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SERVICEMAN’S LOG
Toys with a serious purpose
Dave Thompson
You might think I’m running out of things to repair because I’m working
on toys again. But actually, while this device appears to be made of child’s
toys, it has a serious medical use. It is used to check the hearing of young
children who can’t yet talk (or don’t like to) but this particular example
didn’t survive the tender mercies of one particular delivery service...
It will come as no surprise to many that I sometimes get
weird and wonderful devices through my humble workshop. Word somehow leaks out through the concrete-jungle
telegraph that I am willing to look at anything, always with
a view to (hopefully) repair it.
A few weeks ago, a long-time Silicon Chip reader from
another part of the country contacted me about a device
he had designed and built many moons ago that needed
some electronics-based love and attention.
Darryl was an audiologist in one chapter of his life, and
as an electronics enthusiast, he had designed and built
several VRA (visual reinforcement audiometry) devices
to assist with testing very young children’s hearing. The
usual traditional tone-testing we all know as adults is not
so easily performed on toddlers.
These so-called ‘puppet boxes’ are utilised as an audio-
visual testing aid. In this case, the ‘box’ itself is in the form
of a large, round, carpet-covered timber tube about 1.8m
high and 50cm in diameter. The front ‘face’ of the tube
is covered by a dark Perspex cover almost to the bottom,
where there is a panel covering the electronics.
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There are three levels to this box, all isolated and separated from each other. In each of the levels is a different
animatronic ‘toy’ which, when activated, is illuminated
by an LED spotlight in the top-left corner of that section.
A hand controller – a jiffy-type box with three press-tomake, release-to-break switches on a long lead activates
each of the toys.
The ant, the gorilla and the elephant
In this box, starting in the top section, is a large ant in
a forest-type setting. He speaks a phrase and his bug-eyes
move and blink when the appropriate button on the hand
controller is pressed. The animation and light activates for
about 15 seconds before going dark again.
The middle level contains a furry gorilla toy, set in a
yachting scene; this toy dances and his mouth opens and
closes along (roughly) to a popular 90s novelty song.
The bottom section has a pink plush elephant, which
animates with its legs moving in time to a typical child’s
‘crawling song’. In practice, I suppose it doesn’t really
matter what toys are there and what they do; they are just
something to grab the attention of the child.
I was certainly entertained and admit to pressing those
buttons a lot – once I’d fixed it. I now know the lyrics to a
crawling song, so life is full of surprises!
In use, a child being tested is ‘trained’ to respond to
a test tone they hear through headphones by watching
a visual stimulus every time they hear the tone. The
audiologist plays a tone and activates the puppet box at
the same time. The child looks at the animated toy and
‘learns’ that when they hear the tone, they’ll see the toy
light up and move.
As the audiologist changes the tone frequency and the
volume level, they can build a picture of that child’s hearing and diagnose accordingly. It’s a time-honoured method
of testing children’s hearing.
The idea of the puppet box is relatively simple, and the
implementation in this case very clever; I suppose any animated toy could do the job, and all we need is a suitable
power supply, some lights and a timer board to control it
all. The majority of us would likely never see such a thing,
unless we had a very young child in need of having their
hearing tested.
I’ve certainly never seen one before, even though I’ve
had many hearing tests over the years, so all this has been
an education for me.
Australia's electronics magazine
siliconchip.com.au
The VRA in my workshop is a classic example of someone with electronics knowledge and the vision to create
something practical and useful using that knowledge.
These things should have become an industry standard.
They might very well be, for all I know – no doubt some
company makes and sells them for exorbitant amounts of
money. Still, for whatever reason, this box, and several
others like it Darryl made, have stayed a relatively ‘local’
solution to this problem.
Damaged in transit
The problems with this unit started when the puppet
box was shipped from ‘up north’ to ‘down south’. When
it arrived, it no longer worked. According to the people
involved, the packaging showed no signs of trauma, and
the unit was intact, but there was obviously something
quite wrong with it.
The sections lit up with the button press, but the only
toy moving was the elephant. While I got audio from the
others, the ant and the gorilla were not animating at all,
though their LED spot lights did activate.
The recipient of the box got in touch with Darryl and
then he got hold of me. Me being in the same town down
here as the customer likely sweetened the deal. He asked
me if I could take a look at it, rather than ship it all the
way back ‘up north’.
Of course, I said yes, and really, what else could I do?
The chance to work on something new and unique is many
a serviceman’s dream (well, it is mine anyway).
The box arrived at the workshop nicely bound up in a
woollen rug, although that was not the original shipping
material. After unwrapping, it seemed intact and undamaged when viewed from the outside. However, after plugging it in, connecting the hand controller and trying it,
there was obviously something wrong.
The ant and the gorilla toys looked to be sprawled on the
floor of their respective compartments, and there was no
movement at all visible
when the compartment
lights came on. The elephant at the bottom also
looked a bit skewed, but
it did at least have some
music and motion when
the relevant button was
pushed.
The first thing to do
was remove the smoked
black Perspex cover,
exposing the toys. It was
held on with standard
super-screws, countersunk into the plastic.
Some kind of sealant
had been applied around
the bevelled edges of the
screen, perhaps to remove
any sharp machining
edges that might catch a
small hand.
With the screen off, I
could see what was going
on. The ant was meant to
siliconchip.com.au
Items Covered This Month
•
•
•
•
•
Toys with a serious purpose
A Sony tuner with a side of gum
Washing machine and mixer repair
Repairing a Toyota wheelchair lift
Restoring a Porsche 928
Dave Thompson runs PC Anytime in Christchurch, NZ.
Website: www.pcanytime.co.nz
Email: dave<at>pcanytime.co.nz
Cartoonist – Louis Decrevel
Website: loueee.com
be standing upright and be glued to the back of the compartment, while his ‘feet’ were fixed to the timber ‘floor’
of the section to hold it into position. The glue holding it
upright had torn away from the wrap-around cardboard
picture background, so the toy was just folded up headfirst like a rag-doll on the floor.
I unwound him and stood him up and pressed the button. This time, his eyes rolled and blinked and he said
his lines quite happily. A simple fix for this one then;
all I had to do was clean him up and glue his backpack
back into place on the background to secure him in the
right place.
One sick gorilla
The gorilla section was a bit different. He’d come well
adrift and was crumpled onto the floor. He’d been tacked/
glued in three places to hold him upright – all these points
had been torn away, as evidenced by the paper stuck to
the glued areas. The box had evidently suffered quite an
impact – at least enough to knock these guys free.
The gorilla didn’t move at all, so something electrical
had gone wrong. He did, however, emit the opening notes
of that novelty song,
but it sounded like a
stuck record, playing
the same sound-bite
over and over.
A check with Darryl confirmed that
it should play the
whole song for the
allotted time, while
the gorilla would
usually dance and
‘mouth’ the words.
Apparently, something else was amiss
here.
All the toys were
originally battery-
powered. Power for
this box – and the
toys and lights –
was derived from
a battery charger
mounted into the
cavity in the base of
the unit.
Australia's electronics magazine
November 2022 101
Switched permanently to the 6V setting, the charger was
working because all the compartment LED lights activated
on the press of the button. Two of the toys moved, however
weirdly, so the juice was making it through to all but the ape.
The lights and animation were all controlled by a common timer, so they all operated for the same duration. It was
mounted on top of the charger. The ammeter on the charger indicated when the toys were powered – again, except
for the gorilla, which was not surprising as it seemed to be
the most affected by the drop.
The toy was easy enough to remove – one foot was still
glued to the base, so I carefully got a box-cutter style knife
blade in between the glue and card and gently separated
the two. Once free of that, I then had to desolder the power
leads, which went directly to the battery compartment and
were soldered to the contacts there.
With the toy removed, I pressed the button and my trusty
multimeter showed roughly 6V getting to the now-bare
wires, so whatever was wrong was inside the toy.
Fortunately, the manufacturer had installed a zip in the
bottom of the plush, and when opened, this revealed the
internal mechanism. A large torso-shaped plastic clamshell
box was held together with four screws, and with these
removed, the two halves came away easily.
Access was very tight – the plush would only pull back
a limited amount, as a cable tie secured the neck area to
the actuator case. I had to cut and remove that tie to allow
deeper access, and as there were linkages to the arms, the
head and the mouth, I had to be careful I didn’t damage
those.
More damage inside
Inside the actuator was the sound and movement controller module. This was made from two small PCBs joined at
right angles, screwed to the plastic case, with one containing a COB (chip-on-board) IC that likely had the song programmed into it. There were a few other surface-mounted
components which I assumed controlled the animatronics.
The bottom half of the case also contained a reasonably
complex plastic gearbox and an electric motor. The motor
is a typical small DC motor that powers countless toys. Its
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Silicon Chip
leads were adrift, explaining why there was no movement.
I applied a bench power supply at 5V to that motor
directly and sure enough, it fired into action, so that was
the likely problem. A suppressor capacitor was also connected across the motor’s terminals – this had broken away
on one side, so a quick hunt through my spares box had
that replaced and the connections remade and solidly soldered in place.
A press of the button proved the gorilla now jiggled and
animated, but his mouth didn’t move (it should) and that
song was still just a machine-gun-style delivery of one note.
I didn’t think I’d be able to do anything about the lack of
music, but I could look into that gearbox and see why the
mouth didn’t articulate.
After stripping the gearbox assembly from the toy (which
meant pressing a few pin-hinges out), I could see an actuator shaft that should have operated the mouth had snapped
at a join in the neck area. It was a clean break and there
was plenty of meat there for a glue job, so I hunted through
my adhesives collection for some plastic-welding cement.
This material is standard PVC or similar, and a test drop
of glue onto an open area confirmed that it would indeed
weld those bits together. Once glued and held for a few
minutes (nothing seems to go on as long as waiting for glue
to harden), I carefully reassembled the gearbox, motor and
linkages and left it overnight before powering it up.
The next morning, I held the gorilla roughly in place and
pressed the button. Success! He did a little dance, and his
mouth snapped open and closed. The ‘music’ wasn’t happening properly, but Darryl mentioned that as long as there
was some noise, it would suffice for the purpose.
I suppose we could have sourced another toy, or even
grabbed a sound module from a charity shop talking toy,
but a quick look showed that animated toys are really
expensive these days. I learned over the phone that most
donated toys go pretty quickly from the Salvos and Vinnies stores.
Shaving the gorilla (no, really!)
After zipping him back up, I cleaned off as much of the
old hot-melt glue originally used to hold the gorilla in from
his fur coat as I could. I wouldn’t like to have to get this
glue out of a real coat, because it makes a nasty mess! Shaving it partially was the only way to remove the bulk of it.
I used the rest of the glue as a template to fit the limbs
back into their original positions, which were pretty obvious due to the torn-away card. I also used the same glue
to reattach the elephant toy to the bottom, which was a
little askew on its mounts, but still working as intended.
After a bit of tidying up of wire runs and the dog-eared
and torn panoramic picture backgrounds, I was satisfied it
was all working as well as it ever would. Due to the extra
dollops of glue liberally applied to the toys, I’m reasonably
sure they won’t be coming loose again. [I’m sure the post
office would accept your challenge – Editor]. If they do, I
think we’ll have bigger problems!
The only thing left to do was to replace the front cover
and give the box a good workout. As it has been in the
workshop for a couple of weeks, all my visiting customers see it and, of course, ask what it is and how it works.
I pass them the hand controller and everyone seems to
have fun making the toys animate; it makes for a good
conversation piece.
Australia's electronics magazine
siliconchip.com.au
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It would have gone back by now, but the designer and
the customer are talking about modding it for use with foot-
operated switches as well. That would require finding some
single-pole press-to-make, release-to-break stomp-box type
switches (sometimes called momentary switches), some of
which I think Darryl has already sourced.
I initially thought readily-available musicians’ foot
switches would be ideal, as they are designed to be trodden on. However, they are usually quite expensive and are
typically multi-pole, press-to-make, press-to-break types
used for switching effects in and out of the signal chain.
Anyway, with the right switches in hand, it will be a
relatively simple matter of taking off the power supply
cover again and adding another paralleled multi-pin plug
to the existing facia.
As the audiologist may want to have the switches in a
different room to the box (usually, they are in the same
room), we’ll have to find a way to utilise jack panels on
the walls. Still, that’s for another day – at least now, the
box can be returned to normal service and delight kids
of all ages.
One Sony tuner with a side of gum
B. H., of Little Mountain, Qld ran into one of those situations where, while diagnosing a fault, the measurements
didn’t seem to make sense. Luckily, he managed to figure
out the reason for those discrepancies...
I inherited a Sony tuner that played for many years, but
within the span of one week, its FM output diminished
to zero. I thought the most likely culprit was the first RF
transistor. This unit is beautifully made and is of the PLL
type, which was very novel back in 1981. After googling
for many days, I could not find a schematic, so I started
from the beginning.
This unit is not unusual; the RF input stage is followed by
the mixer/oscillator, then a dual transistorised IF stage, followed by an IC that turned out to be the PLL FM IF decoder,
which includes another six stages of IF amplification.
Three ceramic filters are associated with the transistor
amplifiers. However, I couldn’t find a bias voltage at the
base or emitter of either transistor. I also checked the voltages on the connected resistors.
They had used red gum to stop some flying leads from
interfering with the station pointer dial mechanism. This
blob covered a resistor and solder joint.
I removed the red gum to access the resistor, which I
believed to be the bias provider. The resistor had the correct value on the component side, but the solder joint on
the copper side was peculiar. I could measure a positive
Servicing Stories Wanted
Do you have any good servicing stories that you would like
to share in The Serviceman column in SILICON CHIP? If so,
why not send those stories in to us? It doesn’t matter what
the story is about as long as it’s in some way related to the
electronics or electrical industries, to computers or even to
cars and similar.
We pay for all contributions published but please note that
your material must be original. Send your contribution by
email to: editor<at>siliconchip.com.au
Please be sure to include your full name and address details.
104
Silicon Chip
voltage on the resistor lead, but the surrounding solder
tested 0V, suggesting a dry joint.
Re-soldering it made no difference; the pad and resistor wire were still 14V apart. It all looked proper on closer
inspection; the wire was surrounded by solder with the
correct colour. But I could not find any continuity between
the wire and the solder.
I think the gum from the PCB component side must
have corroded the tin coating of the resistor wire all the
way down into the solder joint, isolating the resistor from
the solder. Replacing the resistor with one soldered on the
copper side of the PCB fixed it.
Washing machine and mixer repair
P. M., of Christchurch, New Zealand made three successful repairs on very different pieces of equipment lately...
The first was my washing machine, which has been reliable for more than ten years. Recently, I switched it on and
instead of the usual bright display of LEDs showing the
wash program and time, the LEDs were dull and flashing
slowly. Switching it off and on again didn’t help.
A Google search first turned up some unhelpful suggestions, but then there was one that seemed to be on the right
track. The post mentioned a faulty 10µF 450V electrolytic
capacitor on the main board and that person had found a
replacement at Jaycar.
I was planning to go to Jaycar later that day, so I added
the capacitor to my list. The post also mentioned cutting
a hole through some plastic with a hole saw to get to the
part, which sounded a bit extreme to me at first.
The machine’s top must be removed to get to the main
board. Once away from the wall, after removing a few
screws and some plugs, out comes the main board. The
board sits in a plastic tray filled with clear sealant covering most of the components. The capacitor was visible in
the middle of the board and was obviously faulty as the
top had bulged open.
The problem was that the solder side of the board was
face-down in the plastic tray, and I didn’t want to disturb
the sealant holding it all there. The hole saw was starting
to make sense now, but still seemed a little risky. Instead,
I drilled a series of small holes to make a circle that I could
nibble out to make a hole to access the solder joints of the
capacitor.
I was glad I did this as there were more components on
the solder side of the board, and hitting any of them with
the hole saw would not end well. I could now replace the
capacitor and used silicone sealant to refit the plastic piece
I had removed.
As I was putting it all back together, I remembered the
original poster had said to be careful not to pinch the rubber hose at the back of the machine when refitting the top
cover. This was valuable advice, as when I looked at the
hose, it was indeed pinched under the top. This hose is
part of the water level sensor, and if I had not freed it, the
machine would have overflowed the first time it was used.
Unsurprisingly, when I fired it back up, it was working
correctly again.
Secondly, I repair a lot of analog audio mixers of various
sizes; some of the most common problems are faulty faders. Those slots in the panel for the faders allow ingress of
all manner of dirt and liquid spills. In most of these units,
everything is mounted on one large circuit board, including
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siliconchip.com.au
the faders, so access means removing all the knobs, nuts
and screws to get the board out.
I have found that in many cases, there is sufficient space
at the front edge of the board to wiggle the fader out once
it has been desoldered, and a new one can be refitted the
same way.
The mixer I worked on recently did not have this space,
but I still managed to get the faulty fader out. Getting the
replacement in would be a different story until I had an idea.
I fed a piece of fine wire through the fader slot from the
top of the panel and wiggled it around until I got it past
the PCB. I then tied the wire to the fader’s shaft and used
it to slowly guide the fader to its location, where I could
then push it back into the holes in the board, resolder it
and test it. That saved me a lot of work.
Thirdly, a friend sent me his large stereo amplifier that
had stopped working after a heavy session. After a bit of
probing, I discovered the power transformer’s primary
winding was open circuit. It is not uncommon for Japanese-
manufactured equipment to have a thermal fuse inside the
power transformer in series with the primary winding.
These fuses are non-resetting, so the unit will no longer
work after they trip.
At first, I could not see the fuse; they are often buried
inside the bobbin that holds the windings.
After snipping away some small pieces of the bobbin,
I could just see the fuse at the bottom of a slot roughly
5mm wide and 40mm deep. With a suitable probe, I could
determine that this was where I needed to connect to the
winding, but how could I connect to it when my soldering iron would not fit in the slot without melting everything around it?
Then I remembered that my soldering gun uses a piece
of looped copper wire as an element and it is not very
wide. I dropped a small grain-of-wheat lamp into the slot
and powered it from my bench power supply so I could
see. I was then able to solder a wire to the fuse to complete the circuit.
That got it back into business, but as I had defeated the
thermal fuse, I checked to ensure a conventional suitably-
rated fuse was in line with the transformer. The thermal
fuse is an extra line of defence, but there are millions of
power transformers out there that do not have one. I have
even seen some transformers with an extra wire to bypass
the thermal fuse should it fail.
Repairing a wheelchair lift inside a car
J. W., of Hillarys, WA is another regular contributor to
this column. His latest entry involves repairing a wheelchair lift built into a Toyota Regius van...
A friend rang recently and asked if I could have a look
at his daughter’s wheelchair lift. He said that the lift was
not going back to the home position in the back of the van.
He had contacted several local auto electricians, but they
were not interested in looking at it, as it was a Japanese
import with no service information available. So I went
around to have a look.
The system was a genuine Toyota accessory and seemed
well-built (much like their cars). If the carriage was taken
too low, it would start to lift the van!
The lift has large motor driving screws that lower and
raise the platform, and that part was working as it should
(see the photo at upper right).
siliconchip.com.au
The wheelchair lift attached to a Toyota Regius van.
Once the platform was back at the level of the van floor,
two smaller motors and a second set of screws was supposed to drive it into the home position. This was not
happening.
The system was all-electric and controlled by four relays
& four microswitches. The main control assembly was easy
to unbolt and inspect. It had three large onboard relays plus
a smaller one.
The large ones were not enclosed, so I could see them
operating; they seemed to be working OK. I unplugged and
tested the small relay, and it was also functional.
Next, I decided to start checking the microswitches. Two
were easy to access and tested OK. The other two, which
switched power from the large motor to the smaller motors
and stopped the platform in the home position, were challenging to access.
After some deliberation and standing on my head in the
back of the van, my friend figured out that we needed to
take off the runner plate as that would let me access the
microswitches and wiring.
After that, I tested the final two switches, which were
fine. I then lay on the van’s floor and used a torch to look
at the wiring to the platform, which was hidden in part
of the frame. It was encased in black plastic cable chain.
Sticking out of the cable chain was a broken wire. I managed to effect a repair by joining the broken ends using a
small section of new wire.
The break had occurred because the plastic cable chain
had broken at one end, so the wiring was not supported.
I managed to cut some flexible conduit and fit it over the
broken section, which did not actually need to be flexible. We then put the whole system back together, and it
worked as it should.
The whole process took many hours over several days.
My friend and I were relieved finally to have the lift back
in the van and working again.
Restoration of a Porsche 928 (Central Warning System)
D. T., of Sylvania Southgate, NSW previously wrote
about repairing a Porsche 928 demister control relay (February 2022, pages 88-90). He’s still working on restoring
that car, but this time, it’s the warning system that’s on
the fritz...
Australia's electronics magazine
November 2022 105
During my restoration of a 1982 Porsche 928, I came to
the Central Warning System (CWS). In addition to all the
usual warning lights in the instrument cluster, the 928
CWS integrates all the warnings that the car generates into
one central warning light, also in the instrument cluster.
As well as illuminating this light if there is a major problem like oil pressure, high temperature or low fuel, it will
also light up with less common things like a low washer
bottle level or worn brake pads.
This warning light repeatedly flashes a specific number
of times, with the number indicating what the problem
is. Low-importance warnings can be cleared by pressing
a button, but high-importance warnings can’t. The central
warning light is also duplicated in the centre console – the
two lights are connected in parallel. I guess that way, if the
driver doesn’t notice it, the passenger might.
Finally, the CWS also turns all the instrument cluster
warning lights on each time you start the car, so you can
verify they’re working correctly.
Electrically, the CWS sits between the sensors and the
dashboard warning lights. The less-expensive model of the
car had a simple adaptor fitted in place of the CWS that
connected the sensors directly to the dash warning lights
in the traditional way.
With it plugged in, there was no response from any of the
instrument cluster warning lights or the light in the centre
console. I found that the light in the centre console was
shorted out with a piece of wire deliberately soldered across
it – I guess at some stage in the past, the CWS has failed,
and this was the easiest way to eliminate the warnings!
The indicator panel cleaned up with the short removed,
but I wasn’t surprised when it didn’t change anything –
with a short across the lamp, the driver was probably toast.
The next step was to open the CWS unit. I’ve found the
Porsche 928 modules to be quite serviceable in the past,
and this one was no exception. After I bent a few tabs, the
internals slid out of the aluminium housing to reveal a sandwiched pair of PCBs with plenty of parts – all through-hole,
and all discretes except for one 14-pin DIP IC.
The IC was an SN8400 with a TI logo, but I couldn’t find
any data on it. I decided it’s nothing like an embedded
microprocessor – this car was designed in the mid-1970s,
and they didn’t exist then. There were plenty of transistors
onboard, of seven or eight different types, with all but two
being in TO-92 plastic packages. Some I could find data
on, but most not.
When I tipped the housing over, a blackened 1W resistor
fell out. It only took a minute to figure out where on the
board the resistor came from, and tracing showed it drove
the two central warning lights – no doubt it overheated and
melted the solder because of the external short. The driver
transistor connected to it also had a crack in it.
I didn’t recognise the number on the transistor and
couldn’t find any data on it, but I measured a few others with the same marking and decided a BC547 would
probably do. Having fixed those two items, I now had the
central warning lights stuck on, but no instrument cluster
warning lights.
Next, I looked at the electros. There were some standard-
looking aluminium electros which all looked OK, but there
were also some plastic-cased 22μF units that had brown
residue around the top. Brown residue is never good on
electros. Funnily enough, it wasn’t anywhere near any
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Silicon Chip
seam in the case, but all the plastic-cased electros had it
to some degree.
I tried measuring them in-circuit with my Fluke, but I
haven’t really used the capacitance measurement facility
on the meter before and was dubious about it, especially
since I was measuring in-circuit. I wasn’t surprised when
I measured something other than the marked value.
I decided to remove one and measure it out of circuit and
it measured low – about 8μF. Not really being sure how
they were used, I thought I might as well replace them all.
I now had a flashing central warning light, but the flashing was inconsistent, bordering on gibberish. I thought it
might be because multiple valid warnings were present (for
example, the fuel tank and washer fluid were both empty).
However, posts on a Porsche forum said that it managed
this OK when it was working correctly.
The next step was to check all the transistor junctions
using the Fluke’s diode tester. I felt more confident about
this than I did with the capacitors – the voltage across a PN
junction should never exceed about 0.7V at low currents.
Plus, there were enough of each type of transistor on the
boards, so I could guess what was normal and what wasn’t.
Some types gave high base-emitter readings of about
1.3V. I decided these were Darlingtons with two diode
drops between the base and emitter.
I found two transistors I didn’t like. One I replaced with
a BC547, but the other was one of these Darlingtons. I spent
a bit of time looking around to try to find something to
replace it with, but TO-92 Darlingtons aren’t that common
even when there isn’t a silicon shortage, so in the end, I
replaced that device with a pair of BC547s connected as
a Darlington.
After that, I had a consistent flash indicating I had no
petrol, and the instrument cluster lights started working.
Afterwards, I measured the aluminium electros I’d replaced
on the bench and saw a range of values, some very low,
under 1μF. Interestingly, when I measured the new ones
in-circuit, they all measured about 22μF – chalk another
one up for the Fluke.
Editor’s note: the SN8400 is likely a quad NAND gate like
the SN7400 but with a different (possibly wider) operating
SC
temperature range to better suit vehicular use.
Australia's electronics magazine
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