This is only a preview of the July 2022 issue of Silicon Chip. You can view 44 of the 112 pages in the full issue, including the advertisments. For full access, purchase the issue for $10.00 or subscribe for access to the latest issues. Articles in this series:
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SERVICEMAN’S LOG
Trail camera fun
Dave Thompson
Sometimes when you’re presented with a faulty device with no obvious
symptoms, you have to take an educated guess and repair the bit you
think is most likely to fail. That’s what I did this time, and while it was
a bit of a circuitous path, it eventually led me to the right conclusion.
Sometimes, you just need to trust your gut instinct.
Remote cameras have been used in sports and wildlife photography for decades, but they have increasingly
become both much more advanced and affordable recently.
One particular use of them that has grown hugely in the
last few years is in the great outdoors.
Hunters, nature photographers and conservationists are
all big users of so-called trail cameras (sometimes called
hunting cameras). These devices use increasingly modern
technology to allow users to ‘set and forget’ camera traps
out in the wild that (hopefully) capture images and videos
of animals or natural activity that is rarely seen.
The basic idea is simple: set up one or more cameras in
an area of interest, and anything that meanders past, day
or night, will trigger the camera into action. Most of the latest devices can record both high-resolution video and still
images, with the captured data stored on a built-in memory card. In some models, it is also transmitted via SMS/
MMS to a mobile phone.
Most of these cameras also have night-vision capability,
using arrays of high-intensity infrared LEDs to provide a
wide area of night-time illumination, even in complete
darkness.
The advantages of this scheme should be obvious; a
standard flashgun would work, but would scare off (not to
mention temporarily blind) any detected game. However,
the invisible-to-most-eyes infrared flash or flood would
not reveal the presence of anything out of the ordinary to
the quarry.
I first heard about these cameras many years ago, after
one of our cats went missing, and I looked into buying one
because reported sightings were coming in. We wanted
some way of knowing if he was turning up to these people’s places. He also may have been coming back home
after dark. Either way, we wanted to know.
I did my ‘due diligence’ and purchased a mid-priced unit
from a reputable brand at a local retailer. This model had
a 2-inch (5cm) screen for reviewing footage and a range of
functions we’d likely never use, all in a relatively compact,
camouflage-motif case.
I had a good play with it before deploying it, and it lived
up to the bumf. The photo quality was especially good,
even in complete darkness, though this was monochrome
– during the day, it took the usual full-colour snaps. Then
again, one would expect decent quality with a purported
12-megapixel sensor and a fixed-focus lens.
The camera used the older SD card format for data storage, and even a relatively-small 4GB card was enough for
a lot of photos. However, if the video recording option was
enabled, it used up the storage space pretty quickly, so I
stuck with stills initially.
Its battery life was good, but this model also had a ‘backpack’ battery holder, meaning an extra four AA-size cells
could be fitted, giving the camera a significant amount of
unattended operation capability.
The whole idea is to ‘set and forget’ and come back in a
few days, weeks or months to download what the camera
has captured in the meantime.
I soon learned that trawling through a thousand
almost-identical images was a considerable time investment! Leaves, wind, birds, hedgehogs, cats, dogs, mice and
bugs could set it off – and often, the image would show
nothing but a slight ‘spot’ in range of the PIR sensors. Ah
well, we don’t get anything for nothing!
Enter the customer
My point – as usual, a long time coming – is that a customer recently brought in one of these cameras for me to
look at. Ironically, he’d brought one into my workshop a
few years previously (a considerably older model) that he’d
been given but did not work.
When I cracked the case open, I could see why; someone
had stored it long-term with batteries in place, and they had
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Items Covered This Month
•
•
•
•
•
Messing around with a trail camera
The dilapidated pair of touch lights
The compact fault whisperer
Follow-up to Clenergy 1.5kW solar inverter
Repairing a lathe’s motor speed controller
Dave Thompson runs PC Anytime in Christchurch, NZ.
Website: www.pcanytime.co.nz
Email: dave<at>pcanytime.co.nz
Cartoonist – Louis Decrevel
Website: loueee.com
leaked – badly. The entire area of PCB beneath the battery
holder had corroded away, and the device was completely
dead. Even if I could see any tracks (or remains of tracks),
it would have been impossible to repair them.
He was philosophical about it – he’d been given it after
all – and used that as a premise to buy a fancy new one. It
was this new model that brought him back this time.
It had worked hard for several years, usually mounted
out by a run on his rural property, monitoring for feral cats
and any other predators that were breaking into the run and
decimating his chicken population. This had become an
essential piece of kit in preventing animals from poaching
his stock, and he was keen to get it back to work.
This meant that it had spent all of its working life sitting in weather, ranging from far below freezing to baking in the scorching summer heat. I was surprised it had
lasted this long! I hated to think what it was like inside,
IP66 rating or not!
The problem was that while it appeared to be working
(various lights on power-up etc), it was not taking any new
photos, the last one having been several weeks previously.
Something had happened in the meantime, although on
careful questioning, he did say that he had changed batteries ‘around’ that time. This was a clue, perhaps.
Getting it open was no challenge. Six screws held it all
together, and after removing them, I could gently ease the
case apart. It was pretty tight, which was caused (it turned
out) by the weather seals holding on tightly.
Each screw turret had a rubber seal between it and the
back of the case, and there was a large, embedded ‘o’ ring
in a channel around the very edge of the case. This is flattened slightly by the screw pressure on the other half of
the case, and should have kept the inside weatherproofed.
I was expecting carnage inside, given its working history, but it was actually pristine. That weatherproofing
did its job well!
The only real possibility of water/environment ingress
into the case would be through the hinged access panel.
When the camera is sitting normally, it is at the very bottom.
That puts it out of any real weather just by being where it
is, and that trapdoor has a seal on it as well.
Popping that hatch open reveals all the main controls,
including an Off/On/Test switch, external power and video
out connectors and mini-USB and SD card sockets.
The screen is on the rear of the device, covered by the
backplate in normal use, and below that are membrane-style
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shuttle buttons for manually taking photos or movies and
for captured video and stills playback. This allows it to
essentially operate like a standard digital camera. Usually,
in ‘test’ mode, the screen is activated, and we can alter
camera settings and preview captured data; but that was
no longer happening.
Turning the camera ‘on’ using that switch would usually
result in a red LED embedded within the LED array flashing for 10 seconds before going dark, indicating the camera
is ‘armed’ and ready to detect any movement. The delay
gives the operator time to shut the hatch and exit the area
without taking any accidental selfies.
Pushing the switch further to ‘Test’ mode also fires up
the red LED, and then a blue one next to it lights up when
the two PIR sensors detect any movement. This allows
more accurate positioning of the camera’s detection area,
similar to a ‘walk’ test we do for home alarm PIR sensors.
As I mentioned earlier, the screen didn’t light up in Test
mode. Neither did the blue LED activate. All roads led to
Test mode not being entered at all, and on top of that, even
in normal operating mode, the camera no longer wrote anything to the SD card.
Something seems fishy
I suspected the switch itself. It didn’t ‘feel’ right when
actuated, and as one of the very few moving parts, it was
at risk of wearing out. Getting to it was not easy; the PCB,
which is stuffed with electronics, sits sandwiched between
the moulded battery holder and the hard-plastic back half
of the case.
Space is very tight, though the PCB screws and clips
would be relatively easy to access with a small screwdriver
once the battery holder was removed. Still, the battery
holder – a separate and quite-complex plastic moulding –
could only be removed once the power connections to the
PCB were de-soldered.
These connections were actually extensions of the battery spring connectors, and they were press-fitted into the
plastic holder. I had to be careful not to go too heavy on
the heat and melt them out of the housing! Some deft soldering iron work and pump/wick application soon had
the leads out and clear; the holder assembly could then
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July 2022 87
be unscrewed and unclipped from the PCB.
Now I had better access to the PCB screws and could take
that away from the case shell. This gave me direct access
to the switch. I was hoping it was the switch because, if
not, there would likely be little more I could do with it.
As is typical, there are no circuits or schematics available anywhere for these cameras and, even if I did have
one, troubleshooting something with this many tiny SMDs
is no fun at all.
The other thing I had to consider is that a very similar – if not better – camera is available from my favourite
online shopping site for under a hundred bucks. So any
fix on this would have to be pretty easy and inexpensive
to make it even worth repairing. Partly out of curiosity
(and the Serviceman’s Curse, obviously), I wanted to see
if I could get it working.
The switch is a reasonably standard-looking triple-pole,
triple-throw sliding type. As is becoming more usual, the
metal outside case is soldered to pads on the PCB, along
with the six soldered pins. Taking mounted components
like this off a PCB can be a chore, especially on multilayer boards.
That is, unless you don’t want them any longer, in
which case just cutting off what we can with a Dremel or
good side-cutters is the easiest way. Then it is just a matter of extracting the cut-off legs and whatever else remains
behind.
Rudimentary tests in-circuit weren’t that conclusive as
to whether it was making the right contacts or not, so I
decided just to cut the switch away and replace it with an
identical one. I have boxes full of new-old-stock switches
but nothing (of course) with the same dimensions and
pinout as the one I removed, so I hit the usual electronics
suppliers to see what they had.
Anyone who has used those
websites knows it can
be tricky to find what
we want among the
gazillions of possible
options. The use of specific search parameters is
essential, but it can still
take time to wade through
the results. I eventually
found one identical in every
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respect. While not expensive, there was a minimum order
amount, so I usually try to find some small hand tools to
top up the order amount.
It’s a tough job, but someone has to do it!
The switch arrived a few days later, and fitting it was
much easier than removing the old one! I temporarily
reassembled the board and battery holder on the bench
and powered it up. I’d like to report that I had fixed the
problem, but I’d be lying. It did precisely the same thing
as before. Oh well; that wasn’t the first time I’d been well
wide of the mark. On to plan B, then.
The SD card slot is the only other part that gets accessed
from the outside of the case, besides the battery holder and
on/off switch. While modern versions of these cameras use
MicroSD cards (which can be found up to 2TB [yes, that’s
2000GB] these days!), older cameras like this one utilise
the older and considerably physically-bigger SD cards.
They are still viable; many laptops come with card readers that can accept this type of media. The customer had
a 16GB card in this one and swapped it out with another
identical card when he went to service the camera every
week or so. That meant the cards got a fair bit of use, as
did the card socket inside the camera.
I tried using one of my own cards. While most cameras
can accept Windows/FAT32-formatted cards, for whatever
reason, they typically recommend that any ‘new’ card be
formatted by the camera itself.
As I couldn’t get to the display, I couldn’t format it, and
as his card worked fine via a card-reader on my workshop
computer, I made the educated guess that it was likely OK.
The user manual states that if a card is faulty, everything
will power on, but a ‘card error’ message is displayed.
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Doing some micro-surgery
Taking all that into
account, I turned my
attention to the socket
itself. As I mentioned earlier, the camera’s interior
was pristine, and nothing
was floating around inside it,
but I put the board under the
scope anyway for a look.
The soldering was not bad
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overall, but a few spots looked dodgy up close. A quick
going over soon had those looking better. I paid particular attention around the SD socket, as several of the pins
looked a bit light on solder as well. And if I flexed the socket
slightly, one pin, in particular, appeared to be lifting away
from the solder pad.
It was difficult to see, even with the microscope, but I
decided to re-do the whole row of solder joints as a precaution. Pushing the media in and taking it out puts a fair
amount of stress on those joints and, unlike the switch
body, the flimsy metal frame of this connector was not well-
soldered to the board, with just a couple of tiny tabs on
either side of the socket near the pins anchoring it down.
Many SD connectors are (by design) very lightweight
and made to fit in very tight places. Given that one has to
‘push to click’ the media in, then push again to remove it,
it stands to reason that some wear and tear is inevitable.
I gave each pad a decent sweat of flux and solder, and it
looked much better. I couldn’t see anything else evident on
the PCB, so this was as far as I would go with it. I reassembled it properly; if it didn’t work now, at least it would be in
one piece for the customer. Getting the battery holder back
in was a bit of an act, but it was straightforward enough.
I loaded up the batteries and hit the switch to ‘Test’.
Imagine my surprise when the display lit up straight away!
I could surf for files on the media, and I could now adjust
settings and do a walk test, noting the blue LED indicating
the PIRs detecting my presence.
I set the switch to ‘On’ and, after the ‘get away’ period,
did several walk-pasts. I’m not much of a runway fashion
model, but it did result in photos of me appearing on the
card, so I was happy with that. It’s always worth giving a
repair a go; after all, it just might work!
Return of the dilapidated gear
B. P., of Dundathu, Qld is at it again, fixing up someone
else’s discarded gear and getting it to work again. It’s certainly cheaper than buying brand new...
I bought a pair of touch lights at the local tip shop, assuming they wouldn’t be working. The lights are ‘antique style’
and were in reasonably good condition, apart from some
corrosion from age and some of the parts in the shades being
loose. So they had nothing major wrong, appearance-wise.
After bringing them home, I removed the shades, put
3W LED globes in them, plugged one in and touched it.
Nothing happened, so I tried the second one, and it also
did not work. I guess this is why the previous owner had
discarded the lights.
I took the base plates off both lights and opened the black
boxes that house the electronics. The first thing I noticed
was that both lights had two bad electrolytic capacitors
on the circuit boards. I found equivalents in my salvaged
capacitors collection. After that, one light stayed on all the
time while the other light only worked sometimes, after
multiple touches. So there was something else wrong.
I could see that these lights used a BT136-600 Triac
and a TT6061 IC. I thought I would swap over the Triacs
between the two lights to see what would happen. Now
neither light worked, indicating that both components
were faulty in both lights. This was likely caused by the
bad electrolytic capacitors.
As I did not have either component in stock, I ordered
them on eBay. They weren’t available from Australian sellers, so I had to order both parts from China.
Once they arrived, I fitted them and set the lights up
for testing again. Now both lights worked. However, one
feature of the lights did not work correctly with the LED
globes. The first touch is supposed to turn the light on to
a dull setting, but they were obviously designed for incandescents and the LED globes flicker badly.
Touching the light a second time changes it to bright
mode, and the LED globes no longer flicker. Touching the
light again returns the light to dull mode, but there is now
very little flickering. Another touch turns the light off.
So the lights were now working correctly, other than the
problem with using LED globes. The best solution is just
to touch the lamp twice to turn it to bright mode straight
away. There isn’t much difference in brightness with the
LED globes between the two settings anyway.
I was able to screw the bases back onto the lights after
finally completing the repairs. After that, I gave them a good
wipe down with a damp cloth. Because the lights are made
from brass-plated steel, the surface cannot be cleaned too
aggressively; otherwise, it will be further damaged.
The slightly deteriorated look of the lights adds to the
antique appearance. Even though they are modern lights,
they look a lot older than they are, both with the style and
the ‘aged patina’.
Upon opening the base of the touch lights two bad electrolytic capacitors were immediately noticeable.
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July 2022 89
Turning my attention to the shades, I straightened the
bent parts on the brackets, tightened the screws and cleaned
them with a damp cloth. The shades were actually in quite
good condition with all the parts being present and nothing
broken or chipped. Then I refitted the shades and screwed
the decorative nut on firmly.
So for a few dollars for the lights and around $7 in parts
(I bought 10 of each component), I now have two working touch lights. So that’s about $5 each in total. I looked
online to see if I could find the same light, and I found a
similar lamp for $220 for just one!
It’s handy to be able to fix things that someone else has
thrown away. The fact that these items can be purchased
cheaply at the tip shop means that they can be recycled or
repaired. Not to mention the massive saving compared to
buying new lights.
The fault whisperer
J. W., of Hillarys, WA ran into that strange situation where
he managed to fix a faulty device but isn’t really sure how
he did it. Oh well, a win is a win...
I was talking to a friend who worked as an audio specialist (now retired) at a Perth radio station about all the
equipment he used to work with. He mentioned that he had
a Studer A730 Professional CD player that had not worked
for a couple of years and asked if I could try to get it going
again. I told him I would take a look at it, so it ended up in
my workshop with the complete service manual.
Upon powering it up, there were no signs of life on the
front panel and a strange clicking noise emanating from
within. It seemed like a power supply problem to me. I
removed the six screws holding the front panel, although
one was difficult and had to be drilled out. I was then presented with the main board with approximately 60 ICs,
including two microprocessors.
With the front panel moved out of the way, I could hear
that the noise was not coming from the CD mechanism
but seemed to be a relay trying to operate at the rear of the
main board.
I checked the service manual and found there should
be four power supply rails: +5V, -5V, +12V and -15V. The
latter three were produced using LM317 and LM337 linear regulators and tested OK. An L296 switching regulator
generated the +5V supply, but the output only measured
about 0.4V. I downloaded the data sheet for the L296 and
found that the current was set to be limited to about 4A.
With my CRO connected to the +5V line, I found that it
was trying to start but being shut down by its over-current
protection. I disconnected the front panel and audio output
boards but found the +5V was still not present.
I then removed the main board from the case and made
a cable for the secondary of the power transformer, so that
An exterior (left) and interior (right) shot of the Studer A730 CD player.
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I could run it away from the case where the mains transformer was situated.
Now I could move the board around and give it a good
visual inspection; nothing seemed to be getting hot or
looked damaged. I manipulated the board and then tapped
around with a probe, producing no change in the situation.
I decided to start trying to isolate sections of the main board
and see if the +5V would come to life.
After cutting several tracks to no avail, I discovered that
the board was multi-layered with a least one copper plane
not accessible, so I could not isolate any more sections. I
decided to remove the output inductor from the switching
regulator and use my high-current linear power supply to
replace the +5V supply. This way, I might be able to produce
some evidence of overheating from the faulty component.
I set my supply to 5V and 4A and powered up the player
and my supply. The current hit its limit at the 4A setting,
delivering about 2.5V. I then started to feel each component to see if it was getting hot. While doing that, its output voltage increased to 4.1V, with the current still at 4A.
A short time later, I noticed that the voltage had gone
up to 5V and the current had dropped to 900mA, so the
overload had cleared. I then tried to bring the fault back
by tapping each component and flexing the board, but it
did not fail again. Had the problem disappeared entirely,
or was it intermittent?
I reconnected the original power and was greeted with
a steady 5.1V. After connecting the front panel and audio
boards back up, I powered the player up again and was
greeted with NO DISC showing on the front panel display. I inserted a CD and pressed play; the player was now
working properly.
I let it run for a few days before ringing my friend to
tell him the news. Two days later, I walked into the workshop to find smoke streaming from the back of the player,
although the CD was still playing.
I turned it off and lifted the front panel to find the mains
filter and switch assembly was quite hot, but the mains
transformer was not. I removed the mains filter and noticed
some smelly liquid coming from the power switch. It looked
like the mains suppression circuit had failed.
I ordered a replacement unit and connected the mains
transformer to a spare power cord so I could let the system
run again. The player ran flawlessly until the replacement
mains filter arrived. I fitted that and screwed the front panel
back in place. After letting it run for another few days, I
rang my friend.
He was delighted and told me he thought the player was
still worth a few thousand dollars. I saw one on eBay for
€3000 – over $4000! It has been a few months now, and
the player is still working fine. I never found out what had
caused the +5V line to be overloaded. Perhaps it was some
sort of ‘tin whisker’ that burned away when I applied 4A
continuously.
Follow-up to the Clenergy 1.5kW solar inverter
R. S., of Figtree Pocket, Qld has a follow-up to the Clenergy 1.5kW solar inverter repair storage that we published
on page 101 of the May 2021 issue (siliconchip.au/Article/
14862)...
The “Ground I Fault” message is caused by drift in the
Hall Effect based current sensor, which monitors any current difference (caused by faulty panel insulation) between
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July 2022 91
The exterior and interior of the motor controller are shown above, while the underside of the replacement motor
controller is shown below. It worked fine for a few weeks, but then blew up, fusing one of the tracks (marked in red).
the inverter AC output Active and Neutral lines. The sensor is in the bottom-left corner of the inverter and looks
like a toroid.
There is more than one version of this sensor. The later
versions are more stable, so the newer inverters do not
have this fault. There does not seem to be an easy way to
adjust for the drift. It might be that the only way to fix an
inverter giving this message is to replace that sensor with
the latest version.
Repairing a lathe’s motor speed controller
While repairing a motor speed controller, D. S., of Maryborough, Qld discovered a horribly flawed design. Had the
controller not failed, it might have been a lethal hazard...
B. P.’s repair in the November 2021 Serviceman’s Log
column reminded me of a service call I made to a local
woodcarver. He called me and said that his wood lathe had
gone bang. Being a mains-powered lathe, I advised him to
switch off the power and wait for me to get there.
When I checked out the lathe, nothing seemed amiss –
no damaged wiring, no burn marks on the motors or any
other signs of a problem.
I switched the power back on and re-checked the lathe.
The spindle motor worked correctly, as did the speed
controller for it. However, this lathe has a small secondary motor. It is much smaller than the main spindle motor
and has a small drill chuck fitted to the end. This auxiliary
motor can be used to carve various patterns into the spinning workpiece by adjusting speeds and the cutting bit.
This motor did not work at all. There were no voltages
present anywhere.
I had to remove the top shield over the main motor controls to access the smaller motor controls. This smaller
motor is an add-on and was modified to fit the existing lathe.
But it seems that its speed controller decided to die a couple of weeks earlier, after giving several years loyal service.
The owner decided that he would find a replacement
controller on eBay. He did find one and at a fraction of
the cost of the original. As the replacement unit had the
same connections as the previous one, he fitted himself. It
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worked fine for a couple of weeks, then boom!
This damage was actually a godsend. As you can see
from the photo of the underside, one of the mains tracks
intersects a mounting hole that has a metal screw going
through it and the metal shield around the whole thing.
The separation is so minimal that the vibration of normal
work eventually caused the track to short against the shield,
causing the track to vaporise.
Neither of the onboard fuses blew, and the safety switch
for the workshop did not trip off. I checked the Earth circuit from the lathe to the power board and found it safe,
and a quick safety switch check revealed a normal trip
current of 30mA. So at least the proximity of that track to
the shield would not have caused the frame of the lathe to
become live, although I don’t know why the safety switch
did not trip.
I replaced this unsafe device with a new controller made
in Australia. Although a bit more expensive, it is a lot safer.
Please be very careful buying mains-powered items from
eBay. Cheap units are flooding the market, and a considerable number of them are simply not safe! If you have any
SC
doubts, please consult a licensed electrician.
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