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SERVICEMAN'S LOG
That ‘80s gear and the art of printer repair
Dave Thompson
Regular readers of this column will know that I’m not one for throwing
stuff away. They will also know that I’m a fan of stuff made a couple of
decades ago. So when a client brought in his circa 30-year-old dot matrix
printer, despite not normally repairing these things, I thought let’s give it
a shot. Especially since it was described as ‘only’ having a broken wire.
D
on’t get me wrong; I’m not one of
those hoarders who has to stand
up to sleep because there is no more
room in the house. However, my workshop is, shall we say, quite ‘busy’ with
bits and bobs I’ve collected over the
years.
For example, a long-time client
recently moved ‘up north’ [to Yorkshire? – Editor] and brought me a couple of presents before he left: a classic
Avo meter and a Megger, both with
original leather storage cases, user
manuals and even leads.
I couldn’t say no to those beauties,
but they take up shelf space that I don’t
really have. Still, I’m not the only one
in this position. I fondly recall visits
to my uncle’s electronics workshop in
Melbourne when I could spend hours
poking around, looking at all the gadgets and devices I’d not seen before.
It was my idea of heaven.
Recently, another long-time client
brought in some familiar devices for
me to repair – again. He has several
Swedish-made electronic gadgets,
built in the early 80s, using that nowclunky analog technology. I have had
these in the workshop several times
over the years for things like broken
RS-232 socket wires or buttons that no
longer work properly.
Fortunately, the owner has a couple
of extra similar devices that stopped
working years before I was involved
with them, and he now uses these for
spares, especially as the buttons wear
out frequently.
The gadgets look surprisingly similar to my dad’s early HP calculator
back in the 70s (Google tells me it was
the HP-65 model). It boasted a swipe
card with a magnetic strip that could
‘program’ the calculator’s functions,
something I was quite taken with at the
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time. The red, bubble-lens LED display
also looks similar and was very much
of its time as well.
When opened up, the Swedish gadgets contained three PCBs packed with
EPROMS and other common chips of
the time, plus room for a rechargeable
3V battery.
I’m still not sure what my client does
with these devices, but as he is retiring soon, he just wants to keep things
going until that happens. I know he
goes to various establishments, plugs
these gadgets into machines (pokies
maybe?) and downloads information
onto them.
He then takes the gadgets home
and connects them via old serial-type
cables to a green-screen computer I
have also been keeping limping along.
He can then print out the data he needs
on a couple of old printers.
What they do isn’t really important
anyway; I just need to be able to keep
them going. As with many handheld
devices, he only uses a few of the keypad buttons to perform common tasks,
so those wear out pretty quickly.
If the plastic button’s top is popped
off, a retained tension spring comes
with it, and the contacts beneath are
revealed. By today’s standards, I
think they are a bit basic, but they
do the job.
Underneath the cap is a
U-shaped copper spring contact
about 15mm square overall but
made from very thin metal,
which looks quite flimsy.
The top-left corner of this
spring contact is connected
through the plastic base of
the switch to the button
PCB underneath. When
the button is pushed,
the bottom right corner
Australia’s electronics magazine
of this piece deflects and touches the
other contact, which is also moulded
into the plastic base of the button.
The obvious problem is that this
main metal piece just wears out with
use and eventually work hardens and
breaks off, meaning the button stops
working.
Sometimes, I can just use a finetipped soldering iron to re-join the
primary spring contact to the broken
piece in the base, but this is a temporary fix only; the usual procedure is to
replace the button itself.
As I mentioned, he has several spare
devices, and I have already used many
of the buttons from these units. While
the buttons are coloured and numbered, I just use the original plastic top
from the broken one and put it onto
the ‘new’ replacement base to restore
functionality.
Unlike a lot of stuff from that era,
I got the distinct impression these
weren’t designed to be worked on by
anyone but the manufacturer. There is
siliconchip.com.au
Items Covered This Month
• That ‘80s gear
• Replacing the plugpacks in a
•
•
dual-handset phone system
A blown and charred mobile
phone charger
Repairing a 15-year-old Epson
scanner
*Dave Thompson runs PC Anytime
in Christchurch, NZ.
Website: www.pcanytime.co.nz
Email: dave<at>pcanytime.co.nz
no information about them anywhere;
no circuits, schematics or other data
except for the user manuals the client
got with them when he bought them
in the early ‘80s.
To get an entire button out, for
example, the whole device must be
disassembled. Many through-wires
must be disconnected/unsoldered
with much gnashing of teeth and
wringing of hands until the bottom
of the button PCB is revealed. There
is no other option, though, so we just
soldier on.
One good repair deserves
another
Recently, the same client called and
asked me about having a look at his
printer, which apparently had a “broken wire” and had stopped working.
This sounded reasonably straightforward; I’m not bad at repairing broken
wires, but printers in general are not
my thing. I usually refer clients with
printer issues to a specialist printer
place.
However, I said I’d have a look, and
when he arrived with it, the job took
on a different angle. This printer is 35
years old, one of two he uses every day
to do whatever he does with them (my
assumption is printing data!).
Anyone who remembers these printers will know the type I’m talking
about. They work very much like a
typewriter, but instead of individual
keys striking paper through an ink ribbon to make their mark, these printers
have a matrix of pins within a print
head which moves back and forth
along the line and forms the characters instead.
The major disadvantage is the sound
they make; the name impact printer
probably says it all. I recall going to
offices and they’d have a special room
set up just for these printers because
they were so loud!
One such office didn’t have a
‘printer room’, and the poor workers
there had to suffer constant high-level
noise; I could barely sit in the office
chair for five minutes, let alone spend
the day there with that racket going on!
Still, these types of printers had their
place and are still used by people who
need duplicate (or even triplicate) copies, all done simultaneously.
Of course, modern inkjets or laser
printers can easily do multiple copies.
However, some businesses still prefer that old tractor-feed printing that
does it all at once (for POS systems
where the customer gets one copy,
for example).
Anyway, the client brought the
printer in and as a testament to the
build quality of these older machines,
it was the first time he’d ever had to
take it in for a service. It showed; covered in dust and dirt, it really did need
cleaning up.
The biggest problem was this “broken wire” the client talked about. It
wasn’t a broken electrical wire, but the
main drive cable that connected the
printer’s moving head assembly to the
stepper motor, which of course, means
nothing worked because the head no
longer moved back and forth.
This connecting cable is much like
a bicycle’s brake cable; multi-stranded
and designed to carry quite a substantial load. It is fixed to the movable
print head of the machine, which is
mounted on a couple of heavy-duty
chromed rods, and the cable wraps
around several pulleys and the stepper motor’s main drive shaft, allowing
the print head to traverse the printer
at some speed.
You certainly wouldn’t want to get
your fingers stuck in there when it’s
going, which is why there is a removable plastic cover over the whole
assembly.
The cable was lying in the bottom of
the printer, and it had obviously come
unstuck somewhere. I’ve repaired a
few cables like this before in different
devices, so I said I’d take a look to see
what I could do.
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November 2021 85
Most repair people would just tell him it has had its
day and to buy a new one, but there were a few problems
with doing that. One, while still available, due to COVID19, there is not one to be purchased in New Zealand at
the moment. Two, even if one was available, the cost is
prohibitive now for a similar machine. Repair seemed
like the only feasible option.
Threading the cable back onto the various spools and
pulleys wasn’t too onerous, except for the fact it has
formed itself into very strong coils as it has been sitting
in the same position for the last 35 years. At least this
gave me a clue as to how it wound back on and where it
could actually go, because it isn’t apparent just by looking at it from under the top cover.
True to form, I couldn’t find a service manual for this
printer anywhere on the web. I had only a vague idea of
where everything should go back into place, so there was
a bit of toing and froing as I tried different methods to get
the cable back on track.
Eventually, I got it into place – or where I thought it
should be – and manually moved the print head back
and forth. The cable was firmly connected to that, and I
assumed that I didn’t want to move it because that might
throw everything else out of whack. I theorised that if it
had come off with the head in that fixed-cable position,
it should go back on there as well. That was the theory
anyway.
With the cable in place, I manually moved the head
along the shafts, and almost instantly, the cable pinged
off the far-right hand pulley. I was back to square one.
With a bit of fettling, I got the cable back into place and
tried it again. Once again, everything just popped off; it
was becoming evident that something else was wrong.
The problem seemed to be with that far pulley, a plastic
moulded disc running on what appeared to be a metal hub
in the centre. It bore a lot of the cable load and, as soon as
anything moved, the cable simply peeled off it. I took out
the circlip holding it on and removed it for a better look.
Straight away, I could see the problem; over the years,
the cable had ground away at the channel it sits in, and it
had simply worn through the plastic. Looking at it from
the side, the bottom of the pulley channel was fine, but
the top edge had disappeared completely, so there was
nothing for the cable to run in anymore.
It needed replacing, so I got on the phone and called
a few printer places I know of to ask if perhaps they had
an old dead unit sitting under the bench I could burgle
parts from. No joy; as I suspected, most examples of this
printer were skip fodder years ago. And new parts are
not an option either, so it was back to looking at what I
could do with this one.
Jury-rigging it
The pulley itself might be able to be repaired, and if I
had a 3D printer, I might have been able to make a new
one. But I didn’t, so I couldn’t. Still, I had an idea. The
bottom edge was not worn through, so obviously, all
the stress was on the top section, which had worn out. I
thought I might be able to simply turn the pulley upsidedown and use it that way.
Unfortunately, the cable wouldn’t stay on this way
either, just falling off the bottom as soon as I moved the
print head, so that wasn’t going to fly. But then I thought
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about using something to build up the missing bottom
part of the pulley.
I looked through my parts bins and found a large washer,
which I know variously as a ‘penny’ washer or a ‘fender’
washer. Basically, it’s an oversized metal washer with a
relatively small hole in the centre. I figured that if I bored
out the hole to the size of the shaft the pulley ran on, I
could glue this washer to the bottom of the pulley and
essentially replace the worn-out edge.
As it would be on the bottom now (because I would
flip the pulley over), it wouldn’t be subject to the upward
forces of the cable, and the now unworn plastic edge of
the pulley would do the job its other half did for the last
35 years.
Drilling the hole out on the washer was no problem,
and I used a 24-hour epoxy resin and a press to glue the
washer to the bottom of the pulley. I made sure to scuff
the plastic to give the glue something to adhere to and
centred everything up using an 8mm drill bit shank which
I could remove easily later.
It wasn’t brilliant, but I reckoned it should work. I reassembled everything once the glue had time to set, and
other than a bit of cleaning of the glue around the cable
run of the pulley, it looked pretty good.
One problem was that now the pulley was around 50%
thicker in cross-section, and I could no longer use the
original circlip to hold this pulley to the shaft. I ended up
drilling and tapping a small hole down the centre of the
shaft, which turned out to be hardened steel, and mounted
a small bolt and washer to hold the pulley in place.
Threading the drive cable back into place was by now
relatively straightforward, as I’d done it so many times, and
the washer-bottomed pulley seemed to rotate and move
just as well as it had before, with no binding or noise.
The proof of any repair is whether it works or not, and
so I plugged the printer in and hit the power button. The
head shot back into its usual resting place, and all the
right lights showed on the front panel. I didn’t have a
parallel port with which to test it, so I asked the client if
he could bring what he needed to try it out.
He duly arrived with a handheld gadget and a bunch
of cables and interfaces, which he plugged in, and soon
we were rewarded with the dulcet tones of an impact
printer doing its thing.
The client has since reported that all is well and it is
going better than it has in years. A job well done!
Changing the plugpacks
in a dual-handset phone system
P. R., of Canterbury, New Zealand took pity on a Gigaset C300A dual-handset DECT phone system at a local
church fair. It came with UK plugpacks, so it would not
be usable for the average buyer, but it looked clean and
tidy, and still in its original box, so he bought it...
Once I got it home, I removed the two AAA cells from
each handset, and they all showed signs of leakage, but
the damage to the phones looked minimal. A new pair of
cells brought life to one handset, but not the other.
The next step was to sort out the plugpacks. I found
two transformer-style plugpacks in my junk boxes, large
enough to house the fairly small plugpack innards from
the UK versions, held together by screws, not ultrasonic
welding.
Australia’s electronics magazine
siliconchip.com.au
It did not take long to cut open the plugpacks and reassemble them into the Australia/NZ style housings. I then
cleaned up the battery housing of the working phone, set
up the smaller charger and plugged the phone in. When I
came back later, the battery was fully charged. It worked
as a regular cordless phone, including an answerphone
(I deleted four old messages).
So that just left the non-working phone. There were no
screws, so this would be one of those Humpty Dumpty
jobs, crack the egg and try to end up with an intact, unblemished egg at the end. After watching a fuzzy video on the
web, I could see that it was possible, and I knew which
end was best to start from (the battery end).
Lacking the usual tools for this, I finally managed to
crack the case by apply gentle pressure using my bench
vice on the battery end until I could fit a small steel ruler
in the gap. I could then work my way up each side of the
case with a small flat-bladed screwdriver until the whole
thing gave up and opened.
I could see some verdigris around the two battery terminals and other areas, but not so bad that it was not
worth trying to save. A quick clean with warm water and
a toothbrush, and it looked pretty good, but it was still
not working. There is one LED between the two terminals
that looked like the worst affected area.
I removed the negative terminal, which was surfacemounted on two rectangular pads. Again, everything
looked good, but an ohmmeter showed no continuity in
the track joining the two pads together, nor in the zig-zag
track through a low-ohm resistor to the ground plane of
the phone.
I could not see any breaks, but it turned out that both
tracks were open at the point where they attached to the
rectangular pads.
This brought me right back to my early days servicing
in the early 1970s. Back then, I discovered that some PCB
designers had no concept of pad-to-track transition or sensible track widths. This was particularly apparent in an
old pocket transistor radio that always suffered broken
tracks when the user changed the batteries and accidentally applied pressure to vertical resistors.
The designer of this phone would probably try to empty
a football stadium through a standard house door. In the
end, I had to repair seven tracks with fine wire, two on
the negative terminal, three on the positive terminal and
two on the LED. Only two tracks had an almost sensible
width, and one of those was open-circuit.
All these tracks could have been at least five times
wider in the space available, and fillets are always good
practice on pads that could be subject to stress (like battery terminals!). While this was a corrosion problem, not
a stress fault, it could have saved all the re-work.
Once reassembled, this phone joined the other and
charged its old battery just fine – looking only a little
battered along one edge from the case opening. Was it all
worth it? Probably not, but for only $4 plus my time made
this a reasonable upgrade from my old phone.
A blown mobile phone charger
B. P., of Dundathu, Qld got a rude surprise when one of
his children handed him a blackened lump to diagnose
and fix. It’s a good thing it didn’t burn the house down...
My son handed me a phone charger and told me that
siliconchip.com.au
Australia’s electronics magazine
November 2021 87
Even just
a glance at
the phone
charger shows
substantial
burn marks
which could
be likely
attributed to a
blown diode
and failed
electrolytic
capacitor.
he was charging his phone after he
went to bed last night, when the charger blew up with a loud bang, bright
flash and smell of burning.
I opened up the charger by undoing the two screws at the back. The
inside of the top cover was blackened
and I could see that the likely cause of
the near-disaster was the failed 2.2μF
400V electrolytic capacitor that had
a bulging top. Further investigation
showed that one of the diodes had a
piece blown out of its lead, and when
I checked resistor R1, it was open-circuit.
I have not previously seen one of
these chargers blow up like this; they
usually just fail silently and just don’t
work anymore. It was only worth a
few dollars, but I thought it would be
interesting to see if it could be returned
to service.
I started by looking through my collection of reclaimed capacitors for a
replacement 2.2μF 400V electrolytic
capacitor, but the only 400V capacitors of the correct physical size I had
were only 1μF.
Then I thought to check another
failed phone charger that I hadn’t been
able to repair because of its more complex circuitry, and luckily, it had a
good 2.2μF 400V electrolytic capacitor I could salvage.
I did have a 1W 1W resistor in my
collection, along with four 1N4004
diodes. I didn’t bother testing the
remaining three diodes that hadn’t
blown up, as I decided to just replace
all four to be safe.
With the replacement components
fitted, I set the top back on the charger in case it decided to blow up again
when plugged in. I plugged it into a
power board, and nothing happened
other than the indicator LED lighting
up; a good sign.
I plugged in a USB voltage tester and
it showed that I had just over 5V, so
the charger was now working again.
This was somewhat surprising, as I
had half expected it to blow up again
when it was plugged in.
I reassembled it, and it can now
be returned to service. I wonder how
many house fires are started by unattended chargers like this one failing
spectacularly.
Epson scanner repair
A. L. S., of Turramurra, NSW went
down a rabbit hole trying to fix his
trusty old scanner. It probably wasn’t
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worth the time he spent given how
cheap they are to buy these days, but
it’s a pity to throw it away just because
a couple of low-cost, easily replaced
components have gone bad...
My 15-year-old scanner started stopping halfway through a scan. Repeating the scan occasionally produced a
complete image, but over time it got
worse, eventually refusing to scan documents at all.
I checked YouTube to see if anyone
else had a similar problem. There was
one person who had a sticking Epson
scanner and described the repair
in excellent detail. He described it
as being “a reasonably easy repair”
(https://youtu.be/RsmRNWoYkQI).
His scanner was a different model
to mine; the workings looked similar, but the repair involved disassembling all the mechanical components
and cleaning the running rails which
guide the scanning assembly. He also
used replacement parts cannibalised
from another scanner.
I checked out available parts online
for this scanner in the hope that I
could find a dead one “for parts only”
or some spare belts and pulleys, but
all I could find was a used controller
board for $90 including postage, which
seemed way too steep.
I thought it would be a waste of time
and money anyway because I assumed
my problem was mechanical, as it
stopped scanning at the same location each time.
If it was a mechanical failure then
all I likely needed to do was free up
the movement, so I split the case to get
to the mechanical gear. It didn’t quite
go according to plan because only
two screws were holding it together,
and as I prised the case open, I heard
the horrible sound of plastic retainers snapping. There were several of
these around the perimeter, and they
all completely broke off.
The plastic retainers required some
sort of magic trick to separate, and I
am still unsure what that was! I have
repaired hundreds of similar devices
and never came across a case like this.
Fortunately, the absence of the plastic bits made no real difference, and
the two halves of the case snapped
back together again after I had finished cleaning the rail for the scanning assembly.
The assembly moved very smoothly
after I cleaned it. The belt and pulleys
were all OK, and I was convinced that
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Two faulty 10μF 6.3V SMD
electolytics were removed
from the controller board of
the scanner and replaced with
through-hole electrolytics
rated at 25V.
the scanner would now come back to
life. After I plugged it in again and set it
off for a scan – nothing had improved;
it still scanned only half a document.
I was really puzzled! If the mechanicals were operated smoothly, what
else could be going wrong?
I put it all down to a faulty motor
or motor controller, but the curiosity
was slowly killing me, so I eventually dragged it out, dusted it off and
fired the thing up again. This time it
scanned half a document immediately,
but when I tried again, it stubbornly
refused to obey any command.
My thoughts turned to the plugpack;
it might have a low output voltage or
be overheating or somehow limiting
the current delivered to the scanner.
I checked it out by loading it with a
68W 10W resistor, but it maintained its
rated voltage, so I had gone up another
blind alley.
It then struck me that I had not
even inspected this controller board
when cleaning it. That’s because it
was entirely covered by a ‘full metal
jacket’ that was screwed in place and
also hidden by another PCB carrying
the switches and the power indicator LED.
Instead of opening it all up again and
taking the time and effort to pull the
circuit board out, I took a shortcut and
zoomed in on the photo of the replacement control board on eBay.
As I zoomed in on the tiny fuzzy
photo, I had a light bulb moment – this
thing had two 10μF 6.3V SMD electrolytics, the same type which caused me
grief on a previous repair and that are
famous for going bad!
One of the symptoms was that the
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scanner started to work when it was
cold, but it would not work after being
switched on for any length of time. I
think that this might be because the
electrolytic capacitors had degraded
and become temperature-sensitive.
So I extracted the circuit board and
removed those two SMD electrolytic
capacitors. This is easy if you know
how to do it correctly. The best method
is to gently rock the SMD electro from
side to side with needle-nose pliers.
This fatigues the pigtails, but you have
to be patient and “gentle” is the operative word.
After removing them, I checked
them with a capacitance meter and
they measured a measly 0.73μF and
2.3μF!
I did not replace these with SMD
capacitors but instead used conventional electros because modern
through-hole types are small enough
and are easy to solder, as you can see
in the photo. These replacements also
had a higher rating of 25V and were
easily soldered to the SMD pads and
insulated with some plastic tubing,
mounted horizontally to allow space
for the metal jacket to clear.
I also replaced two other suspect
conventional electrolytics with new,
higher-rated ones and bingo! The scanner worked perfectly.
I suspect it was only scanning half
the page because it was getting to
a point where greater demand was
placed on the power supply, and
with such poor bypassing, the voltage dropped too much and reset the
controller electronics. This symptom
was a live red herring designed by an
ingenious gremlin.
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