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SERVICEMAN'S LOG
‘Playing’ with fire
Dave Thompson
I always hesitate to ‘help’ repairers or installers do work in my home.
While I presume that my talents would come in handy (even if I’m just
acting as a third hand), I know how frustrating it can be when someone
who is not an expert is hovering over you. Sometimes, a ‘helper’ is
actually a hindrance. In this case, I think the guy appreciated assistance
from someone with decent electronics knowledge.
A
little while ago, I was sitting in
my workshop doing somethingor-other when suddenly there was a
huge boom! The earth shook, dust fell
from the light fittings, and everything
on the bench was rearranged slightly.
This didn’t overly disturb me, as
earthquakes are a dime a dozen here
these days.
I’ll admit that my heart did race a
little, as it always does with quakes,
though I did think it a bit unusual
at the time. Most ‘quakes don’t have
the sharp shock and loud audio
soundtrack this one had, tending
instead to be rolling, rumbling affairs
lasting perhaps 30 seconds or more.
This one was very short and sharp,
and quite loud, but I thought nothing
more of it at the time.
I know, great story, right? However,
this will all become relevant later, I
promise!
Keeping the ‘cave’ comfortable
Increasingly, our news reports seem
to be chock full of extreme weather
events. If it isn’t droughts, it’s floods,
and if it isn’t wildfires, it is plunging
temperatures from seemingly endless
polar blasts. Sometimes both of these
will happen in the same place, just a
few months apart.
While being so far away from the
hottest places on the planet does help
us here in New Zealand a little, being
so close to very cold places does have
its drawbacks. Anyone who has visited Christchurch (or anywhere further
south of here) in the middle of winter will know what I’m talking about.
This year, we have record-breaking
‘cold snaps’, which sound vaguely
appealing, like something my grandma
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would have baked. But to those of us
living here, they are anything but.
When the mercury drops to -7°C of
a morning, for example, one really
appreciates having a well-insulated,
well-heated double-glazed home.
The rub is that most homes built
here before, say, the 1980s are mainly
uninsulated (apart from some having
fibreglass insulating batts retrofitted
into the roof over the living areas if
you were posh).
They typically have single-glazed
windows, making them increasingly
inappropriate for the temperature
extremes we are now seeing in the
summer and winter months.
My parents’ ex-home, which we
have just sold due to them not being
here any longer, is a classic example.
Mum and dad added insulation and
better windows to their 1959-built
house, where practical, while they
lived there.
But with no wall insulation, minimal roof insulation and originally just
two back-to-back fireplaces to heat the
whole house (eventually replaced with
stand-alone electric heaters, then heat
pumps), the home was very susceptible to heat and cold. It was sweltering
in the summer and impossible to warm
up in the winter.
These days, it is increasingly important that houses be properly built and
well-insulated. Not only is it a nicer
place to be, but it is also a lot less
expensive to heat or cool, especially
given that costs of energy – whether
electricity, gas or wood – are all going
through the roof (pun intended!).
Time for an upgrade
Recently, the 35-plus-year-old
Australia’s electronics magazine
Items Covered This Month
• ‘Playing’ with fire
• TV remote control repair
• Surround sound system repair
• RS-485 network with
•
•
intermittent faults
Philips AE5230 radio repair
Repairing two laptops that
wouldn’t POST
*Dave Thompson runs PC Anytime
in Christchurch, NZ.
Website: www.pcanytime.co.nz
Email: dave<at>pcanytime.co.nz
Masport LPG gas fire we inherited
when we bought this house five years
ago started playing up.
The Masport range is well-known
and seems to include pretty decent
products. However, the model in our
lounge was deprecated years ago and
finding information on it turned out
to be a challenge.
The ‘modern’ Masport company has
nothing relating to it on their website,
not even giving it a listing in its ‘old
bangers’ section. I eventually found,
through a helpful forum post, a PDF
service manual for it. With that, I could
finally plumb the depths of what is still
available for it parts-wise, which, as
you can probably guess, is 5/8ths of
less than nothing.
So, the weather was getting colder,
and our gas fire often wouldn’t start
properly (which entails opening a
valve to the ‘light’ position and pushing a piezo striker button repeatedly
until it decides to work). When it did
light, it performed poorly.
September 2021 75
When we first moved in, one push
would ignite it, and the valve was
infinitely adjustable (according to the
equally-spaced markings painted on
the top of the dial) from a tiny flame
to a roaring fire.
It suited us perfectly, especially after
moving from a pellet stove/fire in our
old house which, while efficient and
easy to manage, entailed lugging 20kg
bags of wood pellets around. That
increasingly became a downside for
me over time [people pay good money
to gyms so they can get exercise like
that! – Editor].
However, lately, the fire’s gas valve
had to be set to full before the fire
would even start, and even then, we
often gave up because it just wouldn’t
go at all.
With research (as is the serviceman’s
way), I found the valve’s manufacturer,
as that is where I suspected the problem lay. I then discovered that even if
we could get one, it would cost around
$600-700.
I wasn’t keen on throwing too much
money at this old fire, but probably
would if it was likely to get it back
into full working order.
Calling in the experts
In the end, I bit the bullet and called
in a gas serviceman. I’d need a licensed
gas guy regardless, and if nothing else,
he could ensure our bottled LPG gas
system (with two 45kg cylinders) was
delivering the right amount of juice
to the fire.
We also have a gas cooking hob on
the same line, and while that seemed
OK, for troubleshooting purposes, one
has to start somewhere...
He had all manner of cool tools
to do his work, especially the electronic stuff like digital manometers
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Silicon Chip
and differential pressure meters, all
of which looked like something I
could use!
Now, I’m quite aware of people looking over my shoulder when I’m doing
my thing, so I made sure to ask this guy
if it was OK if I had a look at what he
was doing and how he did it, purely
out of professional interest.
This wasn’t so I could try to do it
myself in the future – working with
gas is fraught with potentially lethal
pitfalls for the amateur. And here I
refer back to my opening statement;
a few years ago, a house a couple of
kilometres from here (as the crow flies)
literally exploded because a gas fitting
job wasn’t done properly, which created the colossal boom I’d heard and
shook the ground.
It was a miracle nobody was killed,
but there were some serious injuries
and a ton of collateral property damage, so I made a pact that I would
never mess with such things. I merely
wanted to look on and understand the
system used in this house for myself.
The guy did some typical pressure
and flow tests and determined our bottle regulator, an ancient switchable gas
valve that I thought could only be manually switched between bottles, was
working but a bit iffy. For the relatively
low cost of 150 kiwi bucks, it was well
worth upgrading to a newer (and presumably more efficient) model.
It also seamlessly auto-switches
between bottles when one runs out,
something the older one apparently
should have done but never did, at
least in my experience.
That meant the old fire itself was the
problem, and though he serviced it, it
still sooted up and gave below-normal
heat output. It was obvious we needed
a new one.
Australia’s electronics magazine
The astute reader will realise there
isn’t much electronics-related material
in this column so far; here is where
that all changes!
It’s a gas, gas, gas
Long story short (thank goodness!),
we decided on a new gas fire. Though
a different brand, the new version is
essentially the same physical size but
has a higher efficiency rating and overall heat output, so that’s a couple of
boxes ticked already.
It also bristles with electronics,
and there is even an app and optional
add-on that allows users to control it
from anywhere with mobile phone
coverage. I like it very much already!
Another feature is the remote controller; this enables instant, singlebutton starting, fan speed control,
on/off timer settings and even thermostatic control of the room temperature.
A thermocouple that picks up the
room temperature is clearly visible
through a 1mm-round opening in the
side of the remote controller. This is a
double-edged sword, though; surely it
would depend on where in the room
the controller was sitting as to what
temperature it picks up.
The remote comes with a wall
mount, which they recommend putting somewhere handy to the fire.
However, common sense tells me that
if I put it on the wall right behind the
stove, it will be a lot warmer there
than across the room, so it won’t have
a good indication of the overall room
temperature. I’ll have to think about
this feature for a while...
Installation was the next step for the
serviceman. This also interested me, as
it became evident as the process went
on that I could have easily done this
job, except for the ‘gas’ side of things,
obviously. The practical side could be
done by anyone reasonably competent
with manual tools such as drills, concrete screws, wall plugs and the like.
In fact, many of the fittings looked
very similar to the hydraulic lines and
fittings I would have used back in my
airline days, and many of the flanging and sealing processes were very
familiar. While I was reasonably confident I could have done all this, there
was the nagging doubt that the house
could explode if I messed it up, and
I’m pretty sure the insurance assessor wouldn’t be overly impressed!
Fair play!
siliconchip.com.au
I didn’t want that on my conscience
anyway.
Lending a helping hand (or 2)
The serviceman who installed the
fire was an older-school type, and
while very adept at the mechanical
side of the task, he seemed to be struggling a bit with the electrical/electronic side of things. It turns out he’d
installed dozens of this type of fire,
but none with the electronic modules
fitted, and this obviously perturbed
him a little.
I offered to help where I could, and
he was grateful, even naming me his
‘wingman’ in several telephone conversations he had with his colleagues. I
doubted I’d be of much use, but helped
out initially holding torches and keeping things steady in cases where a second pair of hands is most welcome.
When it came to wiring it all up, I
could see he was not that comfortable
with the wiring diagrams and sparse
instructions printed in the installation manual.
The first problem I could see, and
something I foresaw the day before as
the guy was drilling holes in the concrete hearth for the fire mounting fasteners, was access to the electronics.
While there is a manual ‘control
panel’ in the bottom front of the unit,
it isn’t very large. It appeared to me
by reading through the manual that
we’d eventually have to take the various electronic enclosures inside the
fire out to work on them.
With the fire bolted down, there was
very limited room out back to remove
this stuff. Surely, they could have
printed the manual so that installers
could do all this electronics-related
work before the thing was installed.
I suppose this is where experience
comes in; the guy will know for next
time, I guess.
So mechanically, the fire was
securely attached to the floor (a
requirement now with quakes being
what they are here), but we needed to
tweak a few things before we could
(ahem) fire it up.
The first thing he had to do was convert the stove to run on bottled LPG
gas rather than the natural (reticulated)
gas it is initially configured for. That
entails swapping several internal jets
over with the supplied kit. It also had
to be changed in the electronic controller, which by now was very difficult
to get to. It just wouldn’t come out the
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front, so we had to try to get it out via
the back access panel.
I eventually managed to finagle
it out. After removing three screws,
which doubled as cable clamps at one
end of the industrial-looking plastic
controller box, I could remove the
top. Apparently, there was a ‘jumper’
in there that had to be set for LPG use,
but the photos in the Xeroxed installation manual were woeful, making it
very difficult to locate.
As the installer guy admitted that he
had never seen one and didn’t know
what to look for, I volunteered for the
job. With the usual holding of torches,
twisting of bodies and lots of blue air, I
finally found the jumper buried in the
shadow of a heatsink of some semiconductor or other.
Fortunately, it was identical to the
typical computer motherboard or hard
drive jumpers I’ve grown old with, so I
recognised it as soon as I saw it. A set
of curved long-nose pliers (supplied by
me) enabled me to flip it around, and
I set it on one pin only. I could have
removed it altogether, but this allows
any future owner (however unlikely
that scenario is) to revert it to natural
gas operation more easily.
With the correct sticker applied
to the lid of the enclosure (to show
it had been converted for LPG use),
I remounted the top, finding that in
the meantime, all the cabling had
expanded, so I needed longer screws.
Once again, I went to my workshop to
look in my parts bins; luckily, I have
literally thousands of screws of all
types saved over the years, and soon
found three that were suitable.
Once buttoned up, I could stuff the
controller box back into the cavity.
I tried to position it as far from anything hot as possible, and routed all the
cabling into place as best I could, tying
it back with cable ties (again supplied
by me) where necessary.
While the front panel was still
open, the last thing was to put a digital manometer onto a tap by the main
jet and adjust the low- and high-pressure settings for the flame. Then the
acid test: with a single tap of the
remote controller button, the electronic lighter crackled, and the fire lit
up immediately.
Flame up and down is just as
smooth, and with thermostatic control,
our gas usage should be much more
manageable. What luxuries modern
electronics give us!
Australia’s electronics magazine
Overall, I think the serviceman/
installer guy was pleased to have my
help, but it is hard to know sometimes.
We haven’t had the bill yet, so we’ll
soon see how much he appreciated it!
TV remote control repair
B. P., of Dundathu, Qld came up
with an unorthodox repair for a wornout TV remote control. You might not
expect it to work, but it did, solving a
common problem that plagues many
old remotes...
Several years ago, we picked up
a 27-inch TCL TV at a charity shop.
This fitted perfectly in our entertainment unit in the lounge room, replacing a more than 20-year-old CRT TV.
This TV only has an analog tuner, but
we were using it with a PVR that has
a digital tuner anyway.
The TV performed well for several
years, but recently I noticed that it
was getting hard to turn on. I had to
hold down the power button on the
remote hard for several seconds. This
fault was at its worst during winter,
so whatever was causing it was apparently temperature-sensitive.
The remote control for the PVR has
a mode where it can operate the TV,
but it only provides limited controls.
But at least it lets you switch the TV
on and adjust the sound and picture. I
tried this and found that the TV turned
on straight away, so the fault was with
the TCL remote control.
I dismantled the TCL remote to diagnose it. Care needs to be taken when
dismantling remote controls, as it’s
quite common for the clips to break.
In this case, though, it was quite easy
to get it apart without any damage; I
was able to use my thumbnail to prise
the case apart.
I inspected the circuit board and
found it to be quite dirty from many
years of use. I cleaned the circuit board
and the rubber pad button contacts,
and then I laid the rubber pads on the
September 2021 77
circuit board and fitted the batteries to test it. Unfortunately, it still didn’t work correctly, suggesting that the
conductive material on the pads had worn out.
I decided to try putting some conductive grease on the
pads to see if that would solve the issue. Being a retired
motorcycle mechanic, I was fairly sure I would have
some sort of conductive grease on hand, such as graphite grease or similar.
I checked my workshop and found some copper-based
grease, so I tried that. I smeared the circuit board contacts with that grease, then overlaid the rubber pad and
worked the buttons to ensure that each button’s contact
had a light covering of grease.
After lightly wiping down both the circuit board and
the pads, I reassembled the remote control and tested it. It
was now as good as new, with just a light touch switching
on the TV. Several months later, it’s still working well, so
this was another successful fix using a simple solution.
Surround sound system repair
B. C., of Dungog, NSW is the type to help out friends by
fixing their gear when it acts up. In this case, the receiver
had already been ‘professionally’ repaired, but it still
needed a lot of work to put right...
It started as a simple request to reconnect all the surround speakers to Trevor’s LG DVD/VCR combo receiver
(model LH-CX640W), a device with more accoutrements
than your average house. Apparently, it had been repaired
by a service centre in a larger town some time ago. After
its return, it had only been reconnected to the television
using an AV cable; the handful of speaker cables had been
left unconnected at the back of the cabinet.
When the cabinet was moved out away from the wall, a
rat’s nest of very light gauge speaker cables was revealed.
I decided to run all-new heavier gauge speaker cables and
also to clip them up on to the floor joists (the old ones
were dangling). The old cables were used as draw wires,
and apart from two of the runs, there was enough crawl
space to fit most of the cables without too much bother.
I then connected all six speakers to the LG receiver and
powered it up. Upon playing a DVD, the centre speaker
and one rear speaker were silent. Tapping the top of the
LG Combi Receiver would intermittently restore audio to
these two channels.
I disconnected everything again, took it to the kitchen
table and removed the main PCB. I resoldered all the terminals on the speaker output block; some had obvious
dry joints. After refitting the PCB, the machine was reconnected to the speakers. It now worked correctly on all six
speakers, and I was confident that this would be the end
to the sound problems.
About a fortnight later, Trevor mentioned that when
the receiver had been in use for a while, it would just
stop working and the power indicator (red LED) would
flash. If the machine was turned off at the power point
and allowed to cool down, it would then recover and go
back to normal operation.
The day eventually arrived that the flashing red LED
(signalling that the unit had gone into a self-protection
mode) was a permanent feature. I went around to his
place and removed the malfunctioning machine and took
it back to my workshop.
The machine was manufactured in 2005 and has
two switch-mode power supplies on the PSU module
(6870R8300AA). The main one supplies +12V, +5V and
some other minor voltages, while the other supplies the
+35V rail for the surround sound amplifier section. In common with most SMPSs, heat and time affect their reliability.
I tested all the electrolytic capacitors with an ESR
meter, getting a mixture of readings from high to none,
particularly on the smaller value electros. These included
C173, C175 & C176 (all 4.7µF/50V) and C115 & C125
(10µF/50V).There were also some high-ESR electros on
the main PCB: C121, C137 & C138 (all 47µF/50V), all near
voltage regulator IC’s.
Having replaced those, I also replaced the following resistors with 2W metal film types: R104, R105 and R108 (the
220kW start-up resistors), R121 & R130 (both 100kW bleed
resistors) and R138 (the 180W bleed resistor for the +5V rail).
The PSU module was refitted into the machine and then
powered up. The problem was still there! I downloaded a
data sheet for the STRW6753 (power supply IC 104) and
looked at the sample circuit diagram. I decided to order
this IC on eBay as the next move. The IC arrived in the
mail, and I fitted it, but it still did not fix the problem!
There was still something not quite right.
On a hunch, I decided to desolder one leg on every fast
rectifier diode in the main power supply section. I then
tested these for reverse leakage set on the multimeter’s
highest ohms range. When I tested D129 on the +5V rail,
it had some reverse leakage. It was a B10A45V fast diode,
so I substituted one MURF1060 (10A 60V fast diode).
It then worked correctly and did not miss a beat! After
another two days of soak testing, I was confident that
the power supply problem was finally fixed. Trevor was
so pleased with the result that he bought me a carton
of ginger beer and shouted the missus and I lunch at a
nearby pub.
RS-485 network with intermittent faults
N. L. of Taylors Lakes, Vic, had to fix an RS-485 network which was having some odd problems. It turned
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Australia’s electronics magazine
siliconchip.com.au
out to be a part that you wouldn’t expect to be at fault...
I was called to a network using an RS-485 physical
layer (cable and interface cards in each machine) with
25 machines per segment and two segments. The two
segments were connected by a network controller which
polled each machine by their assigned network number,
one at a time, up to the last machine numbered 25. The
network controller was connected by USB to the PC, and
then connected to the internet.
The initial fault was that random nodes were not
responding to the network controller at various times.
This occurred on and off for months, and could not be
isolated to a specific machine. Then the faults became
permanent on one node in both segments.
The cable was a 300W shielded pair, but the shielding
was not connected continuously from one length of cable
to the next or terminated on the network controller Earth
either. One blessing the installer bestowed on the system
was the 120W termination resistors were attached at the
last machine on each segment.
Swapping network boards, it was found that the network boards (two boards) on one machine in each segment were faulty. Back at the workshop, testing showed
the boards to be working perfectly.
I decided to change the line interface chip as they
probably get a hiding from the cable. But the fault was
still present with the boards reinstalled; luckily, I only
changed it on one board.
Back at the ranch, I hooked up the Silicon Chip Digital
Audio Signal Generator (March-May 2010; siliconchip.
com.au/Series/1) to deliver a square wave and noted that
at the output of the line interface IC I had changed, it
worked properly. Still, the digital receive signal was not
present at the network board output.
Between the MAX3062E line transceiver chip and the
digital output to the machine microcontroller was an
HCPL-2200 high-speed opto-coupler with a TTL output
which was failing as the switching rate increased.
Of course, replacing the opto-couplers solved the problem on both segments. I also re-cabled the longest segment
with the correct 120W RS-485 cable with a continuous
shield, using the original cable for the recommended reference point connections.
Being differential, I am not sure what the reference
point connection does. My theory is that it protects the
line transceiver IC when one node powers down; any
line over-voltages can dissipate into the powered nodes
supply instead of through the unpowered transceiver’s
internals. I welcome comments on that.
I am now waiting to see how long the incorrect cable
lasts before it gives errors. The customer (and the installer,
whom I know) insists that I am wasting time and money
replacing the cable since the existing one “works OK”.
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Philips radio repair
G. McD., of Jindalee, Qld got angry at his radio when it
began resetting intermittently. Thankfully, he managed
to calm himself down long enough to find the dodgy connection and fix it...
My patience was pushed to the limit recently when
my trusty Philips portable FM/DAB radio, an AE5230
model, shut down on me for the umpteenth time early
one morning.
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Unit 1 /37 Leighton Place Hornsby NSW 2077
(PO Box 606 Hornsby NSW 1630)
Tel: 02 9476 0300
Email: service<at>switchmode.com.au Website: www.switchmode.com.au
Australia’s electronics magazine
September 2021 79
All I was doing at the time was trying to increase the volume. The LCD
screen died immediately, then after
what seemed like a full thirty seconds, it lit up once more as details of
the pre-tuned station began flickering
across the screen.
I barely avoided flinging the radio
across the room in frustration. It had
been acting like a temperamental teenager for months. Later that morning,
I decided that enough was enough;
it was time to see if I could fix the
pesky thing.
The first suspect was the DC jack at
the back of the radio. Close inspection
with a headband magnifier showed
nothing obvious. So I had to open the
radio up and delve a little deeper.
I removed five retaining screws
from the rear of the radio’s enclosure, allowing me to take off the back
panel. I then identified the screws
that held the main PCB in place. I
removed these and unclipped the
main power lead.
The on/off switch was now clearly
visible. I removed the two small
securing screws holding the PCB
upon which it was mounted. With the
aid of a strong lamp and my headband
magnifier, I inspected the condition
of the three wires soldered to traces
on the PCB. What I saw wasn’t pretty.
The solder joints looked as though
they had seen better days, and the
wires were coated with some kind of
dried goo.
After desoldering the three wires
(red, white and yellow), I cleaned up
the through holes on the board with the
aid of a solder sucker and refurbished
the ends of the wires. I then cleaned
up everything and soldered the wires
back into place, and returned everything to its original position.
I plugged in power and hit the on/off
switch. All appeared to be working as
it should, so I set it up once more on
my bedside table. But the next morning, around 4:00AM, the radio spat
the proverbial dummy once more. It
was up to its old tricks, I thought, as I
began pondering my next step.
The problem had to lie with the
power supply; I had been trying to
adjust the volume at the time and in
so doing, had moved the radio slightly
to see the dial better. The DC jack was
now my prime suspect.
I placed the radio back on my workbench early the next morning and
opened it up again. The DC jack is
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Silicon Chip
held in position in much the same
way as the on/off switch, on its own
PCB that is held in place by two small
screws. Once I had removed them, it
was an easy task to slide the PCB out
for inspection.
Under a strong light and with the aid
of my headband magnifier, I noticed
one of the soldered mounting pins
had a hairline crack around its base.
It was immediately evident that this
was a result of stress from the slight
sideways movements caused every
time the plug is inserted or removed.
All I had to do was re-solder the
connections and put everything back
together again — a simple fix to a problem that was not so simple to find. The
radio has behaved itself ever since.
Repairing two laptops that would
not POST
K. D., of Chermside, Qld, writes: in a
previous Serviceman column (August
2014, page 61), I stated that I don’t
believe in coincidences. Following
some recent incidents, I might have
to change my mind.
A friend at a university biochemistry
laboratory told me that two large ultrahigh-speed centrifuges in her laboratory both failed at switch on, within
minutes of each other. Both emitted
smoke and would need repair by the
manufacturer’s technicians. The next
day, at my workplace, two identical
and quite critical refrigerators failed
within 24 hours of each other, having
not missed a beat in over five years.
The third coincidence involved
me, the same friend, and both of our
home computers. It happened only a
week after the coincidental failures at
work. One night, my ageing Dell Vostro
PC simply shut off mid-use. When I
attempted to restart it, the fans all spun
up, but that was it. The computer could
not even generate a beep code from the
power-on self-test (POST).
As I was working at the time, I
decided to leave any further investigation until I had a few days off. Before I
could look at my PC, my friend called
to say that her equally old Dell Inspiron PC wouldn’t switch on. This was
worrying as she didn’t even remember
when the computer was last backed
up, or where the backup was stored.
When she brought it to me, the
symptoms were identical to mine – the
power indicators were on, and the fans
were spinning, but the PC wouldn’t
even get to the POST.
Australia’s electronics magazine
I decided to tackle her Inspiron first.
I checked the voltages from the power
supply, and all were within specification. As the fans ran and responded
to the power button, the motherboard
couldn’t be completely dead. I disconnected everything possible from
the motherboard and removed the
memory modules and graphics card.
The machine could still not get to the
POST.
On the off-chance that the BIOS had
been corrupted, I removed the CMOS
battery and turned on the power. At
last, the machine gave four beeps,
indicating that there was no memory.
I fitted a new CR2032 cell and reconnected everything I had disconnected.
The computer told me the BIOS had
been changed and that the date and
time were invalid. I was prompted to
press ‘F1 for defaults’ or ‘F2 to setup’.
I pressed F2, and the PC hung with
an “ME unconfiguration in progress”
message. ME means the management
engine for the BIOS. This behaviour
was reproducible when turning the
computer on and off – pressing F2
wouldn’t get me into the BIOS.
After the first power cycle, though,
I had an option of pressing F12 for
boot devices. Pressing F12 got me
into the BIOS. All the settings looked
usable except for the date and time.
After setting those details and a ‘save
& exit’, Windows started normally,
and the computer was fixed. It was
sent back along with some unparliamentary language about the need for
regular backups.
My Vostro has had a hard life, but it
had the same symptoms as the Inspiron and I hoped it also had the same
easily-fixed problem. So, I removed
the CMOS battery and applied power,
and that is where the similarity with
the Inspiron ended. The computer
still would not reach the POST. I progressively removed parts and applied
power each time.
When I removed the four 2GB memory modules, the POST test ran and
indicated that the memory was missing. I fitted four replacement modules
from a defunct Vostro obtained from
a friend and reconnected everything.
Pressing F2 at startup allowed me to
reset the date and time in the BIOS
and check that 8GB of memory was
being detected.
Windows then started normally,
and another veteran computer was
returned to service.
SC
siliconchip.com.au
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