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SERVICEMAN'S LOG
If it isn’t one thing, it’s another
Dave Thompson
Sometimes, even when there are no customers lining up, work comes
along anyway. It isn’t always welcome, but when your tools go
down, you have to fix them. It doesn’t help that I’m afflicted with the
Serviceman’s Curse, so I’m allergic to paying for replacement tools when
it’s possible to (uneconomically) fix them!
Over the past year, plenty of local
businesses have folded; there simply
isn’t the customer traffic to keep the
doors open any more due to lockdowns
and general economic malaise.
While our overall revenue has
dropped, as you would expect with
a lot less work coming in, the silver
lining is that I finally have some free
time to get onto those little jobs that
I’d been putting off.
Those of you who live the rock and
roll life of a serviceman know that
sometimes things don’t go according
to plan. An anticipated five-minute job
can easily turn into a two-day mission
in the flash of a shorted battery connector or a clumsily-placed screwdriver.
That sort of thing doesn’t happen to me,
of course! But I do hear rumours that it
happens to other, less-careful people.
The first small job created itself
when I went to use my soldering station, and the pencil was still cold 10
minutes after I switched it on. The astute among you will know soldering
irons are meant to be hot, so the fact
that I could hold on to the wrong end
need,
of it without being burntyou
told me
that
something was up!
The pencil connects to the soldering
station using one of those multi-pin
screw-on plugs, sometimes called a
GX-16 series connector. I removed and
re-connected it, and it seemed sound,
so I guessed that the pencil’s element
had gone open-circuit.
Confirming this theory proved to be
more difficult than I imagined, mainly because the pencil itself appears to
be a moulded unit. Everything is set
into it at manufacture, and it cannot
be disassembled to reveal the innards. The cable stress reliever at
the bottom can be prised out, but
the element appears to have no
means of being removed, other
than by cutting into the pencil’s
plastic body.
This makes them inexpensive to
manufacture, but not great for repairs. I think they expect people to
throw away the dead pencil and buy
a new one. The problem is that I’ve
used this pencil for a while now and
having just ‘broken in’ a new tip, it
is perfect for the work I do. To bin
it without at least trying to repair it
you want.
would be, well, frankly against my
serviceman’s code!
So electrical checks would have
to be made via the GX connector. I
For full details on how to enter, drawing & rules head to: jaycar.com.au/dmax-jaycar
Items Covered This Month
searched for circuit diagrams online
for my model. Once located, my mul• It’s always the other thing
timeter confirmed there was no resist• Coin counter repair
ance or continuity through the element
from any of the pins, let alone the
• Alternative security systems
designated ones, which told me all I
• LED rose garden repair
needed to know. It was dead!
• Electric fence energiser repair
get
that thing
win
that thing
SPEND $50 OR MORE FOR A CHANCE TO WIN AN ISUZU D-MAX
*Dave Thompson runs PC Anytime
in Christchurch, NZ.
Website: www.pcanytime.co.nz
Email: dave<at>pcanytime.co.nz
siliconchip.com.au
Borrowing a spare
Fortunately, I have a spare pencil.
But when I say spare pencil, I mean
spare soldering station. While it is very
much like my usual one, I originally
Australia’s electronics magazine
March 2021 61
*
purchased it as a desoldering station.
My faulty unit has a temperatureadjustable soldering iron on one side
and a hot air wand on the other. In
contrast, the ‘spare’ station has the
same soldering iron setup, with a
temperature-adjustable desoldering
gun and suction pump arrangement
on the other.
The desoldering ‘gun’ on this station looked great on paper, but doesn’t
work well in practice. The ‘real’ version this unit was copied from might
work very well, but this one doesn’t,
at least for me.
It has one of those pistol-grip style
handles, with a hollow, heated tip.
Pressing the ‘trigger’ on the handle
activates the suction pump, so I can
theoretically hoover up the molten
solder. Sadly, it is useless; it wouldn’t
suck the froth off a lager.
Also, the element won’t ‘take’ solder, similar to the metal on some cells;
the solder simply doesn’t stick to it.
I’ve tried ‘seasoning’ it with various
solder pastes to no avail. So trying to
heat a solder joint is a lesson in frustration.
The bottom line is that I’ve never
gotten it to work, which is why it sits in
the corner of the workshop. I expected
it to work as well as the other station,
but it just doesn’t. I’ve long accepted
this and have moved on.
On the plus side, the integrated
soldering iron has almost never been
used. I simply unscrewed/unplugged
that pencil and installed it on my other
station, which immediately resolved
my cold-tip issue.
However satisfying this quick-fix
may have been, I still had a dead pencil, and by extension an incomplete
soldering station (useful or not). And
as a serviceman, that bothered me.
A quick search on AliExpress revealed that a replacement element
was available for just a few dollars.
Or, I could get a whole new pencil and
cable/connector for only a few bucks
more than that. Even better (for a tool
junkie), a new pencil plus two spare
elements could be had for around the
same money! You already know which
option I went for. Of course I am going
to try to fix the broken one.
Now I know what you are thinking;
did I fire six shots or only five? Oh no,
sorry, wrong script. You are thinking
that if the pencil is moulded and cannot be disassembled, how will I replace the element?
62
Silicon Chip
Well, I’m glad you asked as it’s a
good question! Anything can be disassembled with the right tools and the
right attitude. A hammer tap here, or a
Stanley-knife blade applied there, or
even a junior hacksaw placed just so
can achieve amazing results.
These apparently-sealed devices
can be opened, repaired and glued
almost seamlessly back together without anyone (but us!) knowing about it.
I used to watch Dad opening moulded-plastic power supplies using a
carefully calibrated hammer tap, and
when the thing was repaired, he simply glued it back together.
That was in the days when such
power supplies cost a small fortune
and were worth repairing. That obviously isn’t the case today; I literally
have cartons full of these supplies
that will likely never be used, but the
philosophy of the repair still stands,
and I thank my Dad for passing that
on to me.
I wouldn’t usually do this for a paying customer, but to repair my own
tools or appliances, I’ll give anything
a go. If I ruin the pencil, I’m out a few
bucks, but it’s the serviceman’s creed
and the principles of repair that compels me to at least try. I’ll let you know
how it goes!
Some more light work
To be realistic; many repairs are simply not worth the cost. Recently, I had
an LED ceiling light stop working. It
had only been installed (by me) a few
years ago and hadn’t had a lot of use.
Maybe a few minutes a week of ‘on’
time, if that.
These lights are commonly called
“UFO” lights because they look like
a flying saucer. But they are different
than downlights which require cutting large circular holes in the ceiling.
These ones come with a fitting that
simply replaces the existing battenmounted socket we are all familiar
Australia’s electronics magazine
with, and the new UFO light slots into
place, hiding the socket.
That makes retrofitting ceiling lights
a breeze. We did our entire house with
these, and it was an effortless job to
convert all our incandescent lights to
LED versions, without a bunch of tools,
mess and headaches.
And they’ve been great; the light is
better, brighter and more economical
than our original lamps and fitting
them was super-easy. I’d installed a
dozen others in the house, and they’ve
all done a whole lot more work.
Why this one died is likely down to
the fact that 10% of these lights will
fail in the first few years, and that’s
an acceptable failure rate for modern manufacturers. Retailers simply
replace the unit and chuck the dead
one in a skip.
Now, if you are afflicted with the
Serviceman’s Curse, you know you
can’t just throw something out without at least pulling it apart and looking at it. So I had to take it down and
open it up. At the same time, I ordered
another one, because even though it is
seldom used, we need a light in that
spot and at only $11, replacing it is
the obvious solution.
It also means that I could work on
it at my leisure without hearing “get
that bloody light working!”
The housing popped open without
much hassle. Inside is a 200mm diameter PCB with a bunch of surfacemounted LEDs soldered to it. Another small PCB is mounted in a central
cutout, containing the LED driver. A
sniff with my serviceman’s nose told
me something had electrically given
up the ghost.
The usual suspects
My first step was to remove and
check the two electrolytic caps that
dominate the driver board. I fired up
my soldering station and went to try to
desolder those two caps, but the pencil was stone cold. I think you already
know how that went!
After resolving that, I removed the
caps and checked them with my trusty
Peak Electronics ESR meter. One measured 15W, which is on the high side.
The other one was also high, but not as
out-of-spec as the first one. I replaced
both and reassembled the board into
the light.
I powered it up with my non-Variacbranded Variac, and the LEDs sprang
into life. Success! It is now reinstalled
siliconchip.com.au
and happily illuminating our spare
room. So it was well worth having a
go, and when the replacement I ordered finally arrives, I’ll have a spare.
I must be cursed
It’s never fun when the tools we
rely on to do our job don’t work. Last
week I fired up my computer to write
this article, and my machine wouldn’t
boot. The old saying is that a plumber’s
pipes are always clogged, and while
I’m not sure what that means, I’m pretty sure it applies to me!
My main computer is a monster
that I built 11 years ago, so I’ve been
reluctant to upgrade it. That’s because
it was still going very well, played all
the high-performance games I ever
wanted to play, and it has always been
there for me.
For it to fail to boot up one morning was quite devastating. While I’ve
always tried to make these servicing
stories non-computer-centric (as it is
a dull trade), some readers might find
it interesting.
If a machine doesn’t boot, I usually
start by removing everything but the
absolute basics to get the motherboard
up and running. In this case, that still
resulted in no boot. I then started removing and replacing RAM, and suddenly, I had a POST (power-on selftest) screen.
I replaced the single stick I’d left installed one-by-one with the three others, and with the third, the machine
didn’t boot. Leaving that out, but with
the other three sticks installed, the machine booted happily. After 11 years,
one stick of RAM had failed, and that
broke everything. You just cannot take
things for granted in servicing.
printer had broken. The bureaucracy
she works for had said this 12V device was “too dangerous to use” in this
state! That sounds to me that this is a
statement from someone with more
ego than knowledge.
In any case, the solution was simple. It took me an hour or two to design a new cover in OpenSCAD. I
was then able to 3D print the cover,
and the deadly 12V inside was safely
locked away.
The next coin counter fault was
a problem common to many cheap
devices: the front panel membrane
switch developed a fault, so the PRINT
button no longer worked. Pulling it
apart was easy enough, with just three
countersunk self-tapping screws holding the upper case in place.
I did have to cut one wire tie; this
prevented the rotating coin counter
mechanism inside catching on the
multi-core wire connecting the front
panel.
If I had designed it, I would have
used a reusable clip/U-channel to position the wire safely. But this worked,
even if it did make disassembly (and
reassembly) a bit more of a hassle.
Next, I unscrewed the front panel
PCB, unplugged the front panel membrane switch connector and very carefully removed the complete front panel
membrane switch assembly.
Then, using a thin blade (the knife
from a Swiss Army Card works really
well), I separated the two halves of
the membrane near the PRINT button.
Unsurprisingly, one of the conductive tracks was open circuit. To determine if this was the only fault, I ran
some leads to the correct pins on the
PCB and found that the coin counter beeped when I shorted these two
wires together, simulating a press of
the PRINT button.
Well, I had found the fault, but now
I had to figure out how to fix it. The
likelihood of getting a replacement
front panel was low-to-zero. This was
a major problem for the canteen, as the
coin counter is used every (work) day
and having to count coins manually
meant a lot of extra work.
Then I had a thought: as only one
button was faulty, why couldn’t I just
add another switch? Initially, I was
just going to drill an extra hole somewhere and use a standard 6mm pushbutton switch; that would work but
look a bit ugly.
But then I remembered I had some
tiny switches that measured 3mm x
6mm and were only 1mm high. I purchased these as spares for repairing
car remote controls.
After a bit of measuring, it looked
like I could shoehorn one of these
switches to fit into a hole cut in the
plastic case underneath the existing
PRINT button, so that’s what I did.
For speed and simplicity, I drilled
two 3mm holes next to each other and
Coin Counter repair
G. C., of Salamander Bay, NSW has
found (like many others) that it can be
easier to replace a cheap failed part
with a higher quality alternative than
it is to fix the original part. In this case,
it was one of those horrible membrane
buttons. His solution means that it’s
unlikely to fail again…
My daughter runs a canteen for a
large organisation and even with email
ordering, it’s still necessary to count
all the cash each day. They use an unbranded coin counter that’s simply labelled “Coin Counter”.
I have fixed it previously; it was a
totally unnecessary repair, in my opinion. The small cover for the docket
siliconchip.com.au
The coin counter and small docket printer.
Australia’s electronics magazine
March 2021 63
filed until the switch fitted inside, then
used double-sided tape to re-glue the
membrane switch to the case. I pressed
the tiny switch into its new home and
tweaked its vertical position. When
the switch activated reliably when
the PRINT button area was pressed, I
added a couple of drops of super glue
to make it permanent.
I then soldered thin (wire-wrap)
wires to it, then soldered the other
ends to the PCB tracks. Happily, the
coin counter is back in service and
working perfectly and, even better, it’s
externally unmodified – the only difference is that now you can feel a click
when the PRINT button is pressed. I
would go so far as to say that after this
repair, it’s better than new!
Alternative security systems
R. M. of Scotsdale, WA, found out
that there are really cheap security
systems, and really expensive security systems, and neither is all that
appealing. Luckily, he found a middle ground...
Our community shed needed better
security as several of the keys had disappeared over the years. As the only
member with any electronic knowhow, I was volunteered to search out
a suitable replacement.
I went to the biggest security shop
in the local town and made enquiries.
They suggested an RFID system priced
at around $3500. As the shed is a small
non-profit organisation, I knew that we
couldn’t afford that. After some discussion, the committee authorised a
budget of $200 and let me loose.
64
Silicon Chip
Australia’s electronics magazine
I tried sourcing a cheap (~$50) RFID
unit from overseas via eBay, but shortly after I hooked it up and got it working, it failed. So I had to send it back
and get a refund.
During wanderings through Google, I had come across a more elaborate (and more expensive) four-door
controller from Jaycar. After the “fleabay” controller failed, Jaycar (bless
’em) put it on special and dropped
the price by a good $50. The committee agreed, and we were soon in possession of a nice sturdy box of tricks
that actually worked. That left the actual door strike.
Electro-mechanical striker latches require the door to be sturdy and
close-fitting. But our big metal shed
ain’t all that flash. The door (square
steel frame, steel sheet) swings on one
of the portal trusses. And when the
wind blows or the sun shines, there
is a perceptible movement of a few
millimetres between door and frame
– enough to make the standard latch
system unreliable.
However, at the back of my farm
there’s an old ute with two solid door
locks. I nabbed one which is now doing
excellent service on our shed. With a
12V actuator to pull the release lever,
it has enough slop to handle the geometry changes, and plenty of strength to
hold the door shut.
For our little installation, the supplied software is overkill. It’s designed
to control many doors of many departments and keep records of all the workers’ movements. It is mind-boggling in
complexity, and the instruction man-
siliconchip.com.au
ual is a masterpiece of confusion and
poor translation.
For example, on the circuit layout,
it shows two pins labelled “J9: Joint of
closing door by force”. I contacted Jaycar to ask what this meant, and eventually, the answer filtered back: it is a
disable input. Close the circuit (joint
of), and all doors would stay locked
(closing door by force). It makes me
wonder if they created the manual using machine translation!
I spent many hours decoding the
manual and experimenting with the
software. The process of registering
each user is vital, and there are two
ways one can do it. One is a bulk entry
method, and the other, more detailed,
allows individual entry. I chose this
way as we wanted to enter our members’ details one at a time, but I could
not get it to work.
I thought it must be my fault, so I
summoned the local PC expert. He
went straight to the “bulk entry” system, and it worked! Don’t bother with
that other way, he said, it’s no good.
So, finally, we have a working secure entry setup. The total cost was
around $370 with the backup battery
and trickle charger.
Now if a member leaves, or doesn’t
cough up the yearly subscription, we
can simply click a button and forbid
entry. He’d have to resort to removing a sheet of corrugated iron with a
screwdriver to get in!
LED rose garden light repair
B. P., of Dundathu, Qld has some unusually ornate solar garden lights, so
siliconchip.com.au
when they started to fail, it was worthwhile taking the time to fix them...
Some time ago, my wife was given a white LED rose garden light. We
noticed on the packet that there were
also yellow and pink LED roses, so after finding out that a nearby discount
shop sold these, we got a yellow one
and a pink one too.
Later, my wife received another two
LED roses, pink and yellow. However,
this new yellow rose only had a single
flower, whereas the others had two or
three flowers each.
We noticed that in the mornings, it
was only the single yellow rose that
was still lit; the other four roses were
no longer lit due to having more LEDs
(and presumably exhausting the battery charge faster).
After a while, we noticed that both
the white rose and the original yellow rose no longer lit at night. I had
a look at the yellow rose to see what
the problem was.
After removing the four screws
from the bottom of the small box containing the solar panel and battery, I
could see that water had leaked into
the box, causing the positive battery
connection to become rusty. The wire
had also broken off it and the battery
terminal was rusty as well.
I re-sealed the wires coming from
the solar panel properly with hot melt
glue, then cleaned up the battery terminal. It was so badly rusted that I
decided to clean it and coat it with
solder while I was soldering the wire
back on. I also tested the battery and
found that it was still OK.
Australia’s electronics magazine
With the battery refitted, the rose
still didn’t work. I measured the voltage on the battery terminals with the
solar panel lit and got a reading of
2.18V, so the solar panel was charging the battery, but some other fault
was preventing the LED from turning
on at night.
I removed the circuit board and
checked the switch, which was still
functioning correctly. The circuit
board looked clean, with no corrosion.
I then realised that I had a spare
circuit board from one of our garden
lights that had been run over and
smashed by a courier, so I decided
to use that to get the LED rose working again. This board did not have a
switch, but I didn’t think that really
mattered.
I disconnected the original circuit
board and wired up the replacement
circuit board, which was quite easy,
as all the connection points on both
PCBs were marked S+, S-, B+ and B-.
The wires from the LEDs were too
short, so I just used some scrap wire
to extend them.
When I tested the rose, it still didn’t
work, but I noticed that the YX8018
IC was bent over, so I straightened it
and checked the bottom of the circuit
board. I found that the solder joints
were cracked, so I re-soldered them,
but the rest of the PCB was OK.
Now the rose worked, so I sealed up
the hole where the switch used to be
mounted with hot melt glue.
With the yellow rose now reassembled and working, I took a look at the
white one. I found that the same water
ingress problem had affected this light.
After re-sealing the wires from the solar panel, I found that I could use the
battery connector from the smashed
garden light to replace the rusted one
as it was the same size. Once cleaned
and reassembled, the white rose now
also worked again.
The next morning, I was outside
before dawn, and I was amazed to see
that the yellow rose that I had just repaired was still lit brightly. I put this
down to the more complex circuit in
the garden light PCB that I had transplanted, which is apparently more efficient than the simple circuit in the
original LED rose.
As can be seen in the photos, the
‘basic’ rose PCB consists of just one
YX8018 IC and an inductor, whereas
the better garden light PCB has both
of these plus a diode and capacitor.
March 2021 65
At left is one of the ‘basic’ LED rose PCBs which had started to rust, while to its right is a superior garden light PCB.
This makes quite a difference to the
efficiency of the circuit.
I have also repaired several other
garden lights. Two had bad solder
joints on the LEDs, and I also had to
replace the RGB sequencing LEDs in
several lights when they malfunctioned (the blue elements failed). I
found some seven colour LEDs on
eBay, which sequence red-green-bluewhite-green-pink-warm white-repeat,
as the three-colour RGB LEDs were
harder to find and more expensive.
I’ve also replaced the 150mA Liion cells in all our garden lights with
new “1000mAh” (probably actually
400mAh) cells, so they now last all
night, as long as they have sufficient
sun exposure during the day.
Even though these lights are not
expensive, it was still worth repairing them, as it saved some money and
saved them from landfill.
Electric fence energiser repair
K. G. of One Tree Hill, SA, has repaired quite a few electric fence energisers over the years, but this one
posed some unique challenges...
I’ve written about the repair of electric fence energisers before (July 2015;
siliconchip.com.au/Article/8707); every now and again, I get one from the
local fodder store owner to see if I can
fix it. These devices apply a short, high
voltage pulse to a bare galvanised iron
wire running along the fence, supported on insulators.
They are used to control the movement of stock. Most operate from the
mains, but some models are powered
from 12V DC, generally with a solar
panel to keep the battery charged. The
Earth side of the energiser output is
connected to three or more Earth stakes
spaced out by a few metres, as recommended by the manufacturer.
The pulses have a typical duration
of about 30µs and the region of 5-8kV.
The pulse repetition rate is about 1.3
seconds. The main difference between
units is the energy in each pulse (measured in Joules).
This Gallagher model MBX1500 was
made in New Zealand and is the largest I have come across yet. Its pulse
energy is 3J, and it is suitable for fence
runs as long as 94km! A touch on the
fence wire would be excruciating, but
not particularly dangerous.
Testing the unit on the bench
brought some low-level intermittent
clicking instead of the regular pronounced clicks every 1.3 seconds. This
model is capable of being run from
the mains as well as 12V DC; there is
Servicing Stories Wanted
Do you have any good servicing stories that you would like to share in The Serviceman column in SILICON CHIP? If so, why not send those stories in to us? It doesn’t
matter what the story is about as long as it’s in some way related to the electronics
or electrical industries, to computers or even to car electronics.
We pay for all contributions published but please note that your material must
be original. Send your contribution by email to: editor<at>siliconchip.com.au
Please be sure to include your full name and address details.
66
Silicon Chip
Australia’s electronics magazine
a compartment in the rear to hold a
12V, 7Ah SLA battery in addition to
the mains cable and plug.
The two halves of the case come apart
after removing six deeply recessed selftapping screws. Fortunately, they are
normal Philips head types rather than
one of the many ‘security’ screws used
these days.
Inside was an offline switchmode
power supply (SMPS). This, or the
12V battery, fed into a DC-DC converter stepping the low voltage DC
up to several hundred volts to charge
the main capacitor. Then there was
the circuitry associated with the pulse
transformer. There was also a second
PCB containing four LCDs plus a 40pin PIC microcontroller.
In its working condition, the unit
displayed the output pulse voltage
and energy, plus two other parameters which didn’t seem to apply to this
unit. So it was quite a complex unit
with many SMD components down to
M2012 (0805) size.
When fault-finding electric fence
energisers, I first test the large pulse
capacitor(s). There are two in this
unit, one 30µF and the other 6µF, both
rated at 1200V. After ensuring they
were discharged, I measured their capacitance with my Peak Component
Analyser. The larger one was 13µF
and the other 3µF, both well down
on their original values.
This is quite common with these
components, but such a drop should
only reduce the energy of the pulses,
not stop the unit working altogether.
Despite this, I ordered some replacements from a local Adelaide firm and
carried on with my testing.
The other component to test early
siliconchip.com.au
is the main SCR which discharges the
capacitor into the primary of the pulse
transformer. This appeared to be OK
as the voltage across the larger pulse
capacitor was a couple of hundred
volts and fluctuating with the intermittent clicking.
I then measured the voltage out of
the offline SMPS which I found to be
only 4-10V with fluctuations, instead
of a steady 12-15V. I fed 12V DC from
my bench supply to the SMPS output
with the mains input disconnected.
The energiser started working normally, with believable values on the
LCD screens.
Looking at the SMPS more closely,
I noticed a large electrolytic capacitor
with a small bulge in the top. It was
the 100µF 40V filter capacitor on the
output of the mains bridge rectifier. I
removed the capacitor and tested it
on my Electronics Australia ESR Meter. The reading was about double the
typical value shown on the front panel
of the meter; not a show-stopper but it
needed to be replaced.
As I didn’t think this was the main
cause of the problem, I refitted the old
one to continue my search for the real
culprit while I ordered a new capacitor. It wasn’t available from the local
outlets as it was a low-profile device
30mm in diameter and only 20mm
high, so it took a few days to arrive
from Perth.
siliconchip.com.au
The primary active device in the
SMPS was a power Mosfet with an
integrated control circuit in a TO-220
package, riveted to a small heatsink.
It’s coded TOP227Y (TOPSwitch-II)
and is made by Power Integrations Inc.
This makes for a much-reduced component count as it contains the oscillator, PWM modulator, voltage reference
plus all the protection circuits and the
power switching Mosfet.
The circuit used in the energiser
turned out to be very similar to an
application circuit shown in the data
sheet (shown below). As the TOPSwitch device had so much of the
circuitry in it, I decided replacing it
would be a worthwhile punt. The only
stock I could find was from Digi-key. I
ordered two of the devices as the postage cost from the USA was more than
the device itself.
I can’t fault the delivery time; I
placed the order online on a Tuesday,
and it arrived at my local PO on the
following Monday.
Unfortunately, replacing the TOPSwitch device didn’t help my problem except to eliminate it as the
source of the fault. Referring to the
figure, I measured R3 and C5 on the
control input of the TOPSwitch. R3
was fine, but C5 was rather low in
capacitance, about 30µF rather than
47µF. I didn’t pay much attention to
that at the time.
Australia’s electronics magazine
One point of difference between the
MBX1500 circuit and that from the
data sheet is the use of a TL431 voltage
reference rather than the zener diode
shown. I replaced the TL431 and also
the optocoupler connected to it, but
neither changed the result. I also tested
the low-voltage DC rectifier (D2) and
filter capacitor (C2), the latter for both
capacitance and ESR. Both were OK.
I was by then wondering where to
turn next. I read the data sheet more
carefully and realised the part played
by the cap on the control input was
quite important. So I removed the
47µF capacitor and measured its ESR.
The typical value is 1-2W, but this one
was so high that it was above the maximum reading of the ESR meter, which
is 100W. In other words, it was virtually open-circuit.
I lost no time in replacing C5 with
a new one, which had a 1W ESR reading. The power supply came good immediately, and the energiser started
its regular clicking with 7.6kV pulse
voltage showing on the LCD.
The capacitor was a through-hole
type mounted between the PCB and
the heatsink. The elevated temperature of this position probably hastened
its demise. I put the three PCBs back
in the housing and screwed the cover
on, then left the unit to run overnight
as a soak test which it passed with no
SC
problem.
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