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SERVICEMAN’S LOG
Mixing it up a bit
Dave Thompson
It’s frustrating when there is a flawed product on the market, and instead
of recalling or fixing it, the manufacturer blames the user instead. Your
mobile phone has no reception? You must be holding it wrong! This time,
it was our blender, and I had to turn to other users for a solution…
It’s hard to be a serviceman these days without hearing ominous stories about the ‘right to repair’, especially
regarding large US corporations. This has become a really
hot-potato topic and indeed has been commented on with
some insight by the Editor and other contributors to this
magazine.
One of the most serious concerns is the increasing use
of subscription models for hardware, which is becoming
more and more ‘de rigueur’. I think that is terrible news
for consumers and repair people.
Court cases and laws preventing monopolies and protecting the right of repair for consumers have driven some
companies to introduce subscription models, so they are
assured of continued income as well as protecting their
‘intellectual property’. One way they do that is by trying
to maintain control of their products after they are sold.
I suspect this will put many local repair people and servicemen out of work, often in very small communities,
unless, by some miracle, they can score a maintenance
contract with the vendors. No doubt they would demand
exclusivity anyway. If the manufacturer designs products
so that only they can reactivate them after a part is changed,
how is anyone else supposed to fix them?
The repair business isn’t what it used to be
So, a bleak outlook, then. My own computer repair business, almost 30 years old now, has seen the wave and wane
of the industry. Throw in a deep recession in the late 2000s
and the city and my workshop being ruined by earthquakes
in 2011, and it’s a wonder we still have a business at all.
At one point in the mid-2000s, we were averaging 65
calls a day. I employed four guys and two vans on the road.
These days, it is just me, and I’d be lucky to get 65 calls in
six months. It turned out this way because computer service and repair have long been sunset industries. These
days, it’s all mobile devices, and they are consumable, so
if one is dropped and broken, insurance or savings pays
for a new one.
In some cases, data recovery may be required, but even
that is moot as much of our stuff is backed up in ‘the cloud’
anyway. Every bread-and-butter job we had in the 2000s
has long since disappeared, only to be done now by techsavvy householders or the advent of self-install plug-andplay internet.
That’s OK with me, as I am nearing that age where I’ll
hang up my floppy drive anyway. But for dozens of other
companies and service guys, this really is the end of an era.
Manufacturing for unrepairability
It’s the same with just about everything these days. Most
appliances, for example, are manufactured without repair
in mind (or, if you are a bit cynical, with anti-repair in
mind). If you can even source replacement logic or controller boards, they are usually hellishly expensive because
they just aren’t made as available as they were in the past.
The manufacturer wants you to buy a whole new unit,
not fix the broken one. That’s one reason why repair being
monopolised by manufacturers is so troubling. There is a
conflict of interest, so they are more likely to quote you
unreasonably high repair prices in an attempt to convince
you to give up and buy a new one instead.
My wife bought a high-end food blender/mixer type
thing a while back, and overall, it works pretty well. It has
this thing called “wireless detect”, which took us a while
to figure out, but all we really use the thing for is blending and mixing, using the various controls on the front of
the machine.
One thing that always annoyed me is that it will only
run with a jug or attachment sitting in it. Actually, many
blenders have such a safety feature that prevent them from
being used with nothing attached to them. In this particular
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Australia's electronics magazine
siliconchip.com.au
Items Covered This Month
•
•
•
•
Overly complex food mixer ‘repair’
Tracking down interference using an SDR
Three different antenna repairs
Dual tracking power supply excessive ripple
Dave Thompson runs PC Anytime in Christchurch, NZ.
Website: www.pcanytime.co.nz
Email: dave<at>pcanytime.co.nz
Cartoonist – Louis Decrevel
Website: loueee.com
model, this wireless detection feature allows the mixer to
detect different-sized attachments and adjust pre-set programs automatically.
In other words, it detects the particular attachment
and adjusts things accordingly. As there are quite a few
different-sized glass grinder bowls and cups available as
optional extras, it seemed like a handy feature to have.
These attachments are basically glass bowls that screw
into the base that has the blades built into it. The whole
thing then mounts on the blender. The glass bowl part is
removed from the hard-plastic blade-driver section for
loading whatever you want to grind into it.
Let’s say you want to make some powdered salt. You fill
the glass bowl with the desired amount of granular salt,
invert the blade-holder part and screw it blades-first to the
glass bowl. You then flip the whole thing up the other way
and plop it, blade side first, onto the top of the blender,
engaging the splined drive socket.
You can then use one of the pre-programmed routines
or manually drive the mixer using the controls.
An exercise in frustration
It all seems simple enough. Except, on this model, with
the wireless detect feature, you have to have the main mixing jug, one of these herb grinders or any of the other attachments installed on it to even power up. And it turned out
to be so finicky that it made it almost unusable.
The main jug – the one that comes with it – seems solid
enough in operation. However, those optional glass bowl
attachments have what I discovered are NFC (near-field
communication) chips buried inside them that are read
by electronics inside the device.
In practice, though, the majority of the time we tried to
use these attachments, the mixer would not detect that the
bowl was in place, so it would not start. It was the same
with all the attachments we bought for it. Obviously, this
was not going to fly.
The attachments have arrows moulded into them that
show how much the two halves should be torqued for
the thing to work, but even when the arrows are perfectly
aligned, it just will not switch on most of the time. That
certainly created a lot of blue language from the kitchen!
Another problem is that, given the size of the smaller
attachments, cranking them up to have the arrows aligned
means crushing a large O-ring type seal between the two
halves. Trying to undo them once torqued is nigh on impossible for my wife and almost impossible for me. The whole
thing was starting to reek of poor design and implementation.
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Of course, this whole idea is product protectionism
cleverly disguised as a safety mechanism because thirdparty fittings and attachments that don’t have the correct
NFC tag will not work. Only original attachments can be
used on this mixer, and they’re not cheap. When it works,
it works well, but getting it to work was often highly frustrating for us.
Our first stop was the big-box store where we had bought
the main unit, along with these extra fittings we thought
we’d need. Of course, the guy there, while extremely knowledgeable when we were shopping for it in the first place,
now seemed to be struck dumb and claimed he’d not heard
anything from customers about it.
Perhaps our one was faulty, and if we liked, he could
feed it back through the warranty system and in just six
short weeks, we could have it back.
It was only a month old at this time, so I suggested that
if he thought it was faulty, perhaps they could see their
way clear to replace it under the Consumer Guarantees Act.
Well, you’d think I’d suggested sending his grandmother
on a one-way trip to Switzerland!
That solution apparently wasn’t going to happen, for
various reasons, first and foremost because we had used
the mixer! I contemplated going through the finer points
of finding faults without actually using an appliance. Still,
this guy had obviously been down the annoyed-client road
before and, like a debating team captain, had a pat answer
prepared for everything and anything I could say.
At this point, my serviceman’s lizard brain kicked in,
and I thought I’d open it up, have a look and see if there
was anything I could do. Perhaps the sensor had fallen off
or had been glued in at an angle, or something silly that I’d
be able to fix with my rudimentary knowledge of blender
repairs. I mean, how hard could it be?
We all know the answer to that, and you’d think that
after all these years, I’d know too!
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At least it was well made
Pulling this thing apart was not that difficult. These are
‘proudly’ made in the USA and using American-made parts,
or so the blurb states. That means no dumb security screws,
just straight-forward, meat-and-three-veg screws that can be
undone with a longish-reach Posidrive screwdriver. Everything came apart so easily. No breakaway clips, no hidden
screws under mouldings. Very refreshing!
I did have to pop out the rubber feet from the bottom to
reveal some case screws, but I’ll give them that as a neat
design.
Once the screws were out, the two halves of the case
came apart easily. There are no warranty-voiding stickers
across the join or any of those breakable foil screw covers
over anything. At least these appliances are designed to be
repaired, and I like that a lot. Spares are apparently widely
available from what the sales guy told me the first time we
were at the shop looking into buying one.
Inside is what you’d typically find in a blender. After
removing a well-made protective metal cover, I could see
the main space was taken up with a large brushed motor. It
directly powers a splined drive socket at the top of the mixer
via a square drive shaft at the end of the motor’s armature.
The splined drive socket is easily removable by loosening
a grub screw with an Allen wrench, if need be, and while
the splined and square drive parts are cast from relatively
heavy metal, the body of the drive socket is hard plastic.
This is actually by design; if something in the jug or bowl
fouls the blades and stalls the mixer, this plastic moulding will shear or crack, and the metal square-drive part of
it will just spin harmlessly inside the moulding to protect
the motor from stalling and potentially burning out motor
windings and electronics.
It is a relatively crude but very effective protection system. Replacement drive sockets are inexpensive and readily available. Another big plus for the repairability of this
device.
The mouldings and mounting for the motor and electronics are all super heavy-duty plastics, almost like Bakelite,
especially given what I usually see in most cheaper modern
appliances. This is definitely higher quality, and it is typical of the brand. The unit is certainly built to last, which
you’d hope for, given the relatively high purchase price.
The front panel controls – two toggle switches, a speed
control pot and the LED display – are all directly mounted
to a circuit on the inside front of the case. This PCB is populated with the usual mix of SMDs and discrete components, with heavy wiring to the motor and power switch
on the right rear side of the mixer.
It all looked pretty standard and what I would expect to
see in any reasonably advanced blender. However, I could
see nothing in or around the top of the unit that resembled
an NFC reader, so I assumed it was mounted on the main
circuit board instead.
This ‘initiator’ side of the NFC system should throw out
a magnetic field that would (hopefully) detect the passive
NFC chip embedded in the attachments and then allow the
mixer to be powered up, or not.
The thing is that I could see the NFC chips embedded
in the glass bowls on opposite sides, so why was this not
detecting attachments 90% of the time? As the attachments
have a spline-shaped base, they can sit at any angle in the
drive system, but no matter where they sat, the blender
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would not detect them most of the time. There seemed to
be no rhyme or reason.
So, to my mind, there was either a fault with our unit
or the NFC system is somewhat flawed. I reassembled the
blender, as there was really nothing I could do, except
feel a little better that I had at least tried to do something!
An unexpected solution
Next, I did what I always do and hit the web to see what
was going on. Perhaps unsurprisingly, it turns out that this
is a well-known problem with these blenders; a lot of people were moaning about it in online forums and videos.
Nice one, big-box store guy; we won’t be shopping with
you again!
As is typical with the information available, there is
a lot of it, and not much is helpful. Plenty of these slick
kitchen-type presenters were talking as if we were imbeciles and saying all we have to do is align the arrows on
the attachments, and it will work.
Oh really? They are either completely ignorant or wilfully obtuse, and the comments sections usually refer to
the former. While there are no instructions with the attachments, and the arrows are pretty hard to find unless you
are looking for them, this resolution didn’t seem to help
the majority of affected consumers.
The party line from the manufacturer themselves was
that a video would be ‘out soon’ to explain how to make
this more reliable. To date, nothing has been posted, so, as
is typical for a lot of technology, they leave it to end users
to resolve their issues and find a workaround.
As it turns out, there was only one video among hundreds where a home-chef type presenter found an almost
foolproof way of making it so the attachments were detected
and worked every time. She claimed she had just stumbled
across it after spending many hours trying to get her (much
more expensive model) mixer to work properly.
Her method was to screw the two halves of the attachment
together and line up the arrows. She would then place the
attachment on the blender, and typically, it would not be
detected. While it was in place, she cranked the glass part
about 30° more and magically, the blender would see it.
She could replicate this every single time, and of course,
the arrows on the case of the attachment no longer lined
up, but the appliance would detect it just fine.
This, of course, would make it impossible to undo again
due to being so tight. However, she then backed off the
bowl in-place, using the grip of the blender to help her.
She ensured she was still maintaining the seal – any contents would soon fall out if she undid it too far – and then
removed it and flipped it upside down before completing the unscrewing and removing the blades part of the
attachment.
Of course, the first thing I did was try that method with
ours, and it worked every time. The fact that the manufacturer hasn’t modified the attachments to show new arrow
positions, or at least put out a workaround video of their
own, is extremely disappointing. Sometimes, there is no
electronic fix, just a clever end-user who figures out how
to make it work.
The source of the interference
G. G., of Macleod, Vic thought he was solving one problem when he was actually creating a new one. He explains
Australia's electronics magazine
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how a software-defined radio (SDR) helped track down the
source of the problems...
I have a weather station to monitor the roof cavity temperature so I know when to turn on an extractor fan on a hot
day. I realise that it could be thermostatically controlled,
but I don’t want it running when we’re away.
The roof cavity sensor/sender seemed to be chewing
through batteries. Because of the nuisance value of getting into the ceiling, I decided to power it from a plugpack
plugged into a ceiling power point. That worked OK for a
few weeks, then the display stopped updating.
Then I started noticing that the remote controls for our
alarm system and garage doors had become less sensitive and
we had to be much closer to their receivers to get operation.
Next, a remotely-controlled ceiling fan refused to operate.
At about this time, I had brought home a system for repair
that included radio microphones and a mobile internet dongle. My wife was convinced it was causing the problems.
I replaced the batteries in the alarm remotes, which gave
a slight improvement. They had tuning capacitors, so I tried
tweaking them and got a bit more range, but barely enough.
Retraining and new batteries in the garage remotes seemed
to gain a little more range.
A web search told me that the alarm remotes were on
304MHz, so to check their outputs, I thought I’d install
an SDR that had been given to me years ago but that I had
never used. The software installation was tedious and even
required manual installation of the drivers, but it eventually sprang to life.
Stepping across that part of the spectrum, I couldn’t see
any response to my button presses. Testing with the radio
mic in the system in for repair confirmed that the SDR was
working correctly.
I then did a web search on the garage remotes. I found
a very useful site (www.remotepro.com.au) that gives all
manner of Australian wireless remotes and the programming of garage door openers, and even has full installation
details for many garage openers. That site told me that my
Merlin controllers were on 433.92MHz, so I tuned the SDR
to that frequency to check the garage remotes.
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December 2023 83
I found that there was already a very strong continuous
signal, 30dB greater than the local FM radio stations. Rough
direction finding with the whip antenna gave a null when
pointed toward the weather station sender. Powering down
the circuit going into the ceiling immediately stopped the
rogue signal, and all remotes started operating perfectly.
Reapplying the power even restored the temperature display, and on the SDR, I could now see a short update burst
coming from the sender about once per minute.
It seems that an occasional software glitch sent the
weather station into a continual transmission mode and,
as it was within a couple of meters of all the other devices’
receivers, it swamped their reception.
Likely previous similar glitches had flattened the batteries
before we’d noticed any effect, but my new power source
was able to keep the rogue transmission going. After the
reset, it has been performing normally for a few weeks; until
I get around to replacing it, I at least know how to restart it.
I later discovered that the alarm remotes also operate in
the 433MHz band.
A trio of antenna repairs
Around fifty years ago, I. G., of Banyo, Qld was a Radio
Trainee with the Department of Civil Aviation, field training
at his home station, the Gold Coast Airport (Coolangatta)...
I was lucky to have great mentors at the station, the supervisor and technician, who involved me in fault clearance
and regular maintenance. Still, one time I was left to my
own devices as they worked on a particularly troublesome
fault with the non-directional beacon (NDB).
The NDB was the most common and simplest navigation aid at the time. It is a low-frequency 200-400kHz AM
transmitter, transmitting a short two- or three-letter identifier in Morse code a couple of times per minute.
Before WW2, broadcast stations were used as navigation
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aids. With bearings from two stations, you could determine
your position on a map or track towards a known location.
That was not ideal as few broadcast stations transmitted
24 hours per day, and when broadcast networks became
the norm, you could not be dead sure which station you
were tuned to.
NDBs were a more reliable alternative. The lower frequency gave a better ground wave, with no chance of skip.
The Coolangatta beacon’s antenna was electrically short,
a single vertical wire supported by several horizontal wires
strung between two 22-metre tall towers. These horizontal
wires formed a capacitive top-load to increase the antenna
current and thus the antenna’s efficiency. The NDB transmitters were a pair of 100W vacuum tube units, providing
operational redundancy.
They were monitored by a receiver fed from a short whip
antenna inside the NDB hut. If any of the monitored parameters fell below the Low-Performance Level, the monitor
would change from the running transmitter to the standby.
Frequent intermittent faults were causing changeovers.
It was determined that the fault was causing a varying carrier level.
After a lot of investigation, the fault appeared to be in
the antenna itself. The DCA lines section was called in to
lower the antenna and investigate its condition. This was
reasonable because, being a coastal station, salt corrosion
was a likely culprit. However, the antenna checked out OK
and was hoisted back into position. The fault persisted.
During this process, the trainee (me) was superfluous
and left to his own devices. As I wandered about like a lost
soul, in one of my walks around the hut, I noticed that the
iron roof had a metal drainpipe down one corner that finished just above the ground and level with the ant cap on
the building foundation.
The drainpipe was not fully anchored and moved in the
breeze, bumping into the ant cap. I wedged it back with a
piece of timber and sought out the boss. We found that the
fault could be induced by pushing the drainpipe against
the ant cap. Grounding the roof and downpipe altered the
signal strength at the monitor receiver. Problem solved!
After completing my training, I was stationed at Charle
ville in southwest Queensland and became the acting
supervisor after a few years. This time, there was another
very intermittent fault with the Charleville NDB. It only
happened occasionally during wet weather. In this case,
the fault kept recurring for a long time with an unknown
cause; the short duration made it difficult to pin down.
When the beacon was eventually updated, the new installation required re-siting the transmitter in the “transmitter
hall” and the complete replacement of the antenna coaxial feeder (changed from 70W to 50W). When the old feeder
was removed, they discovered a female-to-female connector
under a little ‘sand dune’ in the building’s sub-floor cable
duct that dated from the previous NDB upgrade. Heaven
knows how long ago that was. It was not weatherproof
in any way and showed signs of distress. In the words of
Homer Simpson, “D’oh!”
The last item is also from Charleville. In the 1970s, before
the adoption of SSB high-frequency communications for
air/ground communications, comms were amplitude modulated. To cover all of the Flight Information Zone with
varying ionospheric conditions, three frequency ranges
were used near 3MHz, 6MHz and 8MHz.
Australia's electronics magazine
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The fault this time was interference on one of the 3MHz
channels. The interfering signal was the local radio station program (918kHz) mixed with the ident code from
the local NDB (267kHz). This was determined by sitting
down with a calculator and figuring out what combination
of harmonics of these two transmitters fell on the problem
receiver frequency.
The receiver antenna system was three half-wave dipoles
strung between two towers, with the lowest frequency at
the top and the highest at the bottom, to maintain the same
height relative to the wavelength. The feeders (shielded
twin) were laced to a vertical guide wire at the centres of
the dipoles.
Since the problem manifested itself only in the local
receiver, it was likely local. The immediate low-tech solution was to belt the receiver antenna feeders with a broom
handle, which alleviated the fault!
The fault was located in the supporting guide wire in
the receiving antenna system. Initially, the eyes used in the
mechanical structure of the supporting cables and other
fittings were provided with small plastic sleeves to stop
spurious rectifying joints from being formed by contact
between the dissimilar metals and/or their oxides, making
an unintended but efficient mixer.
The plastic sleeves were long gone in the western sun.
To clear the problem permanently, all these joints were
eventually bonded.
Fixing AC ripple in a dual-tracking power supply
T. I., of Penguin, Tas had a trusty old power supply until
it could no longer be trusted. Some gremlins were lurking
within that would need to be dealt with...
Following the completion of my electrical apprenticeship last century, I completed a course in Industrial Electronics, culminating in the construction of a Dual Tracking Power Supply kit, the details of which appeared as a
project in Electronics Australia in March 1982. The power
supply utilises LM317 and LM337 three-terminal regulators and provides ±1.5-22V DC at up to 2A.
It has been my main DC source for experimentation in
electronics over the years. “Tracking” refers to the magnitude of the negative rail voltage following the positive rail
across the entire voltage range. It does this by measuring
the positive regulator’s adjust/reference signal, inverting
it and feeding it to the negative regulator’s adjust terminal. There is also a fixed 5V reference supplied by a separate regulator.
The power supply has performed faultlessly over the
years – until recently.
Having built Nixie tube projects in the past, I am now
in the process of building a VFD (vacuum fluorescent display) clock with a 32,768Hz crystal timing reference. I
design, build and test the PCBs using the power supply
mentioned above.
I completed the crystal oscillator timing board and the
divide-by-32,768 circuit to provide the 1Hz count for the
clock timing. I connected my CRO lead to observe the
32,768Hz waveform, only to find significant noise on the
trace.
Although it was a definite sinusoidal waveform, I could
not achieve a clean single trace and initially thought that
the crystal was possibly being overdriven. However, after
spending some unnecessary time changing components
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around the crystal, I just could not get a clean signal.
Instead of a clear trace, it appeared as a sinewave drawn
by a 10mm-thick noisy trace.
Somewhat frustrated and overdue for lunch, I switched
off the AC supply to the power supply with the CRO still
connected, and the signal instantly became a clean sinusoidal trace until the power supply’s onboard filter capacitors drained their charge away. That got me wondering
whether the unit I’d built all those years ago was in trouble.
I was able to prove things weren’t right by powering the
crystal oscillator with an alternative DC supply; it produced
a perfect trace on the CRO. I then put the CRO leads across
my power supply’s output and could see significant AC
ripple that obviously shouldn’t be there. My timing circuit
was being modulated with AC ripple from the DC supply.
I removed the four screws holding on the lid and slid the
cover off. I could see four tantalum capacitors and several
aluminium electrolytics. Given the age of the unit, I suspected that at least one was faulty.
Looking at the circuit, I could see a 1μF tantalum at the
input to each regulator, a 100μF electro across the output
of each regulator, and a 10μF tantalum across the voltage
adjustment potentiometer. I could also see some discolouration on one 120W resistor between the adjust and output
terminals of the positive regulator.
I clearly needed to remove the PCB and therefore took
heaps of photos and marked the wires before going any
further. I desoldered the main transformer AC connections
plus the wiring to both the regulators, which are mounted
on the side of the case for heatsinking. I then removed four
other connections to various switches and indicator LEDs.
I could then swing the PCB out far enough on the remaining wiring to enable component replacement. While the
board was out, I checked the integrity of all the onboard
diodes and any suspect dry joints. However, all was good
and certainly acceptable, given my inexperience at the
time I built it.
I replaced the four tantalum capacitors, the two 100μF
electros and the discoloured 120W resistor, then set about
restoring all wiring connections. After checking and
rechecking, I plugged the unit back in with the lid still
removed and with fingers crossed, switched it on. Great –
no smoke, so a good start.
A test of the voltages proved that the unit was functional
across the full range. Connecting the CRO leads showed a
perfect, ripple-free DC supply. However, I then noticed a red
LED fully illuminated. This was the dropout LED, which
should only be illuminated if a fault draws too much current
on the output so that the regulator drops out of regulation.
What was going on here? I had no load connected, and
the voltage tested perfectly across the entire range.
Spending too much time measuring voltages around the
components driving the LED, I finally realised that the sunshine coming through the window (yes, we do get sunshine
in Tassie’s winter occasionally) was shining through the
back of the LED, which was mounted on the front panel,
giving the impression that it was illuminated. Shading the
sunlight stopped the glow. No wonder the wrinkles on my
forehead keep multiplying!
With the lid back on, I connected the crystal oscillator
to the power supply and tested the signal with the CRO,
to see a perfectly clean trace. Hopefully the unit will serve
me for many more years to come.
SC
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