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SERVICEMAN’S LOG
Gaining a superpower, at least temporarily
Dave Thompson
I’ve always wanted to be able to see in the dark, but sadly, that is not
among my superpowers (mainly, I’m just good at repairing stuff). But
when the opportunity presented itself to try a ‘toy’ that could give me
that power, if only briefly, I jumped at the chance.
Every now and then, a job comes into the workshop
that I find very interesting. Much of my work is boring
computer stuff that any current 12-year-old can do, and is
barely worth mentioning. But there is a wealth of projects
out there built by keen hobbyists that sometimes don’t go
to plan, and sometimes they need help getting them going.
Any newly-built electronic device, powered up for the
first time, might not work. At least not correctly. In the
worst case, the magic smoke escapes in a catastrophic failure. I’ve had plenty of all of these scenarios in my time,
but I have learned not to be so reckless when powering up
newly built devices!
I remember all too clearly that eagerness to solder everything in, wire it all up and just throw the switch (while
throwing caution to the wind) without first checking thoroughly whether I have made mistakes. In that moment of
excitement, the thought doesn’t even occur!
Errors are not always lethal in hobby electronics, but
caution is still more prudent than impatience.
A blast from the past
A while ago, a local guy brought in a device that I
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recognised immediately because I’d wanted to make one
since I first saw plans and kits advertised in those small
ads typical of late ‘70s to early ‘80s American electronics
magazines.
It was a ‘see in the dark’ “scope”, and back then, I
thought it was merely a joke, like those X-Ray glasses you
could buy for a buck. We all know they were a con – disappointingly, you couldn’t see the bones in your hand or
see-through clothes like the ads promised. That was until,
in the mid-1980s, I sent away for a book titled “Build Your
Own Space-Age Projects” by a chap named Robert Ianini.
Buying anything from overseas was a real mission in
those days, before the internet existed or was widely
accessible. I had to write to the company in America and
enclose a money order, sourced from the post office, for
an equivalent number of US dollars. Hopefully, after about
six months, I’d receive the book.
It did eventually arrive, and that ‘see in the dark’ project
was one of the devices featured (along with such projects as
anti-gravity machines and various home-built high-powered
lasers and electron “ray” guns). It was then that I realised
it was a legitimate electronics project that could be built
by the home hobbyist.
I’ve always been fascinated with night-vision stuff,
and here was something I could potentially build myself.
Although it was adequate for basic experimentation back
in the ‘80s, it was nowhere near as good as commercial
equivalents available at the time.
Night-vision hardware – or, more correctly, the image
intensifier tube inside the device – is typically classified
in ‘generations’. This starts at Generation 0 and goes up to
3rd generation for modern starlight-amplified devices – at
least for civilian use.
These days, it is almost impossible to import any of
today’s Gen3 night-vision devices from the USA or the UK
without an export license from those countries, which of
course isn’t easy (or cheap) to acquire. This DIY device
would likely be somewhere between Generation zero and
one, in that it requires an external illumination source to
see anything at all.
In other words, it doesn’t amplify available ambient light
as the later generation devices do.
The biggest problem for me back then, and what eventually stopped me from building one, was the requirement
for a very specific type of vacuum tube called an “image
tube” or “image converter tube”. This tube has a mirrored
28mm ‘lens’ at the front and a small, green, phosphor-coated
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cathode-ray-tube style ‘viewer’ at the rear, about 15mm in
diameter.
These tubes were not available anywhere in New Zealand
at the time (or even Australia as it turned out; I looked for
one on a couple of my early visits there). So this project
was dead in the water from the beginning. Even the supplier in the USA – the guy who wrote the book (still) runs
a company there providing kits and plans – couldn’t supply the tube, so it had to be sourced separately.
Oh well, just another dead idea among many others!
And this is the way it remained until a few years ago. I
was browsing an overseas auction site for valves for guitar
amplifiers when, suggested to me at the bottom of the listings, was one of these image tubes, a Capehart Farnsworth
6302 Image Converter tube. I remembered, from all those
years ago, that it was a direct substitute for the original
IR16 type tube specified in the plans.
This one was ‘new old stock’ (NOS), still in the box for
only US$80, including shipping. As this triggered my memories, I thought I might just revisit this project after 30 years.
So I snapped it up and hoped it didn’t get broken in transit.
It arrived safely, and I put it with my other tubes in a
drawer. There it sat, unused. I never did get around to building a ‘see in the dark device’ because, well, just because.
to check it, but even with fresh batteries, the output (invisible to the naked eye) was pretty weak. I had an idea to fix
Enter the customer
this, but I would talk to the client about it later.
Imagine my great surprise when a customer brought one
I also put a fresh 9V battery into the handle of the ‘scope’
of these exact units in to see if I could fix it! He’d been and pressed the button, but there was no life from the tube
given it by an uncle or some-such who had built it way at all. That didn’t bode well. The problem could be caused
back when and he knew very little about it, except that it by the tube or any part of the power supply or oscillator
used to work, but it didn’t anymore.
boards.
It looked almost identical to the project from all those
The circuit is pretty straightforward; the power input
years ago, so I was keen to get stuck in and see what was takes 6-12V DC (9V rechargeable battery preferred). A reawhat.
sonably standard single-transistor, free-running LC oscilThe customer – as is typical – didn’t want to spend a lator drives the primary of a custom transformer.
fortune on it, so I said I’d assess it and see what I could do.
The secondary connects to a 12-stage full-wave voltage
I started with the illuminator. This was a crudely- multiplier (in this case, a classic Cockroft-Walton arrangeconverted torch, with the reflector chopped up to accom- ment of diodes and capacitors) which supplies high-voltage
modate a small array of infrared LEDs. I used my camcorder
DC ranging from 12-20kV (typically 15kV depending on
the battery state) to drive the tube.
There is also a tap from early on in the voltage multiplier that provides about 1/6th of the overall potential to
connect to the tube’s focus ring, allowing builders to adjust
focus within the tube. This is typically done once the rest
of the circuit is operating. Various taps can be taken from
different junctions on the multiplier and tried until the
sharpest image displays on the viewing end.
Items Covered This Month
•
•
•
•
•
Gaining a brief superpower
Fixing a ducted gas heater
Tektronix 556 oscilloscope repair
The revolving door of PVR repairs
Fixing an aircon with a faulty switch
Dave Thompson runs PC Anytime in Christchurch, NZ.
Website: www.pcanytime.co.nz
Email: dave<at>pcanytime.co.nz
Cartoonist – Louis Decrevel
Website: loueee.com
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April 2022 93
By itself, the tube image is inverted from one end to the
other, so a sliding lens arrangement is used at the input
end to correct this, allowing manual optical focus and also
making things a bit larger. An eyepiece mounted at the back
end of the PVC tube body is added mainly to protect the
rear of the tube; it is basically a plain, unmagnified ‘lens’.
Acquiring the right lens and eyepiece was another giant
hurdle in the project back then, but obviously, the guy
who made this one had purchased the short-form kit and
sourced an image tube from somewhere else.
Judging by the condition and colour of the PVC pipe used
to build the device, it was likely quite old. Pulling it apart
was easy enough – at least he hadn’t glued it all together.
Pulling out the power supply from the handle and the
tube-driver board from the main body of the viewer was
also straightforward.
The build quality was average, with some relatively
sloppy perfboard point-to-point soldering employed. When
boosting a voltage to this level, it is imperative that nice
round solder joints are used on the multiplier, or at least
normal joints insulated with enamel paint or corona dope,
because arcs can form at the solder junctions if they are
sharp and exposed.
It all looked a bit rough and ready, but it obviously had
worked at some point, so all I had to do was figure out why
it wasn’t going now.
Battery power was certainly getting to the board but
stopped at the transistor, a classic TO-220 style MJE3055.
From memory, this should have a heatsink, but it had
none. I had several similar transistors in my parts bins, so
I pulled this one and replaced it with a known-good one.
This time, when I fired it up very carefully on the bench,
I could hear the familiar faint HV crackle from the multiplier, which could indicate that something might be breaking down somewhere. The tube remained dark.
It was good to know that at least the oscillator was working. The proprietary transformer used was also likely not
open-circuit, but working around these Cockcroft-Walton
circuits always makes me very nervous. I’ve experimented
with them before many times, in the likes of air ionisers
and various electrostatic experiments. It’s a case of once
bitten, a hundred times shy!
This one ‘only’ puts out in the region of 200µA at the
nominal 15kV, but that’s enough to make someone jump
and yell!
flying leads, so a standard valve tester wouldn’t be of any
help. I could find nothing about testing them online, so it
was just a matter of swapping it out and hoping for the best.
I temporarily put my tube alongside the unit. The IR16
has pre-connected wiring while the 6032 doesn’t, and
that meant soldering directly to the metal body and rings
around the tube itself. That also made me nervous, and the
other thing was that the book plans (which I’d since dug
out of storage) didn’t show which wires went where with
this particular tube.
There was nothing to do but try it, so I guessed where
they were supposed to go by the physical layout of the
tube itself. I mean, there are only three connections: one
at the front, one as a ‘ground’ on the main metal body of
the tube and one for the focus, which I assumed was the
middle ring. What could possibly go wrong?
As it turned out, nothing. I wired it how I thought, was
über-careful soldering to the tube’s metal parts and used
one of my trusty bench power supplies to power it all up. I
started with severe current limiting, just in case, but gradually increased it until things started happening.
It all looked OK, and the tube started glowing at the rear
end. I could vaguely see an image, but it was very faint in
bright light. I’d need to mount it and adjust the lenses and
the focus voltage to really test it properly, not to mention
using it with a decent IR source.
I called the client and told him what the costs would
be, and as he was OK with it, I persevered with the rest
of the job.
First, I resoldered all the multiplier’s connections and
any others that looked dodgy, then mounted a heatsink on
the transistor. I didn’t have a lot of room, but a small Jaycar
heatsink I had (HH8514) fitted in the case and should suffice. As I might need to have the tube in and out to set the
focus voltage, I temporarily mounted it in the PVC body
and held it in place with sponge wedges.
With the workshop lights out, and the illuminator on,
I could make out some outlines, but the focus was off. So
out it all came, and I used another tap to test it. There is a
provision in the plans for adding a resistive voltage divider
network to further fine-tune it, but as it turned out, the
image was pretty sharp with the next tap along, so I left it
at that for now.
The converted torch illuminator was very crudely made,
Taking the tube
I don’t have the gear to measure that kind of voltage, but
it appeared to be working, so that left the tube itself. This
one was the IR16 version of the tube, which was different
in connections and size to my 6032 type, but if necessary,
I could make it work – as long as my tube was functional.
I wouldn’t know unless I tried it, so I set about removing
the IR16 from the body tube.
It was held in with three long screws, 120° apart,
threaded into the PVC body. These pressed lightly on
the tube and centred it. They had been coated in what
looked like RTV or some other silicone sealant to stick it
all together. Space was tight, but with patience, perseverance and a sharp hobby knife, I managed to get it all out
without breaking anything.
From the outside, there’s no way to tell if the tube is
working or not. It has no pins like typical tubes, just three
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and while it would work, I had a better solution. When
dad was alive, he experimented a lot with then-quite-new
LED torches, and he had several that were rechargeable
and about the size of a three-cell Maglite torch.
I inherited several working models and a few he had used
for parts. The torches use an array of bright white LEDs
mounted in a specially-moulded reflector and were very
bright; all I’d have to do is swap the white LEDs for infrared versions, and I’d have a very powerful, self-contained
IR illuminator.
I’d already factored in the cost of this to the client, and
while I was happy to give him the torch, I did need to buy
25 IR LEDs for the job.
I disassembled the torch and, using my trusty Goot desoldering pump(s) and lashings of solder wick, managed to
extract the old LEDs without damaging the PCB they were
all mounted on. It was then simply a matter of installing
the IR LEDs and putting it all back together.
Turning it on resulted in absolutely nothing because it
is invisible. But my camcorder showed a powerful beam.
That night, I fired up the whole thing and scanned our
backyard. The output from the tube was patchy in darker
areas, but everything was visible. I was pretty impressed
and spent quite a while playing with it.
Satisfied that it was operational, I used RTV to bog in
the tube and buttoned it all up properly. So, after all these
years, I finally got to play with one and didn’t mind losing
my tube to a working model.
Sometimes I love this job.
Fixing a ducted gas heater which had a faulty ignition
M. H., of Albury, NSW had a whole range of electronic
appliances fail in a short time. Is he cursed? Probably not,
considering that he managed to fix them all with just a few
dollars’ worth of parts and some hard work...
My pool chlorinator cell wore out. My attempts to repair
it worked for a short time, but the plates were corroded
away after seven years of hard work. A new one was the
only option, and $650 later, it was back in service.
At the same time, some small ants had entered the chlorinator supply box and destroyed the SMPS driver IC. After
an eBay purchase and a few weeks delay, the supply was
back in service.
Then tree leaves got past the filters, entered the impeller
and jammed the motor, and the pool started going green
again.
The motor is designed to be easily split to remove the
obstruction, and the motor ran again without relying on
the thermal cutout device to protect itself.
If I had called the pool company to fix all these problems, I would have probably spent $1000 more than I did,
given all the service call fees and the fact that they would
likely replace all the parts rather than fix them.
I realise that they have a lot of overheads, and quoting
for a new part is the best option for them. In part, that’s
because it moves the warranty for the repair restoration to
the manufacture for 12 months (or more) and moves liability away from the serviceman.
Next? Now my ducted gas heater would not start. With
an ear pressed to the outer case of the in-ceiling heater, I
could hear the combustion chamber fan start and run. After
a short delay, the fan stopped and the unit smelled of gas
with no ignition. The cycle repeated endlessly.
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I removed the power for five minutes and tried again.
Success, the combustion chamber fan ran, the gas relay
operated and ignition. But the ignition lacked the aggressive volley of sparks sound that it usually had. The Honeywell ignition box was sad; most likely, it uses capacitor
discharge via an SCR.
The unit was easy to remove, easy to open, but impossible
to repair. The manufacturer had covered the EHT section
with epoxy resin. A lot of heat, wiggling and cutting eventually got the single-sided PCB out of the case to reveal a
dry joint on the discharge capacitor (1μF 250V polyester).
The remainder of the circuit design looked (to me)
straightforward and expected, with a thin, cheap singlesided PCB manufactured by solder reflow. The capacitor
measured close to 1μF, but I replaced it anyway with a
1μF 2kV polyester capacitor pinched out of a plasma TV.
The unit produced the clearly audible volley of aggressive
sparks while the flame established itself. Success!
A professional serviceman (in my opinion) would not
be inclined to diagnose the fault. After a quick assessment
of the age of the unit, they would give the expected “I will
get a quote for a new one” and “that model is not made
anymore”. The replacement ignition system would come
in about $500 plus the hourly service rate and call out fee.
Again, I was greeted with a small pop and two blown
30W resistors. This had me quite confused, as all components for that rail tested good, and no other faults were
obvious. These 30W resistors are no slouches, being 5W
wirewound types, making me think there must be a catastrophic short somewhere.
I then realised that testing the transistors out-of-circuit
was a mistake; when installed back onto the heatsink, there
was a short from collector to ground. On one of the little
boots that insulate the transistor screw from the heatsink
and allow a connection to the collector, there was a burned
carbonised track from a previous arc. This was impossible
to see as the boot is black.
All that separated the 225V rail and ground was 1mm of
burned plastic. Upon replacing this and the two 30W resistors again, the scope powered up as it should. I left it for
half an hour before trimming the -150V, 100V and 225V
rails. I’ll need to recalibrate the timebase as I fiddled with
the voltage rails, but that can wait for another day.
I can only assume that a build-up of dust and condensation from recent cold days caused the insulator to arc over.
Evidence of greasy, dusty grime was present. So before reassembling the scope, I gave it a thorough cleaning throughout in the hope that this never happens again.
Fixing a fried Tektronix 556 oscilloscope
The revolving door of PVR repairs
D. V., of Hervey Bay, Qld got a shock when one of his
prized possessions had a minor explosion when he powered it on. The cause appears to be age-related, but perhaps
not in the way you might think...
I have a collection of old Tektronix oscilloscopes; the
latest acquisition was a mint-condition 556. Even though
I had switched it on several times before, on this occasion,
I was greeted with a loud bang followed by what could
only be described as the sound an egg makes when frying
on the barbie.
Reaching to switch it off felt like an eternity, but in reality, only a few seconds passed. However, the damage had
been done.
On inspecting the underside, I found two 30W resistors
had burned out. These are part of the +225V circuit, and the
fact they were damaged at all surprised me, as the 225V rail
is individually fused and the fuse was intact. This led me to
believe the fault was within the power supply unit (PSU).
Scopes like my 556, while discontinued mid-1970s, are
marvels of engineering. It is a true dual-beam scope and
boasts tunnel diode triggering, dual plugins, individual
timebases and 50MHz bandwidth. It is a monster weighing
40kg, with 34 valves and sinks 840W when in operation. No
wonder it was the last of the 500 series scopes to be made!
The regulator circuits in the 556 are semiconductor-based
whereas the previous 500-series scopes used valves. Transistors T03 and T02 in the PSU are mounted on a heatsink
directly behind the fan assembly because Tektronix had
difficulty keeping these components cool. T03, the main
pass transistor for the 225V rail, had gone short-circuit. It
was a 2N4348, so I substituted a 2N5672 from the junk box.
I removed all the other transistors from the defective
rail and they tested OK. I replaced the two 30W resistors
and wondered if this will be the magic bullet, but I had
doubts. So with the 225V rail fuse removed for posterity,
I proceeded to switch the unit on for just a second to see
what would happen.
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B. P., of Dundathu, Qld has had to fix the same devices
multiple times due to similar faults. It seems that they were
made with poor quality components...
We use two Beyonwiz DP-P2 Personal Video Recorders
(PVRs) to record and play back TV programs. I originally
bought both of these units on eBay as “not working, for
parts”, both with an ERROR 0000 fault. In both cases, the
cause of the faults were bad electrolytic capacitors in the
power supply.
I fixed both these units when I got them a few years ago
by replacing the bad capacitors, and both worked well for
some time, although I had the same fault return in one unit
when another capacitor failed.
Recently, my son told me that the PVR in the camper
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was playing up. Sometimes it would work correctly; other
times, it would show the ERROR 0000 and yet other times,
it would be on when it should be off. Usually when it’s off,
it shows the time on the front panel, and everything else is
on standby. But sometimes, it would be off with the hard
drive still running.
Removing the lid, I could see a bad 3300μF 10V capacitor.
I looked through my salvaged capacitors, found a suitable
replacement and fitted it. While looking over the circuit
board, I spotted a small capacitor that looked suspicious.
It was a 330μF 25V capacitor, so I removed it.
Then I noticed another one of these capacitors that looked
suspicious, and this kept happening until, in the end, I had
removed at least six of the same value electrolytic capacitors. I later tested these with my ESR meter, and all read
well above what they should have.
I found replacement capacitors in my salvaged capacitors collection, installed them, and then put the power
supply board back in the PVR. After buttoning it up again,
it was working well.
Not even a week later, I turned on the other PVR in the
lounge room, and it showed ERROR 0000. This PVR had
been working well since its original repair, apart from
Channel 7 being corrupted during the day, although it
was usually mostly OK at night. There was also occasional corruption on SBS. None of the other channels
had this problem.
After removing the lid, I could see a really badly bulged
3300μF 10V electrolytic capacitor. Not only had the top
bulged, but the seal on the bottom had been pushed out,
and the capacitor was sitting at a significant angle. This
was obviously the cause of the ERROR 0000 fault.
I removed the defective capacitor and I found a replacement Nichicon capacitor in my salvaged capacitors. I
scanned the PCB, but I could not see any other problems.
All the rest of the capacitors, including the small ones I’d
replaced in the other PVR, were fine.
A quick test again showed the unit to be working. Since
the repair, the corruption on Channel 7 seems to have disappeared. It’s really handy being able to make these repairs;
otherwise, taking the unit(s) to get repaired could easily
run into hundreds of dollars, and purchasing replacements
would be similarly expensive.
Aircon repair reveals a faulty switch
R. W., of Hadspen, Tas offered to fix his friend’s air conditioner (which was said to be unrepairable) and traced the
fault came back to poor installation practices...
Many years ago, I was asked by a friend whether I knew
anything about air conditioners. He had 5kW and 2.4kW
units from a reputable manufacturer installed in an innercity apartment in Brisbane, and the 2.4kW unit stopped
working after a year or so.
An air-conditioning tech looked at the unit and told
him it needed replacement, as the boards and refrigerant were no longer available. A quick check on the internet revealed that was not the case; while there would be
benefits in replacing the unit with an inverter system, the
cost seemed unwarranted on such a relatively new unit. I
thought it was worth a look.
During the installation, the electrician had routed the
single-circuit power cable through the downstairs ceiling
and had cut several holes in the plasterboard, which were
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later covered by four blank switch-plates and a snap-in ventilator. The smaller unit had a square section of adhesive
conduit emanating from a bedroom power point, then passing through the external wall to the outside isolator switch.
My friend was not happy with the blank plates, and had
a plasterer make good the ceiling. He put up with the conduit as it was largely hidden by a bedside table. This suboptimal installation should have given me a clue.
The 2.4kW unit responded to the remote commands, and
when the internal fan started the louvres were able to be
adjusted. About three minutes after powering it on, I could
hear a relay click, but no cold nor warm air emanated. The
problem seemed to be in the outdoor unit.
This air conditioner had all of the control electronics on
a board in the indoor unit with two switched Active wires
going to the outdoor unit, one for the compressor and outdoor fan and one for the reverse-cycle solenoid – all fairly
simple. I monitored the outdoor unit, and after the compressor timer had run, the outdoor fan ‘kicked’ but that was
all. It was time to look at the circuit board.
After removing some connectors and prising some clips
off, the board was easy to remove. I looked for the usual
suspects like dry joints, bulging capacitors and burnt components but found none. I decided to connect the infrared
sensor and bench test it with mains applied, taking the
usual safety precautions.
The board behaved faultlessly. The relay clicked in, and
power was available to the outdoor unit terminals. I connected a fan heater to these terminals in case the relay contacts had failed, but it sustained a 10A load. It had to be
something in the outdoor unit. I was thinking possibly a
failed compressor or motor run capacitor, but this did not
explain why the outdoor fan would not run.
I reinstalled the board and put it through its paces again
while up on the ladder. This time, I noticed something that
I should have realised earlier. The relay clicked in then
dropped out, and the indoor fan lost speed when it clicked
in. I connected a voltmeter to the input mains and noticed
it drop to less than 100V AC when the relay energised. This
drop was not apparent at the power point.
I flipped the power circuit breaker and went to recheck
the outdoor unit. It was then that I noticed a rust stain down
the wall behind the isolating switch. I took the switch cover
off, and rusty water poured out.
The switch was not sealed against the wall; water had
entered, rusted the mounting screws and caused a high
impedance path within the switch. My friend engaged a
better electrician to replace the switch, and the unit is still
running some ten years later.
SC
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