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SERVICEMAN’S LOG
The oven with a mind of its own
Dave Thompson
I’m probably not the only one among us who finds modern appliances
failing relatively quickly so annoying, especially as it always seems to
happen just outside the factory warranty. Some often joke that they must
put a timer in there!
Appliances can be a significant
investment, and when compared to
the whitegoods of old, they seem to
reach their end-of-life very quickly.
The term “planned obsolescence”
comes to mind.
My mother used a well-known
branded mixer every weekend for
nearly 40 years before it needed replacing. Admittedly, it had a new armature
fitted after 30 years (by dad) to keep
it going, but the mixer she shelled out
good money for, as a replacement,
lasted just six years, and was deemed
‘unrepairable’ by the service people.
There is a tendency to think that
because modern equipment is far more
‘feature rich’ (read: complicated) that
it is more likely to fail, but that only
explains a fraction of the problem. A
lack of replacement parts and the high
repair cost, even if you can source the
parts, is another bugbear.
This time, it’s personal
When we bought our current house
six years ago, we renovated the kitchen
(among other spaces) and installed a
Samsung wall oven. We’d had a previous model in our old place for several years and liked it a lot, so it was
a natural step to upgrade to the newer
version here.
It’s a very good oven; it even has a
feature so you can put a heat-shield
divider in it and cook a roast on the
bottom and a cake on top, but why
you’d want a chocolate-flavoured lamb
roast and a lamb-flavoured chocolate
cake is beyond me!
The controls were also ‘upgraded’,
and not for the better (in my opinion).
Of course, we only realised that once
we had unpacked and installed it.
For example: on the old model, the
various touch functions were backlit,
so in dimmer light, you could see what
you were doing. On the new one, they
rely on a dull graphic printed on the
glass touch panel, and unless you are
in good light, they are practically invisible. Why the designers thought that
was an improvement is beyond my pay
grade [it sounds like it was designed
by accountants – Editor].
One of the most commonly-used
controls on our oven is the timer function, which is initiated by pressing a
bell icon on the aforementioned touch
area, then by tweaking one of the two
very modern push-in, pop-out infinity knobs to dial in the desired time.
Then you either wait for a few seconds
for it to automatically set that time, or
press the almost-invisible timer button again.
To set it, I usually just fish around
on the panel in the general area of the
timer touch button until I hear the
beep and see the timer display show; I
then set the knob to my time and walk
away. Of course, turning off the timer
alarm when it starts harping on at me
is another fishing expedition if the
light in the kitchen is not that great.
I’m used to it enough now that I usually hit it every time, but I still think it
is a bad ‘feature’ and a step backwards.
One thing we do like is the oven’s
ability to self-clean using what they
call a ‘pyrolytic’ system. While this
might invoke thoughts of robotic
hands moving all about the inside
and leaving things sparkling clean, the
reality is that it is a far cruder system.
What it basically does is lock the
door and pump the temperature to a
ridiculous degree (har!). This turns
anything inside the oven to a fine ash,
including any burnt-on grime and
Items Covered This Month
•
•
•
•
An oven with a mind of its own
Testing lifeboat sets
Repairing a bricked NAS
A not so fusey MPPT controller
Dave Thompson runs PC Anytime in
Christchurch, NZ.
Website: www.pcanytime.co.nz
Email: dave<at>pcanytime.co.nz
siliconchip.com.au
Australia's electronics magazine
March 2022 61
grease. Obviously, this can be a problem if you forget to take out the roast,
or any cookware that might disintegrate above 400°C.
But it does seem to work well
enough, and it is easy enough to wipe
the ash out afterwards with a damp
rag (once the oven has cooled down,
of course). The rub is this can only be
done around 30 times in the entire
life of the oven, as it places a lot of
stress on the oven’s components and
seals, so we have to mete out cleaning
as-needed with an eye on the longevity of the appliance.
The soup thickens
So, besides these gripes, for the last
six years it has been going well. That is,
until a few weeks ago when I walked
past and the LED display was flashing
randomly between the different program settings. I touched the left-hand
knob (which controls these things) and
it suddenly went quiet again.
I was a bit perturbed, but after giving
the knob a good back-and-forth tweaking and nothing untoward happening,
I thought it must be just the pot or
encoder inside getting a bit dirty (I’ll
call them pots for simplicity; they’re
sealed so I don’t know what mechanism is inside).
However, one night we were sitting enthralled in the latest streaming
drama on the box when I heard pinging from the kitchen. Once again, the
display was going crazy but this time
we had sound to go with it. And again,
merely touching the settings control
stopped the graphics and noise.
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There was obviously something
going on with the pot or something
else in the control board. And what’s
worse is a few days later, I walked
past again and noticed the oven was
on. I was pretty sure the wife hadn’t
switched it on for anything and I certainly hadn’t, so it was time to do
something about this.
The biggest problem with wall ovens
is that they live in a hole in the wall,
and access to the internals is not great
until they are removed. I probably
could have hefted the thing out myself,
but I’m getting too long in the tooth for
those sorts of shenanigans, so I asked
a friend over for lunch.
This was the guy who initially
helped us renovate this place, and I
Australia's electronics magazine
bribed him with a nice meal so I could
make use of his muscles. With the
retaining screws removed, it was easy
enough for us both to manhandle the
thing out and onto a piece of carpet
I’d put on the kitchen floor.
It has a nice long cable, which plugs
via the usual wall switch arrangement
into the grid and that had been coiled
up behind and just came out with it.
Once on the floor, it was just a matter of removing a few chassis screws
to remove the outer shell and reveal
the internals (after making sure the
wall switch was off, obviously). This
gave me access to remove the panel
that held the control PCBs.
Everything on this oven is handled
by four printed circuit boards mounted
internally at the top of the oven cavity;
the main PCB that appears to manage
all the heavy-duty power switching
functions is away from the rest, with
the three smaller ones immediately
behind the front control panel. It was
those three that I was going for first.
The manual controls – the two joggling infinity pots mounted on either
side of the oven’s control panel –
boasted a small circuit board of their
own at the rear, and then one larger
board housed all the touchscreen buttons and displays that we could see
through the front glass bezel. These
were mounted directly to the panel.
I removed the entire front panel easily after finding the three screws that
held it on, unplugging a ribbon connector that runs off to the main board,
and sliding it forward out of the chassis. There were many more screws
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holding the various PCBs to the front
panel but once taken out, the boards
just lifted clear.
My goal here was just to have a good
look and possibly squirt some contact
cleaner about, or look for and repair
obviously dodgy solder joints before
calling in someone more specialised in
oven repair. It’s the Serviceman’s Curse!
Even though well-isolated heat-wise
from the rest of the oven, these boards
live in an inhospitable environment.
Wall ovens (especially) heat right
through every time they are used for an
extended period, so the effects of constant heating and cooling must have
an impact on the boards and various
solder and plug/socket joints.
There are several fans and ducts to
keep the heat away from the electronics, but it still must have an effect, and
that’s what I started looking for.
Everything was surprisingly clean
inside; I was expecting greasy residue and other rubbish, but it looked
pretty good. All the boards seemed in
good nick. It looked increasingly like
this was all a waste of time, and a bit
overly ambitious of me to think I could
do something with it. I reassembled the
boards to the front panel, and we sat
back and had a coffee before we put
the oven back into the wall.
Once the caffeine hit, I considered
that one thing I could look at was the
mechanical parts of the control pot. On
these model ovens, the whole ‘knob’ at
the front can be pushed into the panel
– clicking into place – to get them out
of the way and give that modern, sleek
stainless look (and apparently make it
easier to keep clean).
When needed, a simple push
inwards pops the knob out, and it can
then be joggled to whatever program is
required. In practice, we almost never
pop them in and just leave them looking like regular control knobs. Perhaps
there was something physically there
that was affecting things.
This one certainly gets way more
use than the one on the right side, but
as I was already clutching at straws, I
decided to disassemble this left-hand
one and have a look at it. Mechanically, it is pretty simple: the mechanism for hiding the knob is similar to
many push-on/push-off switches we
are already familiar with and it works
much the same way.
Except this is the whole knob assembly that can move in and out, and a
sliding shaft allows it to operate in
siliconchip.com.au
either the closed or open position.
While it can be turned awkwardly
closed, it is designed to be operated
in the open position.
The motion felt smooth, but a little
different to the right-hand knob – and
in any service situation, it is always
good to have a second working component to compare to the suspect one.
These knobs also sit in the line of
fire; that is, when the oven is up to
temperature or something is cooking
in there, opening the door exposes the
exterior bottom section of the control
panel to waves of intense heat and
potentially other fumes, steams and
smoke – especially the way I tend to
cook things.
I thought that the control panel
could do with a good clean, so I
pulled the knobs off, used a spanner
to undo the shaft nuts, pulled the pots,
removed the display circuit boards and
disassembled the whole shebang down
to metal parts.
It’s all stainless and glass, so I threw
it all through a quick wash in the dishwasher. While that was processing, I
used isopropyl alcohol and soft rags to
wipe everything else down and clear
the grime out of the nooks and crannies (which are naturally created by
these pop-in knobs).
I also cleaned the pots and whatever
other contacts I could see with contact
cleaner while it was all out, and then
Australia's electronics magazine
once the metalwork was finished, I put
it all back together.
I had to bribe my friend with another
lunch so he could help me wrangle the
thing back into the wall; it all went
without a hitch. It hasn’t faulted again
… yet, but I fully expect that what I
did didn’t do much, and this run won’t
last long.
If I do need to buy a new control or
board for it, apparently there are parts
available to order – cost unknown – but
it irks me that something this ‘young’
would fault at all, considering the purchase price. Time will tell.
Leftovers
Another trying job through the
workshop recently was an amplifier
module – one built by a friend from a
design from the ‘80s or ‘90s. It looked
like one that I’d seen featured in the
likes of Electronics Australia, or perhaps even Silicon Chip, but I couldn’t
find a matching project for it in those
archives.
It had never worked. It came with
its own power supply in a case, so I
isolated the amplifier board and tested
the PSU first; as per the owner’s comments, it did indeed work. The line
and output fuses were all good, but
after rigging it up on the bench and
connecting it to my workshop speakers, there was just no signal getting
from the input to the output.
March 2022 63
All the soldering looked pretty good,
and the owner said he had the original documentation that came with the
project somewhere if required. Still, I
couldn’t see any obvious component
misplacements due to the board overlay or anything else really obvious. I’d
have to dig deeper.
The output transistors are a good
place to start because sometimes one
or more can just give up if things don’t
go well, so I pulled them one by one
and tested them out. All were fine.
There were also a couple of homewound inductors on the circuit board,
and I wondered if the problem could
lie with them.
I also pulled them from the board
and went to measure them, but I
couldn’t get a reading on my LCR
meter. And I noticed that the solder
that had been holding the inductors
to the boards was also just falling off
the legs as I tried to get test leads on.
I soon clicked to the problem; the
enamel coating had not been stripped
off the wire sufficiently before the
inductors were soldered into the
board. How he’d even managed to get
any solder to stick was beyond me.
I’m sure the documentation that
came with the kit clearly stated he had
to strip the coating off the copper wire,
but I guess he either skipped that part
or thought he’d done it using just the
soldering iron.
This is not the way to do it; that
enamel coating is quite tough and
while I’ve seen people burn it off – with
varying success – on smaller wires with
lighters or those wee gas torches, it is
far better to do it the old-fashioned way
with a craft knife and manual labour.
I cleaned off the wire ends, used
some liquid solder flux and tinned
them properly before reapplying
them back into the board. I had a second check for any other dry joints but
found none, so I reassembled everything back together and applied power.
Now I got a good signal through the
amp and, after a few minor tweaks,
it was ready to go back to a grateful
owner.
It just shows that the smallest bad
joint can cause an entire project to be
a paperweight.
Testing lifeboat sets
R. C., of Mooroopna, Vic had a frustrating day trying to find a working
emergency radio for a lifeboat. It seems
that they were not well designed...
Back in the 1970s, I was a Commonwealth of Australia Marine Radio
Surveyor. The purpose of radio surveyors is to make sure that all the
radio equipment onboard ships, from
small to as big as they get, was in good
order to maintain communications in
an emergency. For example, if a ship
starts sinking, its emergency communications equipment must function
properly.
This is a story about a string of faulty
lifeboat sets. I was called to the Port
of Melbourne to test the equipment on
board a tug that was to sail from Melbourne to Sydney. It required a onetrip authorisation certificate, indicating that all the radio equipment was
fully functional. Other surveyors dealt
with other aspects of the ship like the
hull, machinery etc.
I tested all the radio equipment,
and the only item left to test was
the lifeboat set. These operated on
500kHz MCW, 2182kHz AM voice and
8364kHz. They were powered using
pedals or hand-cranks, and when
stowed, they would float. I tested the
set, a Clifford and Snell RN610, and
found it was not working as the wave
change switch was damaged.
As there was a small fleet of tugs
in Melbourne, I asked if there was
another lifeboat set, and they replied
yes, and obtained it. I tested this one,
and it also failed with a faulty transistor. I asked if there were any other
sets, so another was obtained, and it
also failed. They got another one, and it
also failed, each with a different fault.
Having had four sets in a row fail
with different faults, you begin to wonder if you are doing something wrong.
Things were getting desperate, as the
tug could not sail unless I gave the
Servicing Stories Wanted
Do you have any good servicing stories that you would like to share in The Serviceman
column? If so, why not send those stories in to us?
We pay for all contributions published but please note that your material must be
original. Send your contribution by email to: editor<at>siliconchip.com.au
Please be sure to include your full name and address details.
64
Silicon Chip
Australia's electronics magazine
all-clear that all radio gear was working correctly. The cost of preventing a
ship from sailing is high; it was into the
thousands even then. You did everything you could to make sure a vessel
was not held up.
I asked if they had a Solas III lifeboat set, and they replied that they did.
That one worked! I had always found
this type of set worked well. The faulty
sets were repaired later by shore service as the tugs were telephony-only
ships, with no dedicated radio officer.
The Clifford and Snell RN610 was a
compact set – too compact, as the top
cover was shallow, and it was difficult to get headphones etc in the top
cover above the operating controls of
the set. This meant that the large wave
change switch often had pressure on
it, damaging the switch and causing
other problems.
After I moved on from the surveying
work, the following surveyor tested the
ability of one of the sets to float (they
are meant to). It didn’t and continued
to the bottom of the Yarra River. That
caused a stir.
A significant percentage of the troubles with these sets was because the
top waterproof cover of the set was so
small/shallow that you had difficulty
getting the two sections together to
make a watertight seal. If you did get
it to seal, was the wave change switch
damaged in the process?
I often wondered how this particular model set obtained authorisation/
approval under the Safety of Life At
Sea (SOLAS) Convention for use on
ships, considering how often they
were found to be faulty.
The case of the bricked NAS
K. R., of Auckland, New Zealand
knows the saying, “if you don’t have
backups, you will be sorry”. He didn’t
want to be sorry, so he set up a backup
system, but it broke and then he had
to fix it back up...
About ten years ago, I realised that
our home PC had become the de facto
family photo album as digital camera
images replaced film. Worrying stories
of people losing these family memories because of hard disk failure were
becoming commonplace. The ever-
increasing pixel count and decreasing
price of digital cameras added to the
problem as our media storage needs
increased exponentially.
Additionally, more and more businesses are emailing invoices and
siliconchip.com.au
statements, so the PC is also becoming
our bill filing system. Then there is that
gigantic email archive. With 100GB,
including 70GB of photos and growing fast, it was time to put a backup
system in place.
I was satisfied to add another HDD
inside the PC and copy the files across
for a while. But what if the PC suffered
a serious power incident that fried
everything inside it, or it was stolen?
My next step was to connect an
external USB HDD to run a backup
each month so that the backup data
was in two places, but these backups
ended up being done at somewhat
irregular intervals, often three months
or more. I decided that we needed a
separate appliance that could be kept
out of sight in a more secure location, like a Network Attached Storage
device (NAS).
I selected a Taurus brand enclosure
with a gigabit Ethernet interface and
fitted two 1TB HDDs running in RAID
1 (RAID = Redundant Array of Inexpensive Disks). RAID 1 mode allows
one of the two drives to fail without
losing any data by ‘mirroring’ the data
across both drives.
I was now able to schedule backups
of the important data each day, and
once a week, I backed up the operating system for good measure. Even
when compressed to about 100GB, my
150GB of data took about two hours to
transfer over gigabit.
All was well for several years, and I
had to use the backups when upgrading hard drives in the PC and even
fully recovered the operating system
after the motherboard failed and was
replaced under warranty. Annoying
as this failure was, it was a pleasant
change to have the failure occur just
within the warranty period instead of
shortly after it expired.
Just as the proof of a pudding is in
the eating, the proof of the backup
is when it is restored. So I was well
pleased when it worked as designed.
Then, the scheduled backups started
intermittently failing for no apparent reason. Power cycling the Taurus NAS would usually fix it, a clue
I ignored completely. When the failures became annoyingly frequent, I
searched the Taurus NAS website for
updated firmware as my first step in
troubleshooting.
I downloaded the latest version of
firmware and then double-checked the
process to load it. It was a good thing
that I checked because I had downloaded the wrong version. After finding the correct firmware, I started the
upgrade, which went just as expected.
Once completed, I navigated to the
NAS web interface to find a slightly
different menu, and there was no longer an option to set the RAID mode.
A frantic check revealed I had managed to delete the correct firmware
and uploaded the incorrect firmware
instead, designed for a cheaper version
with a single HDD! Oh well, no matter, simply download the correct firmware again and reload, right? Wrong!
The latest firmware has version check
software built-in, and it helpfully
refused to allow me to load what it
now thought was the wrong firmware.
Where was this version checking feature when I needed it?
Google helped me find the original earlier version of firmware, but it
would not allow that to load either;
the computer still said “No”. The
NAS worked fine; it just would not
recognise the second HDD for RAID
operation.
Every cloud has a silver lining,
and with the NAS opened up on the
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siliconchip.com.au
Australia's electronics magazine
March 2022 65
“workbench” (dining table), I realised that the intermittent failure I was trying to fix was actually caused by the
HDDs not spinning up every time. A multimeter revealed
the 5V rail was spot on, but the 12V rail was about 9V –
the power supply was failing.
This was four years after I bought it, but I called in at
the supplier Digizone and, bless their after-sales service,
they replaced the power supply without question or evidence of purchase. When I explained the firmware mess
I was in, they said it would need to be returned to China
to be re-flashed. I got the feeling their tech had made a
similar firmware error at some stage; he was extremely
helpful and even offered me a loan NAS if I needed it to
recover any data from my HDDs.
Now that I had resolved the intermittent problem, I was
more determined than ever to fix the firmware myself.
I found a reference to the firmware version inside the
“imageinfo.ini” file. Using Notepad, I cunningly changed
this reference to the correct firmware description and tried
again to upload the RAID capable firmware. Not so simple
apparently; again, the computer said “No”.
Back to Google, and I found a set of instructions on how
to ‘unbrick’ the Taurus NAS by connecting a serial data
cable to some solder pads on the circuit board. I soon soldered a donor serial data cable in place (Rx, Tx, Power,
GND) and installed PuTTy on my PC. You have to admire
the determined person who reverse engineered these factory connections.
I set the serial port to 19200 baud but cold-booting the
NAS with the serial cable connected generated a meaningless stream of green ASCII characters in the PuTTy
window, like a sequence from the movie “The Matrix”.
It looked like a voltage compatibility problem, so back
to Google, where I found an amazingly simple 5V TTL to
RS232 converter that used just two FETs and two resistors.
A trip to Jaycar, and $3 later, I had it built on a breadboard
and tried again. Success! The now perfectly-readable boot
sequence could be interrupted with an old-
fashioned
Ctrl-C to present a Linux boot loader menu.
Using the TFTP option (Trivial File Transfer Protocol)
and tftp32 freeware software on the PC, I was finally able
to upload the correct version firmware files, and the NAS
rebooted, as good as new.
Learning how to use PuTTy and tftp32 was an exercise in itself, but the reward of fixing the NAS was huge,
especially when I caused the problem in the first place.
I put in place a truly paranoid backup methodology of
daily backups to a separate HDD inside the PC, weekly
backups to the Taurus NAS and, just for good measure
each month or so, I back up to a portable 1TB HDD that
I leave at the office. I can backup gigabytes of data to the
cloud, but I still use the NAS just in case.
A not so fusey MPPT controller
S. L., of Whitfield, Cairns had been ‘gifted’ a dead MPPT
controller. Despite it giving him the cold shoulder, he
went on his way to having it work again...
Several companies make almost identical blue coloured
MPPT controllers: Victron, Fangpusun and HanFong, to
name some popular ones. Recently, I was given a dead
Fangpusun MPPT 100/50 unit to experiment with.
Editor’s note: the others are ‘clones’ of the Victron units;
our experience is that Victron make quality devices, and
we bet that the clones will last nowhere near as long.
These units are not designed to be repaired. They have
an epoxy solution in the lid when it is attached during
manufacture. This epoxy binds to the top of several electronic components, making it impossible to remove the lid
without destroying components. (“No serviceable parts
inside” – yeah, right. It’s full of serviceable parts; you just
can’t get to them!).
This faulty unit had no output, and the documentation talks about a non-user-replaceable fuse that protects
against reverse-polarity battery connection.
On a good working unit, a multimeter will show a
reverse polarity diode across the battery connection. On
this faulty unit, the battery connection tested open-circuit,
indicating the battery had been connected incorrectly,
and the reverse polarity diode had done its job by blowing the fuse. Because there is no way to access this fuse,
the unit is deemed a throw-away item.
After some checking, I carefully cut away a small part
A small part of the MPPT controller’s
lid was cut away to access a normally
“non-user-replaceable” fuse. This fuse
was open-circuit; it was bridged and
the unit now uses an external battery
fuse.
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Australia's electronics magazine
siliconchip.com.au
of the lid with a Dremel to expose the fuse. It was open-
circuit as expected, and rated at 250V AC 80A for this
50A controller. I bridged the fuse with solder and wire,
and the unit is now fully functional. It now requires an
external battery fuse for protection.
These units automatically detect a 12V or 24V battery
and are further configured with a plug-in switch that
allows eight different operational modes to be set, to
cater for different battery types. These settings are in the
user manual, available on the internet. The absorption,
equalise and float settings are different for each mode.
This programming switch plugs into a 4-pin RS232 connector on the unit. The RS232 pinouts are 1: GND, 2: RX,
3: TX and 4: Vcc (5V).
A cable can be easily made up for communications with
a laptop. An RS232-to-USB TTL serial converter module is
required. The TX, RX and GND pins from the serial module can then be wired straight to the MPPT controller port.
To test the cable, use PuTTy (a serial communications program) by selecting the “Serial” button, changing the “Serial Line” to the COM port number assigned
to the device, changing the “Speed” to 19200 and clicking “Open”.
You should get about 20 lines of data, repeating every
second, showing the status of the MPPT controller.
To experiment further with this Fangpusun unit, I downloaded the free “VictronConnect” software from www.
victronenergy.com/support-and-downloads/software
After installing the software and connecting the homemade interface cable, the “VictronConnect” software
talked perfectly to the Fangpusun unit.
The first thing it did was advise that the firmware needed
to be updated, which I allowed, and the latest Victron
firmware was loaded into the Fangpusun unit.
The unit then rebooted, and I had access to a lot of historical data, and could modify many settings. Now the
absorption, float and equalise settings are all individually adjustable, as well as things like the solar and battery maximum current.
The unit retains the last 30 working days of data in history. This is not the last 30 calendar days, but the last 30
days when it was producing power.
The only thing left for me to do was glue the piece of
the lid that I cut out back on, and I had a fully functional
SC
MPPT controller.
After dealing with the fuse, the unit was tested with the
VictronConnect software.
siliconchip.com.au
Australia's electronics magazine
March 2022 67
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