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SERVICEMAN'S LOG
Some jobs are much harder than they should be
Dave Thompson
It is often the way of the serviceman that some of the small jobs turn
out to be the most testing. My progressing age doesn’t help, but nor
do modern manufacturing techniques which cram so many tiny
components into a tight space.
One reason for my increasing difficulty effecting these repairs could be
that I’m getting on a bit now, and my
once-dexterous hands don’t feel quite
as capable as they once did. Nor do
my eyes seem as sharp as when I was
20 years old.
A good magnifier with a bright
light (or better still, a high-resolution
USB microscope with a decent-sized
screen) will help with the fading eyesight. But there isn’t a lot I can do to
keep my motor skills young.
It isn’t as if I can’t pick up a cup or
walk up the stairs without my bones
creaking and groaning, like many of
my martial-artist friends who practised the striking arts. They spent their
careers punching and kicking each
other and breaking bits of wood and
bricks, and many are now feeling the
effects of doing such a sport.
I spent 25 years practising Aikido;
one of the skills involved is learning to
fall over without getting hurt, so that’ll
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set me in good stead for the future!
But I am noticing a slow but inevitable decline. It’s the same when people suddenly find they can no longer
run 100 meters without a rest break,
or throw or kick a ball nearly as far as
they used to.
Obviously, this is all part of getting
older, but it still affects what we servicemen do. I’ve been lucky enough
to have steady hands and good tools
to help with some of the trickier jobs
I’ve done over the years.
While good tools help, it’s the skill
behind them that makes all the difference. Dad taught me to solder
about the time I started talking, and I
gained further valuable skills in this
area working at the airline. However,
much of this knowledge is deprecated
now, given the massive increase in
the usage of SMDs over through-hole
components.
Many of those SMDs are almost
invisible to my old eyes. As a
result, some projects and
device repairs are beyond
the scope of even skilled
servicemen, and repairs
increasingly require specialist (read: expensive) kit
that many of us don’t see
the value in acquiring.
I recently had a quite
challenging small-form job through the
workshop: a Logitech mouse. Before
you all jump up and down and query
the wisdom of repairing something
like this, it isn’t one of those 10-dollar corded jobs you buy at the checkouts at a supermarket. This 7-button
wireless mouse was quite costly, and
the owner thought it prudent to try to
have it repaired before shelling out
for a new one.
The problem was the left click button; for some reason, it started douAustralia’s electronics magazine
Items Covered This Month
• Of mice and men
• Volume control issues with an
•
•
electric guitar kit
The lab and the variac
Clenergy SPH15 1.5kW solar
inverter repair
*Dave Thompson runs PC Anytime
in Christchurch, NZ.
Website: www.pcanytime.co.nz
Email: dave<at>pcanytime.co.nz
ble-clicking, no matter how gently or
firmly one manipulated the flexible
plastic actuator. Thinking it could be
a software problem, even though the
owner had tested an old mouse and
found it free of this defect, I plugged
it into my machine.
Sure enough, a single click of the
left button resulted in a double-click
action. The right button was fine, and
if you listened and felt the tactile difference between the two button clicks,
you could sense something was up
with the left one. It felt and sounded
worn out.
This mouse hadn’t been used all
that much, so it was unusual that the
button had ‘worn out’ in such a short
time. Micro-switches typically have a
stipulated lifetime, measured in actuations, but I have mice that are decades
old and have literally travelled many
hundreds of kilometres with millions
of clicks.
I know this because, for many years,
I had a piece of software installed
that enhanced my mouse’s capabilities, which also measured how far my
mouse had travelled and how many
of the various button clicks I’d performed. It is astonishing how quickly
siliconchip.com.au
the kilometres and clicks add up!
Sadly, this software won’t run on Windows 10 and is now abandon-ware.
Returning to the
mouse in question
My semi-educated guess is that
the switch was just one of the small
percentage of the many millions
mass-produced every year that fail
early. This so-called acceptable failure rate happens with everything from
ovens to soldering irons and cars to
hard disks; it is just part of modern
manufacturing.
A famous case (to computer nerds
at least) is a hard drive that came out
in the 90s called the Quantum Bigfoot (https://w.wiki/3AmL). For about
a year, most PCs purchased came with
one of these drives. My first PC had a
2.1GB Bigfoot; a massive amount of
disk space at the time.
The Bigfoot got its name from the
large form factor it had compared to
other hard drives, which were physically smaller, known as 3.5-inch drives
(referring to the diameter of the platters
inside). The Bigfoot was much larger,
being the same width and taking up
the same bay space as one of those
ancient 5.25-inch floppy drives, or a
slightly more modern CD-ROM drive.
It had one flaw, though: it was rubbish! Most hard disk manufacturers
have an acceptable failure rate for their
products in the region of 2.5% or so,
meaning that out of every 40 manufactured, one will fail within the first
12 months of use. That sounds pretty
good, unless you are one of those who
experience that failure and the data
loss that ensues.
The Bigfoot had a failure rate
of close to 50%, which was previously unheard of. I found out about
it because the Bigfoot in my desktop
PC failed within a couple of months,
taking all my data with it.
I replaced it with another make
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and model of drive, at my expense,
because the company I’d bought it
from had gone under. That was a common occurrence in the early days of
pop-up stores selling computers in the
mid-90s boom.
This did teach me some very
valuable lessons, though. The first:
always assume a computer will fail.
It is almost inevitable. If you haven’t
backed up your data, how much trouble would you be in if it went ‘bang’
when you next fire it up and you lost
everything?
The second: computer repair guys
back then were often sharks and rip-off
merchants, playing on the ignorance
of the average owner. Being a beginner at the time, I got burned. A little
later, when I unexpectedly lost a gig
working at a local TV studio, I looked
into fixing computers for a living and
realised that it was something I could
probably do.
I understood the basic principles
and systems well enough, and with
the arrogance of youth, I figured that
I could do it. That was 27 years ago,
and for the record, I probably wouldn’t
have the nous to make that same decision today. But I’m glad that I did at
the time.
Back to the mouse again
If you’ve ever had the pleasure of
opening one up to see what’s inside,
you were probably surprised at how
little lives inside
them. The bulk of
your basic twoor three-button
corded mouse is
likely taken up
with the laser
Australia’s electronics magazine
and (optional) scroll-wheel assembly, with their associated switches
mounted to a small PCB on the bottom
of the chassis, which also has the USB
or PS/2 interface circuitry.
It’s pretty simple stuff, and certainly
not worth fixing given the ultra-low
cost of them these days. That’s not to
say I haven’t re-terminated cables or
cleaned balls and optical wheel sensors out in my time; I have, many
times. But these days, unless someone really loves their mouse and is
prepared to pay to have it fixed, it will
end up in the bin.
This particular customer likes his
mouse a lot, and since this type costs
a lot more than your garden variety
mouse, he was keen to have the errant
microswitch swapped out. He’d had a
look inside and baulked at the many
PCBs stuffed with SMDs and the complex internal construction, concluding that the fitting of a new switch
was beyond his pay grade. And so he
brought it all to me.
It turned out that I have an identical
mouse stored away in my, erm, mouse
storage place. This could be a stroke
of luck, as it is always nice to have
an identical model to refer back to,
especially if the breadcrumbs I leave
or photos I take along the way don’t
lead me back to an easy reassembly!
To be honest, I felt pretty much the
same way as my client when I took the
case off. It looked like a Mars Rover
without the wheels, stacked with electronics on layered PCBs. Fortunately,
the customer had already opened up
the case; he’d done the hard work of
finding the four hidden screws and
plastic clips that were holding it all
together.
This is a classic case of manufacturers making things difficult to repair. I
guess it could be worse; they could
have used deeply-buried anti-tamper
fasteners. Despite that, the unwary or
inexperienced might just conclude
that because there aren’t any visible screws holding it together, there
mustn’t be any, and begin by trying
to pry the case apart.
Of course, this will end in tears (or
at the very least, a mouse with a mangled case that won’t come apart).
The two front screws are hidden
behind a couple of those stuck-on
Teflon bumpers many computer mice
have these days. These are to help it
slide more smoothly over a desktop
or mouse pad.
May 2021 97
You might assume the two rear screws were hidden
under the back bumper, but no. Those back screws
were cunningly hidden inside the battery compartment, underneath the stickers that denote battery type
and polarity.
The ends of the stickers had to be carefully peeled
back to find and access the screw holes. The cowboy
in me might have been tempted to just punch straight
through the stickers with my screwdriver if this was my
own mouse, but for a client, one has to maintain certain
standards and decorum. So it was fortunate that he’d
already done the hard work, peeling back those stickers
and removing the screws.
I could see the offending microswitch as plain as day
at the bottom of the heap, but getting to it was going to
involve removing a lot of tiny screws, most of which were
different sizes and threads. The photos I took periodically
during disassembly would definitely help with putting
it all back together.
My memory of what part went where would also be a
valuable tool; thank goodness that hasn’t gone south on
me yet...
A challenging repair job
The various boards inside the mouse were connected
with a mix of those really stiff, hard-soldered flying leads
and thin, flexible ribbon cables terminating into ‘backflip’ edge connectors. These connectors are very similar
to what I find in laptops, phones and tablets to connect
PCBs together.
One problem I’ve found with this type of connector is
that they are often limited-use items. If I toggle them open
and closed too many times, many break, give out or won’t
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connect properly anymore. Replacing them is also very
difficult for mere mortals like me.
Long story short, I had to disassemble the whole mouse
just to gain access to the switch in question. Replacement
switches are available all over the usual auction sites
online, but as I had a good collection of NOS (new old
stock) microswitches, I was sure one of them would be
fit-for-purpose. The bigger problem for me was removing
the old one, given the small form-factor and tight spaces.
Sometimes it is easier to cut the component off with
the likes of a Dremel/rotary tool with a cut-off disc attachment, but there was no room for that rather ham-fisted
approach here. I could just get my soldering iron’s finest
tip to the contacts, but even though I could melt the solder, removing the switch was not easy.
It appeared to be stuck down, likely to ensure it stayed
in place for the reflow soldering process. While I had the
legs unsoldered and clear of the board, the switch would
just not let go. I tried soaking it with isopropyl alcohol
and various contact cleaners in the hope it would loosen
up; it didn’t.
I had to resort to using my dental picks to try to break
the bond, being very careful not to damage anything on
the PCB underneath, all to no avail. It was stuck fast.
I ended up breaking the switch off the board as gently as I could, but was horrified to see several of the tiny
copper tracks coming with it. That pretty much ended
the repair job right there.
While I could see where the three tracks had been torn
from, re-joining them, especially on a double-sided PCB,
was not going to be feasible. While I might have been able
to do it, the time involved would push the repair into
loss-making territory for me.
Fortunately, I had that identical mouse. After installing batteries and using the Unifying software to associate
my mouse with the customer’s dongle, I figured it would
be much easier to just sell him this one as a second-hand
device rather than persevere with the now-damaged one.
He was grateful for this option, so we all went home happy.
This was one of those jobs that, if it went well, it was
worthwhile doing, but as soon as something went awry,
it became a non-feasible repair. As a serviceman, I have
to try the former option, but I also need to know when to
pull the pin on a dead-end job. Having a suitable replacement mouse in this case was just good luck. If I didn’t
have one, the client would likely have had to shell out
for a new one. Such is life.
And I have to say that gluing components to the board
might be convenient for manufacturers, but it certainly
makes those parts hard to replace if they fail! Ideally they
should use a type of glue that loses its strength over time
or with heat, or that is just tacky enough to hold the components down for soldering but still allows the possibility of pulling it off later, should it need to be replaced.
That might even help the manufacturers if they have
to ‘rework’ any of their products before sending them
out to be sold.
An electric guitar kit with volume control issues
J. N. of Mt Maunganui in New Zealand recently built
an electric guitar from a kit. He had a bit of a problem
with some of the electronics, and the solution was a bit
unusual…
Australia’s electronics magazine
siliconchip.com.au
All went well with my guitar build until I began playing
the guitar via an amplifier. I started having intermittent
faults with the volume control to one of the two Humbucker single-coil pickups.
Naturally, I re-checked all my wiring to find nothing
amiss. Then the volume control started working again,
but not for long! So the problem must either be in the
pickup or its associated volume control. However, both
checked out fine. The pot measured 500kW and a normal
10kW+ for the pickup.
But as soon as I reinstalled everything, it happened
again. This repeated several times, with me checking and
re-checking until the penny dropped. The volume control
worked when removed, but as soon as I remounted it, it
would not function. So it had to be an installation problem.
Sure enough, on very close inspection, I noticed that
this particular pot (unlike the other three), was mounted
on a slightly curved part of the guitar soundboard. Consequently, when the fixing nut and washer were tightened, the pot became warped and would not function. I
replaced the steel washers with rubber washers and had
no more problems after that.
The lab, the questionable students and the variacs
D. D. of Coogee, NSW, wrote in to say that he loved the
story about the Old TV Repair in Serviceman’s Log, April
2020. It reminded him of when he was a young serviceman in the 1960s, which prompted him to write the following story...
Back in the 60s, I worked in the chemistry department
of a university in the UK, where I was in charge of the
electronics workshop. One winter morning, soon after I
arrived for work, I had a call from the glassblower. He
was a lovely chap and a real glass craftsman but had no
real understanding of “electrics”, and I realised he was
a bit scared of it.
I grabbed my trusty Avometer and set off for his workshop. When I arrived, he showed me a machine and said:
“the green light is on, but I haven’t turned the power on
yet, what do you think could be going on?”
The machine was an induction heater in a large metal
case mounted on the wall, about 60cm above the bench,
so he could feed glass tubes into the induction coil to heat
them up. It had various controls and an on/off switch on
the front panel as well as a large green indicator light. This
was glowing brightly and was freaking him out.
He was very worried about this and asked if I thought
we should call the university electrician in case some
weird power fault had occurred.
I was initially puzzled because I didn’t think it was likely
that the machine could be on without being switched on.
I pointed out that the switch was still in the off position,
but he was not convinced. I then said, “Well, I can’t see the
light glowing from here.” He pulled me back over to the
door and said: “look, you can see it from here.”
It was only then I realised that where the machine was
mounted on the wall, the sunlight from a window behind
it could enter through the perforated metal back of the
cabinet and make the light appear to be on!
Needless to say, he was a bit embarrassed, but we had
a good laugh about it and became firm friends afterwards.
In fact, he became a bit of a mentor to me and helped me
in lots of ways.
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Australia’s electronics magazine
May 2021 99
Another problem I had to solve
concerned variacs. They were used
in constant-temperature water baths
in the teaching and research laboratories. These were magnificent brass
tanks about 1m square and 0.5m deep.
They had a pyrotenax heating element
in the bottom, a slowly-rotating paddle wheel to circulate the water and a
mercury-in-glass thermostat.
They were made in-house; Ron, in
the main workshop, made the tank
and the paddle wheel. “Big wheels
turning slow, mate” he said to me one
day with a knowing tap of his nose. (I
had no idea what he meant but pretended I did!)
My mate the glassblower made the
thermostat, which was basically a
mercury thermometer with one fixed
platinum wire contact and another
mounted on an adjustment screw to
allow the temperature to be set to the
desired level. Ron wired these contacts through a relay to switch power
on and off to the heater.
The variac was needed because the
heater had a resistance of about 10W
and needed about 4A to heat the water
to the required temperature.
The system worked really well and
could control the water temperature to
a small fraction of a degree at a much
lower cost than commercially-available units.
The problem, however, was the
users; mainly research students, who
while they were very good at chemistry, could not do a simple Ohm’s Law
calculation and so tended to overload
the variacs.
When they put a flask of chemicals
into a water bath, it took a long time
to warm up the contents before they
could start their experiments. With the
Professor breathing down their necks
for results, and the fact that they often
had late starts due to too much social
life, there was a great temptation to
wind the variac up a bit to speed up
the heating process.
They had a current rating of 4A, and
despite being warned not to exceed
40V, the users did not seem to realise that exceeding this could cause a
problem.
Of course, the carbon brushes overheated and eventually failed. Each
time a brush failed, damage was
caused to the copper winding of the
variac, and before long, the inevitable
happened – a winding burned out.
This proved to be the case one day
when I was called to “Derek’s” lab. He
had been copping a bit of flak lately
from his Professor about various blunders and delays, so he was in a right
panic when I told him his variac was
“cactus”. To try to help him out, I
offered to go to the main store and get
a new one for him.
I didn’t stock variacs; they were far
too expensive, but there were a couple in the storeroom. It didn’t occur to
me that maybe I shouldn’t just walk
in; after all, I was a staff member, not
a student; so in I went.
I was chatting to the stores girls
whose main occupation seemed to
be filling beautiful old glass-topped
reagent bottles engraved with the Latin
names of chemicals. They were filling them from large tubs of chemicals
and putting them on the shelves to be
issued later (a cost-cutting measure).
The manager strode up to me and
drew himself to his full height. “Can
I help you?” he asked. He was what I
suppose you would call a dapper little
man, impeccably dressed (unlike the
rest of us) in a striped white shirt, tie,
neatly ironed trousers and his white
lab coat starched to within an inch of
its life. He carried a plastic wallet in
his breast pocket with black, blue and
red biros and a propelling pencil.
“Yes, please” I said, “I’d like a
variac; I see you’ve got two left.”
The girls later told me they could see
the steam coming out of his ears! When
he had finally regained his composure,
he rushed me into his office and shut
the door. “Dave I know you’re new and
that, but that’s not how things are done
Servicing Stories Wanted
Do you have any good servicing stories that you would like to share in The Serviceman column in SILICON CHIP? If so, why not send those stories in to us? It doesn’t
matter what the story is about as long as it’s in some way related to the electronics
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We pay for all contributions published but please note that your material must
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100
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Australia’s electronics magazine
you know!” He proceeded to explain
his “stores system” to me.
He gave me a stores requisition book
and a stock list and explained that four
carbon copies were needed.
“You fill it in, with your name,
department, extension number and the
details of what you want, referenced
from my stock list. Then you sign it,
hand it in at the stable door and we
will bring your items out to you.
Don’t forget to put the carbon paper
in; the white copy is for my records,
red for the office to charge to your
account, yellow goes into storage, and
you keep the green copy in your book.
Understand?”
Feeling somewhat chastised by all
this, and as it was nearly hometime, I
withdrew back to my workshop and
went home, forgetting all about poor
Derek waiting upstairs!
The next day I returned to the stores
with a neatly filled out requisition and
rang the bell at the half-stable door.
One of the girls came up, and I handed
her the requisition. She went off with
it, and after a little while, the manager
came over to the door. “Sorry Dave, I
can’t let you have one” he said, much
to my surprise.
“Why not?” I asked, “Have I filled
out the requisition wrong somehow?”
“Oh no, that’s OK” he said, “It’s just
that I haven’t got enough stock.” This
was a bit puzzling because I knew he
had two yesterday and didn’t think he
could have issued both of them already.
Eventually, I blurted out, “But you
had two yesterday.”
“Yes,” he replied in an irritated tone.
“So why can’t I have one?” I said. Imagine my amazement when he explained
that one was needed in case “someone” wants one and the other was a
pattern for re-ordering!
“But I’m someone” I tried. He
wouldn’t budge, however, and I felt
like I had been sent off or sin-binned!
Later, I found out that the only way I
could get one was to get Derek’s Professor to ring down for one. Jim explained
the Professor was the “someone” – his
secretary would fill out the requisition, which would be sent to the stores
in the internal mail and a girl would
deliver the item to Derek’s lab.
This was duly done, and I installed
the new variac, telling Derek to more
careful in future not to turn the “herbs”
up too much.
That should have probably been the
end of the story, but I couldn’t resist
siliconchip.com.au
getting my own back on the manager. I
had just bought a huge Circuits Manual
from the USA, and as I was browsing
through it, I saw something exciting.
It was billed as a solid-state variac
replacement; just what I needed, I
thought! The circuit showed a power
controller consisting of a UJT firing
circuit and an SCR. It was said to be
capable of controlling resistive loads
of any current, limited only by the
SCR rating.
I soon had the parts and shortly after,
had a breadboard version working.
Of course, it was much smaller and
cheaper than a variac, and I soon had
a few prototypes out in some of the
labs. The guys seemed to like them,
but they had a few teething problems.
They had terrible hysteresis, which
meant that as you reduced the power
level, they would suddenly turn off
and to get them to fire again, you had
to turn up the power way past the point
where you were before. The guys naturally didn’t like this, especially as
they weren’t sure what was happening.
Later versions used a quadrac,
which was a new device consisting
of a Triac with an integrated Diac.
The manufacturers even helpfully
included a low-hysteresis firing circuit and RFI filter on the data sheet. It
wasn’t long before we had the device
perfected, and the researchers were all
ordering them to replace their variacs.
All went well for about six months
until one day, the stores manager
bailed me up after morning tea and
said: “If you still want that variac, I
have just received an order of a dozen
so you can have one!”
siliconchip.com.au
The look on his face was priceless
when I said: “Oh, we don’t use those
any more. They’re old hat now. I’ve
replaced them all with solid-state
power controllers!” At least he would
not have stock problems any more!
Clenergy 1.5kW
solar inverter repair
R. S., of Fig Tree Pocket, Qld, got
sick of having to get his solar inverter
replaced under warranty. So he
decided to try to fix it himself, with
some success...
The Clenergy SPH15 1.5kW solar
inverter was supplied by Origin
Energy as part of their low-cost solar
power system.
These inverters started giving an
“Output Relay Failure” message after
a few years. Mine was replaced twice
due to this fault. I can see that the
inverter boards now have external
diodes placed across the relay coils, so
it appears that the relay drivers were
being destroyed by back-EMF from the
coils. This must have been costly, with
so many units replaced.
A new problem is now occurring,
with messages such as “GFCI Fault”,
indicating leakage current to ground
from the solar panels. However, megger testing of the panels shows no
leakage. It seems that the currents on
the DC inputs (from the solar panel)
are being compared and the error is
displayed if an imbalance is detected.
There are two current transformers
on the main board, one on the positive
input and one on the negative input.
There is a buck-boost converter immediately after the input, with two IGBTs
Australia’s electronics magazine
in parallel and a large rectifier. The
IGBTs are driven by an ICC2818 controller, optically coupled via a TLP350
Mosfet/IGBT driver for isolation (see
photo directly below).
As current transformers need current pulses to produce an output, I
thought that the buck-boost converter
might not be operating. I have had
problems with optically coupled isolators in the past gradually failing due
to either low output from the internal
LED and/or low sensitivity of the optical receiver. So I replaced the TLP350,
and the inverter started working again.
The GFCI fault disappeared.
I am wondering how many of these
inverters have been scrapped due to
these problems.
Be careful when working on these
inverters, as the large high voltage
capacitors take a long time to discharge. The low voltages are also supplied from these capacitors, so be sure
that these are not present when working on the control section.
I notice that to reset the display
board, it is sometimes necessary to
disconnect and then reconnect the ribbon cable. This is because the supply
voltages persist, as described above.
Since I repaired my inverter, a new
error message is now showing: “Ground
I Fault”. This has stopped the inverter
working again. I will investigate this,
but it will take some time as there are
no circuit diagrams available. The only
hope I have is to compare the operation
of a working unit with the faulty one. It
seems to be a fault on the main board,
as swapping display boards does not
make the error go away.
SC
May 2021 101
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