 30V at
20mA, I was able to power each strip
separately, to find that two strips did
not work.
Upon closer inspection, I noticed
a discoloured LED on one strip but I
had to find the faulty one on the other
strip with the aid of a meter.
Not having suitable replacements on
hand, I decided to simply short out the
two faulty LEDs, and because they are
wired as two strings of thirty, it would
probably still work fine.
I carefully reassembled everything
and held my breath while I switched
it on. It worked just fine, and the only
time you could tell two LEDs are missing is on a pure white screen. Even
then, it is not that obvious.
The YouTube video had a link to a
store which sells a full set of replacement strips for US$60, so I will order
a set when I can.
The heatless clothes iron
R. S. of Fig Tree Pocket, Qld, had
a problem which has been repeated
many times over the last few years in
these columns. You may get a sense of
deja vu while reading it...
Our Braun clothes iron stopped
heating. It was more than two years
old, so already out of warranty. If you
take the grey rubber pad out of the
end of the iron, you can undo two T20
‘security’ screws. This allows the end
to come off, and there is a black plastic
box with a small circuit board inside. It
contains an unmarked surface-mount
96
Silicon Chip
8-pin IC with its supply regulated by
a 5V zener.
The low-voltage supply from the
mains is via a 220nF 220V AC rated
X2 capacitor and a resistor. The capacitor tested OK using the capacitance
range on a Fluke 77 IV multimeter, but
I replaced it with another 220nF X2
capacitor, and the iron now works. It
seems that the capacitance is lower at
high voltages. I note that the replacement capacitor was many times the
size of the original.
This is another example of highvoltage series capacitor failure. I notice
that the inverters in microwave ovens
use a high-wattage resistor to drop the
voltage for the control circuit. This
is more reliable, but with a higher
power loss.
Mazda 3 aircon repair
D. W., of Georges Hall thought his
daughter’s car might have had a serious malfunction buried deep within,
but luckily, it turned out to be a much
simpler (and cheaper) fault than originally envisaged…
My daughter told me that the air
conditioner in her 2008 Mazda 3 was
playing up. It didn’t work straight
away; the car had to be running for
about 15 minutes before it would produce cold air.
Up close to the front of the car, I
could hear a strange noise from under
the bonnet somewhere. It sounded
like it could have been a compressor
belt or clutch problem. Maybe one or
the other was slipping a bit, but then
it eventually grabbed. That might
explain the delayed turn-on.
Maybe the belt had stretched or
worse, the compressor could be on its
way out. A faulty compressor would
probably be a costly fix.
That night, I found myself on YouTube searching for Mazda 3 aircon
compressor faults and fixes. Sure
enough, there were a couple of detailed
and somewhat educational video clips
depicting Mazda 3 compressor and
clutch faults and fixes.
A couple of days later, my daughter brought her car over, and I had a
bit more time to look at the problem.
Thanks to the YouTube video clip, I
knew where to look for the compressor. The noise I had heard previously
wasn’t evident on this occasion. Turning the aircon on and off and watching
the compressor belt and clutch didn’t
reveal anything unusual to my eye.
Australia’s electronics magazine
I noticed a slight coating of frost
on one of the compressor pipes, so I
thought that the compressor must be
doing its job.
I was now getting that feeling that I’d
missed something. While sitting in the
car operating the controls and mulling over things, it suddenly dawned
on me that there was no airflow from
the outlets in the car. Regardless of all
else, there should be airflow.
The fan control knob appeared to
be working OK as the dash LCD was
indicating the different fan speeds. So
it was not a compressor belt or clutch
problem; it was a fan blower problem.
Not for the first time, my brain had led
me up the garden path. So I headed
back to YouTube for more advice.
YouTube has a lot of video clips on
Mazda 3 fan blowers. Unfortunately,
everything is located up behind the
glove box, and it’s hard to get to the
fan assembly.
I realised that since the blower fan
does come on after a delay, the fan
itself must be OK. So I had to think of
what else might be causing this problem. I checked the 40A blower fuse
(marked heater) and it was OK.
Next, I pulled out the small
quick-connect blower relay (also
marked heater) close to the fan blower
fuse and tested it on the bench with
a 12V power supply and multimeter.
And that was it! I could hear the relay
clicking in and out, but the contacts
were simply not closing.
It was easy enough to lever off the
relay’s dust cover and inspect the SPST
contacts. I set about cleaning the contacts with wet and dry and contact
cleaner but surprisingly, to no avail.
While testing the relay, I could feel the
relay getting warm while energised,
and after about 15 minutes just sitting
on the bench, the contacts eventually
closed, as if by magic.
I think heat and fatigue over the
years had affected the spring steel
relay contact arm. As a temporary fix, I
bent the arm a fraction of a millimetre
to close the gap a bit. After replacing
the dust cover and returning the relay
to the car, the problem had obviously
been licked.
I’ll source a new relay in due
course, and I’m still a little worried
about that noise I heard initially, but
hopefully it was just the blower fan
operating erratically with its control
relay making dodgy contact. Time
will tell.
SC
siliconchip.com.au
|