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How I made a 30mm desktop
Spark-Gap Tesla Coil
by Flavio Spedalieri
My Solid-State “Flame Discharge” Tesla Coil project from the February 2022
issue (siliconchip.au/Article/15196) worked well but lacked the iconic metal
toroid ‘top load’ that most people think of when they hear “Tesla Coil”. So I
built an even larger device, that while still quite small, is more traditional!
This device generates hazardous voltages!
While we are not providing instructions on building or operating a Tesla Coil in this article, we
advise caution if you build or operate a similar device.
All parts of the Tesla Coil operate at lethal voltages and can deliver enough current to stop
a heart or cause serious burns. You can also suffer RF burns if you come close to or contact
the discharge terminal, even when no discharge is apparent.
Always ensure that you are nowhere near the breakout point when the unit is powered
up. Keep all parts of your body (or anyone else’s) clear of it until power has been switched
off and the discharge stops. Remember that high voltages can still be present even when
no discharge is visible.
Electromagnetic interference warning
This Tesla Coil is an RF generator. The input power is up to 180W and the spark gaps are
broadband RF radiators.
During operation, it can cause RF interference over a wide range of frequencies,
especially the MF band, including the AM broadcast frequencies, MF amateur band and
some mobile phone frequencies. Operation within a Faraday cage is advisable.
52
Silicon Chip
Australia's electronics magazine
siliconchip.com.au
B
uilding a full-size Tesla Coil is a
significant undertaking. Therefore, in August 2020, when my
motivation started to peak, I decided
to make a small-scale but traditional
Tesla Coil. It is traditional both
because it is capped with a metal torus
and it uses a spark gap-based oscillator.
That oscillator drives the transformer
that generates the extremely high voltages (tens of kilovolts) required for
breakout.
While my February 2022 article
explained how to build your own very
small Tesla Coil, this article is more of
a story describing how I built a somewhat larger Coil. I won’t go back over
the theory of Tesla Coils that I presented in the February 2022 issue,
but I will quickly recap it to explain
how this one differs from that earlier
version.
A Tesla Coil is a type of resonant
transformer invented by Nikola Tesla
(patented on the 25th April 1891). It
transforms relatively low-voltage AC
(a few hundred volts to a few kilovolts)
to very high voltages (tens of kilovolts
to megavolts) via two LC (inductor-
capacitor) tuned resonant circuits that
are loosely inductively coupled.
The primary LC circuit comprises
the ‘tank’ capacitor, primary coil
(inductor), and a ‘switch’ to complete
the circuit. The primary circuit can
be switched by several methods; In a
‘classic’ Tesla Coil, a basic spark gap
is used (see Fig.1).
Other topologies use vacuum tubes
while, in modern dual-resonant
solid-
state Tesla Coils (DRSSTCs),
solid-state transistors (IGBTs or Mosfets) are employed. That latter configuration is what I used in my February
2022 project.
The secondary LC circuit comprises
Photo 1: the
secondary
coil has
close to 38
turns per
centimetre.
the secondary coil (the large central
tower that is iconic to a Tesla Coil),
and the ‘top load’, which provides
the capacitance and a place for the
high-voltage breakout to occur.
In this case, the capacitor begins to
charge when power is applied to the
primary circuit. Eventually, the voltage across the capacitor increases to
the point that the air in the spark gap
breaks down. The energy in the capacitor then discharges across that gap and
through the primary coil.
The energy then oscillates back and
forth between the capacitor and the
primary coil at a high frequency that is
determined by the capacitor value and
the primary coil’s inductance.
A Tesla Coil’s ability to generate very
high voltages and long arcs (streamers)
is due to a process known as resonant
voltage rise occurring in the secondary
LC circuit. Tesla coils can be scaled
up to produce many millions of volts.
New design concept
My initial idea was to build a small
Tesla Coil using an arc lighter or neon
sign transformer (6kV/30mA) power
supply as the high-voltage source. I
had some suitable components at hand,
including 3nF 20kV AC rated capacitors, a ‘doorknob’ ceramic capacitor,
plenty of 0.25mm diameter enamelled
copper wire and a 107mm diameter,
27mm high aluminium toroid.
Fig.1: a circuit
showing one of
the most basic
arrangements of a
Tesla coil.
Fig.2: the output
data from the
JavaTC software
that I used to help
me design the Tesla
Coil.
siliconchip.com.au
Australia's electronics magazine
In the very early stages of the project, I considered a 50mm diameter secondary coil. However, it would have
required so much wire that I would
have had to special-order a large spool.
My local Jaycar Electronics store
had a small spool of 0.25mm diameter enamelled copper wire. Given the
available length and the wide range
of available diameters of PVC tubes,
I spent several hours calculating a
secondary form that would allow
for around a 4:1 aspect ratio. The
final design was a 33.5mm diameter,
132mm high coil of the Jaycar wire on
a 30mm PVC former.
Winding the secondary
I cut a 160mm length of 30mm PVC
tube to give approximately 10mm of
clearance at each end. I then sanded
the PVC and sealed the surface with
two coats of UltiMeg 2000 electrical
varnish (siliconchip.au/link/abha).
I used a hand drill to hold the form
and slowly guided the wire onto it,
taking ~2.5 hours. During the next few
days, I coated and sealed the secondary with several coats of clear varnish.
I measured 38 turns per centimetre
(Photo 1), very close to the 37.88 calculated (shown in Fig.2), giving close
to 500 total turns.
I sealed the ends of the secondary
form using FR-4 (unclad PCB). The
construction techniques I used for the
SECONDARY COIL OUTPUT DATA
Secondary resonant frequency
Angle of secondary
Length of winding
Turns per unit
Space between turns (e/e)
Length of wire
H/D aspect ratio
DC resistance
Weight of wire
Effec. series inductance (Les)
Equiv. energy inductance (Lee)
Low frequency inductance (Ldc)
Effec. shunt capacitance (Ces)
Equiv. energy capacitance (Cee)
Low frequency capacitance (Cdc)
Topload effective capacitance
Skin depth
AC resistance
Secondary Q
1618.28
90
13.2
37.88
0.00936
52.62
3.94
17.6699
0.024
1.848
1.931
1.879
5.233
5.009
8.014
3.997
0.0562
88.3825
213
kHz
deg°
cm
cm
mm
m
:1
W
kg
mH
mH
mH
pF
pF
pF
pF
mm
W
February 2023 53
Tesla Coil Specifications
Primary
] Capacitor: 3nF, 20kV AC
] Tap: 4.25 turns
] Tap frequency: 1527kHz
] Tap inductance: 2.23μH
] Total inductance: 13.5μH
Secondary
] Turns: ~500
] Resonant frequency without
toroid: 2489kHz
] Resonant frequency with toroid:
1708kHz
] DC resistance: 19.2W
] Inductance: 1720μH
Toroid
] Major diameter: 107mm
] Minor diameter: 27mm
] Calculated capacitance: 4.62pF
] Calculated breakout: 80.62kV
Neon Transformer
] Power supply output: 6kV <at>
30mA (180W)
] Primary resistance: 11W
] Secondary resistance: 12.7kW
(6.3kW to centre tap)
] Secondary impedance: 200kW
secondary are the same as for much
larger (high-performance) coils; no
part of the winding can penetrate the
former. I terminated the ground end of
the winding via a copper tab, while the
top of the coil is supported by a Nylon
screw that I epoxied to the top plate
before sealing the secondary.
I finished the ends of the windings
with black electrical tape and gave
the secondary several more coats of
clear varnish.
I decided upon a coupling method
that would allow the secondary to
plug into the overall system, allowing
a modular approach and safe storage
of the secondary when not in use. The
coupling also serves as the electrical
ground connecting point at the base of
the secondary, as shown in Photo 2.
With the secondary complete, I characterised it using an oscilloscope and
signal generator. Its DC resistance is
19.2W, while its resonant frequency is
1708kHz with the toroid and 2489kHz
without it.
At this point, I decided that it was
going well enough that I would build
a high-quality instrument where the
aesthetic aspect was important. I also
switched from the idea of using the
arc lighter to a neon sign transformer
(NST) that I had acquired, rated at 6kV
and 30mA (180W).
Additional calculations suggested
that the resonant capacitor should be
15.9nF, with a larger-than-
resonant
(LTR) capacitor being 240nF. Still, I
pressed on with the initially selected
3nF capacitor as I could always
increase the capacitance later.
Using a neon sign transformer meant
that some additional components
would be required: a protection filter
(‘Terry Filter’), power factor correction
(PFC) capacitor and an EMI line filter.
Primary construction
Photo 2: a coupling was added at the
base of the secondary so that it could
easily be removed when not in use. It
also serves as a ground connection.
54
Silicon Chip
The next phase of the project was
the design and construction of the primary coil, supports and platforms to
mount all the main coil components.
Some of the crucial criteria when
working with high voltages at high
frequencies are sufficient clearances
(to minimise arcing and insulation
breakdown), selection of appropriate
materials suitable for electrical work
and fastening techniques.
I selected “SwitchPanel Type X”
as the main support material for the
primary coil. It is a fibre-reinforced
impregnated phenolic resin designed
Australia's electronics magazine
Photo 3: a conical primary (30°)
was decided on, with an adjustable
platform made from hardwood.
for electrical insulation (siliconchip.
au/link/abhb).
I ordered three sections for the coil
supports from Vale Plastics, all 180mm
× 180mm, with one panel having a
50mm central hole to allow it to clear
the coupling.
The primary design took considerable analysis, considering the electrical parameters, size and shape (flat
spiral, vertical or conical). Due to the
way the primary coil’s electromagnet
flux is presented to the secondary coil,
I decided on a 30° conical primary
(see Photo 3).
The field of a conical primary coil is
more uniform over the secondary coil’s
aspect. At the widest point (outermost
turn), the primary width is approximately the same as the secondary
height (~140mm). I used a 2.14mm
diameter copper capillary tube with
an inter-turn (edge-to-edge) spacing of
5mm (7.14mm to the centres), giving a
total of 10.5 turns for tuning flexibility.
The mounting platform of the primary coil should be adjustable to allow
for fine-tuning of the coupling to the
secondary. I started building it by making the four support wedges, cut from
hardwood.
I attached them to the SwitchPanel
Standard Soldering
Ball Soldering
Fig.4: the components for the filter
were soldered using a technique
called “ball soldering”. This technique
helps to minimise corona losses at
high voltages.
siliconchip.com.au
using Loctite two-part epoxy, which
has good gap-filling characteristics.
No metal screws or nails can be used,
so all fixed components are glued or
fastened using Nylon fixings.
With the coil made and on the supports, I glued the final timber caps
in place with more epoxy for better
mechanical support and to improve
the aesthetics. I also glued the central
coupler into place. A copper strip, central brass screw, nut and acorn completed the grounding termination for
the secondary.
At this point, the primary and secondary were almost complete.
Terry Filter and safety gaps
Intending to use a neon sign transformer (NST) as the power supply, I
made the secondary windings from
very fine wire. Typically, enamel wire
insulation is not very good at handling
the fast, high-voltage transients generated in a Tesla Coil each time the
spark gap fires, which can shorten the
life of the NST.
One method of protecting the transformer’s secondary windings is a lowpass RC filter network known as a
Terry Filter (www.hvtesla.com/terry.
html) – see Fig.5.
I started building one by mounting
the main capacitors and MOVs on
FR-4 laminate board. I came up with
the component layout, marked holes
for drilling using a piece of ‘perfboard’
(prototyping PCB) and drilled the 1mm
holes by hand.
I soldered the components using
a special technique called ‘ball soldering’, where the joints are made as
smooth and spherical as possible to
minimise corona losses at high voltages (see Fig.4).
The safety gaps are made from three
brass drawer knobs. I sanded each
ball with fine wet & dry sandpaper to
remove the clear lacquered coating,
then drilled and tapped them with M4
threads. I repurposed three aluminium
blocks as the supports.
I drilled and tapped each block with
an M4 thread to mount them onto the
FR-4 substrate. The position of the
two left/right balls can be adjusted
for correct operation of the safety gap
(ie, so the air gap will break down at
an appropriate voltage). You can see
how this arrangement is mounted on
the Terry Filter assembly in Photo 4.
I made the high-voltage cables that
connect to the coil itself using 7.5mm2
siliconchip.com.au
Fig.5: the protection filter circuit (Terry Filter) for the Tesla Coil.
Photo 4: the safety gap uses three brass knobs mounted to the Terry Filter
circuitry (components placed but not yet wired up). The knobs were mounted
onto aluminium blocks and set up so that their positions can be adjusted.
Australia's electronics magazine
February 2023 55
t0
Photo 5: after mounting the Terry
Filter onto a plate of SwitchPanel
Type X, a test was performed to verify
the operation of the safety gaps.
OFC stranded power cable with two
layers of PTFE tape applied. Heatshrink tubing was added, followed by
an additional layer of PTFE tape and a
final layer of heatshrink tubing.
Readily-available white PTFE
(plumbing tape) has a high dielectric
strength of around 60-70kV/mm (see
siliconchip.au/link/abhc). Common
high-density PTFE plumbing tape has
a density of about 0.3g/cm3 and a nominal thickness of 0.1mm (siliconchip.
au/link/abhd), so it has a dielectric
strength of about 6-7kV.
I mounted the Terry Filter and safety
gaps onto a 150 × 250 × 12mm plate of
SwitchPanel Type X. I made the electrical connections to the filter with
brass hardware and acorn nuts, while
the connection to the Tesla Coil is via
the two aluminium blocks on the left
and right sides. Photo 5 shows my tests
to verify the operation of and adjust
the safety spark gaps.
Main spark gap & tank circuit
With the Terry filter finalised, I
moved on to the main spark gap and
the layout of the tank circuit components.
The performance of a Tesla Coil is
determined by the performance of the
spark gap, which acts as a momentary switch that completes the circuit between the capacitor and the
primary coil. The capacitor’s energy
is discharged into the primary coil
when the gap conducts. A spark gap
is a simple device, but the dynamics
of its operation are complex.
The distance between the electrodes
56
Silicon Chip
t1
t2
Fig.6: the times
labelled t1 & t3
are the first and
second primary
notches – the
times when
the current
in either the
primary has
fallen to zero
and the spark
gap can be
quenched.
t3
t0: gap fires.
t0 > t1: primary energy transfers to the secondary.
t1: all energy is now stored in the secondary (1st primary notch).
t1 > t2: remaining energy in the secondary transfers to the primary.
t2: all energy is now stored in the primary (1st secondary notch).
t2 > t3: remaining energy in the primary transfers to the secondary.
t3: all energy is now stored in the secondary (2nd primary notch).
This process repeats until the gap stops conducting (quenches). Once quench occurs,
an exponential ringdown will occcur.
sets the breakdown voltage of the spark
gap. With a static gap, the width would
be set at the power supply line voltage
(6kV in this case) and would be at the
correct setting with the gap firing at the
full applied voltage of the transformer.
This project utilises a static gap
arrangement; however, much larger
coils employ rotary spark gaps, giving better control and performance.
For a coil of this size, that would be
slight overkill.
The main spark gap consists of
the electrode holders and the actual
electrodes. For this project, I have
employed 6.35mm diameter parallel-
faced tungsten rods. Tungsten is a
favoured material for spark gaps due
to its high melting point and, therefore, resistance to burning and pitting.
When the gap fires, the arc ionises
and heats the air within it, making
it highly conductive. Once the gap
conducts, it will continue to conduct
even when the capacitor’s voltage has
dropped below the initial breakdown
voltage. This can allow the energy
from the secondary to return to the primary; this energy will be lost as heat,
sound and light, reducing the coil’s
performance.
Extinguishing a conducting spark
gap is known as ‘quenching’ and
is essential to maximise the energy
retained in the secondary.
Quenching is the action of the spark
gap going open-circuit and ceasing
conduction, and can only occur when
the current through a conducting gap
falls to a certain point. Then, the arc
may no longer be sustained, and the
Australia's electronics magazine
air within the gap cools enough to prevent arc-over as the voltage begins to
rise again on the next cycle.
The total energy transfer time is
the number of half-cycles it takes at
the resonant frequency to transfer all
the energy from the primary circuit to
the secondary (not including losses).
Ideally, we would like to trap all the
energy within the secondary, as any
energy that returns to the primary will
contribute to inefficiency and, thus,
less energy for the output arcs.
The only way to trap the maximum energy within the secondary is
to stop the gap conducting as soon
as the current in the primary circuit
reaches zero.
Known as the ‘first (primary)
notch’, this period is very short, and
the amount of energy still within the
1st secondary notch
Secondary Envelope
2nd secondary notch
Exponential ringdown
3rd primary notch
2nd primary notch
1st primary notch
Fig.7: this waveform shows the third
notch quenching, meaning the third
primary notch is where the gap
stopped conducting, followed by the
secondary ringdown.
siliconchip.com.au
Photo 6: a centrifugal blower fan was
used on the main spark gap instead of
an axial fan, as it provides superior
airflow.
Photo 7: the spark gap assembly is
composed of two electrode holders
mounted on a FR-4 substrate.
primary is sufficiently high to keep
the gap conducting (see Figs.6 & 7).
If the gap continues to conduct, the
next available opportunity to open
the spark gap is at the next point that
the current returns to zero (the second
primary notch) and so on.
Early quenching of the spark gap
may be achieved through various methods, including magnetic quenching
(siliconchip.au/link/abhe), air blast
(siliconchip.au/link/abhf), vacuum
(siliconchip.au/link/abhg) or with a
rotary spark gap.
Using forced air, a vacuum or a
rotary gap allows the gap to cool by
removing hot, ionised air from it,
reducing the chance of the gap re-
arcing. I decided to use a centrifugal
blower fan (drawing 12V <at> 860mA),
as such fans generate high-pressure
air flows compared to an axial fan
(see Photo 6).
I was going to use PWM fan speed
control but, in testing, it offered little
effective control; therefore, I abandoned that idea. Instead, the fan just
runs at full speed during operation.
I used a copper bus bar to form the
support for the capacitor, with a short
copper tube to connect it to one side
of the gap.
One last detail for the coil is the
strike rail, which protects the primary
coil and primary circuit components
from arc strikes, made from a 2.3mm
capillary copper tube (Photo 8).
The ground rail must present a low
impedance path to RF ground, so I
made a clip from a copper saddle that
is snug fit onto the strike rail. I then
added a grounding post to terminate
the secondary ground and the strike
rail (Photo 9).
The strike rail mustn’t form a closed
loop, as would otherwise present as a
shorted turn.
The strike rail supports are made
from 9×9×46mm timber sections with
a 2.5mm hole drilled through each
support. I sanded and stained these
before gluing them into place with Loctite epoxy. I then slid the copper tube
into place and used heatshrink tubing
to cover the open section.
Primary tap point
Constructing the primary tap connection was a challenge. Early in the
project, I drilled four clearance holes
with the idea of bringing the tap wire
up through the bases. However, this
made it difficult to disassemble and
reassemble.
So instead, I brought up the tap wire
from the side, using a clip made from
a modified M205 fuse clip, reduced
to create a snug fit. I used a length of
copper braid to strengthen the clip and
provide a better connection.
At this point, I had completed much
of the Tesla Coil, but was still waiting
Main gap & strike rail
The main gap is the critical part of
the spark gap oscillator. I cut a phenolic resin plinth as the mounting base
for both the spark gap assembly and the
connections to the capacitor. The gap
itself was formed by mounting electrode holders onto two phenolic support blocks, which I then affixed to a
strip of FR-4 substrate. I then attached
the whole assembly to the phenolic
base (see Photo 7).
siliconchip.com.au
Photo 8: the outermost copper tubing
is the strike rail, which was added to
protect the primary from arc strikes.
Photo 9: after building this, a clip was
added to the strike rail to ground it
(shown in the photo at right).
Australia's electronics magazine
February 2023 57
for the high-voltage bleed resistors
(10MW, 10kV) for the main capacitor.
I searched Digi-Key’s website and
found they stock 100MW 10kV 2.5W
Maxi-Mox resistors from Ohmite
(MOX-1-121006FE). As well as being
available, they had the advantage that
a 10MW bleeder resistor would have
dissipated 7.2W. Increasing to 100MW
reduced that below 1W while still discharging the capacitor to a safe level
(50V) in 1.5 seconds.
Radio frequency (RF) Earthing
One of the more overlooked and
important areas with any RF system
is the provisioning of a suitable low-
impedance Earth system. Tesla Coils
generate heavy RF currents which
must be appropriately distributed to
Earth. A sound Earthing system is key
to a well-performing Coil as the Earth
forms the return path for the secondary side of the LC circuit.
So I sunk a 19mm diameter,
2.4m-long Earth rod to 1.8m depth,
plus a second ‘domestic’ size rod to
1.2m, bonded them together and connected them to the coil via 25mm2
welding cable.
Measurements
With the Coil essentially complete,
I made some measurements to determine the tuning parameters and confirm the resonant frequencies against
my calculations.
I measured the resonant waveform
period as approximately 124μs, corresponding to the total energy transfer
time; the first notch came after approximately 8.2μs.
Power supply
I mounted the neon sign transformer
to a 12mm-thick 200 × 300mm base
made from SwitchPanel. I added two
timber stand-offs to mount the Terry
Filter module (Photo 10).
I then added the control box,
which includes a TE Connectivity 3A
EMC-series EFI/RFI line filter to prevent interference from feeding back
into the mains. The control box also
contains a small mains switchmode
power supply (SMPS) to provide 12V
<at> 1.2A for the quenching fan.
The control box also includes a
mains switch, a switch for the fan
and a switch to supply power to the
transformer, lamps to confirm active
power to the circuits and a 2A thermal magnetic circuit breaker (Photo
11). This control box is used with a
variac to provide fully adjustable control of the Coil.
First tests
Following nearly three months of
development, I fired it up for a momentary test. I noted a flashover from the
end of the primary winding to the strike
rail, occurring several times at the same
location, causing a tracking burn.
I realised this was due to the end of
the primary not being smoothed off
and sealed. Another overlooked area
was that I hadn’t sealed the supports
with varnish such as Ultimeg.
I repaired the area, smoothed the
copper end and applied epoxy resin
to seal it. After cleaning up the tracking burns, I also sealed the support.
I added more epoxy to all key areas
at the primary junction and supports
and applied several coats of Ultimeg
electrical varnish to the timber supports. I left the primary coil assembly
to cure for several days.
In hindsight, considering the pulsed
nature of the high-voltage present on
the primary coil, timber is not the best
material to use. A more suitable material would be a phenolic resin; however, it is expensive in small quantities
and with suitable dimensions. SwitchPanel Type-X could be used to create
the smaller parts, but it would need
to be cut from a larger sheet, which
would take a great deal of time.
With those repairs and improvements completed, I returned to testing,
closing down the spark gap to around
3-4mm for the test. The low-power test
was successful, with a nice breakout
occurring (Photo 12).
I then opened the gap to about 5mm
and made another run (Photo 13). It
was successful, but I noted some random flashover between the final turn
of the primary to the strike rail.
I obviously needed to improve the
insulation between the strike rail and
the final turn of the primary coil. I did
that by adding more layers of Ultimeg
varnish, as well as adding short lengths
of clear vinyl tube around crucial
points on the strike rail and final primary turn. I let the varnish cure over
a week before getting back to testing.
I then ran a full power test, applying
the full mains voltage to the NST. In
doing so, I tweaked the parallel alignment of the spark gap electrodes. The
full power test was very successful,
with many streamers forming but no
arcing at the support points.
Photo 10: the neon
transformer was
mounted to a 12mm
thick base made
from SwitchPanel.
Timber stand-offs
were then used to
attach the finished
Terry Filter above it.
Photo 11: the control
box for the Tesla
Coil. It contains
a mains switch, a
switch for the fan,
another for the
transformer, lamps
to confirm activity,
and more.
58
Silicon Chip
Australia's electronics magazine
siliconchip.com.au
Top-load upgrade
I decided to order a larger toroid
from a company based in the USA.
It took close to two months to arrive.
Their customer service left a lot to be
desired, so I don’t want to mention the
company’s name.
The larger toroid has a major diameter of 152mm, a minor diameter of
38.64mm, a calculated capacitance of
6.61pF and a calculated breakout voltage of 114.74kV.
The additional capacitance of the
larger toroid required re-tapping the
primary coil to bring the primary
into tune with the lower resonant frequency of the secondary. A further resonant test using an oscilloscope and
signal generator on the secondary coil
confirmed the new resonant frequency
as 1360kHz.
I moved the primary tap by one turn
to account for the extra load on the
secondary, bringing the system back
in resonance. The lead photo shows
the result of a full-power test with
the larger toroid in place. It generated streamers long enough to reach
the strike rail; they are equivalent in
length to the secondary coil.
I conducted another experiment
by simply placing the two toroids on
the coil, resulting in longer streamers
(Photo 14). Re-tuning the coil was not
necessary.
Photos 12 & 13: on the left is the initial low-power test with a spark gap of
3-4mm, while on the right was another test run with the spark gap at 5mm.
Conclusion
It was a lot of work, but I am
delighted with how this small Tesla
Coil turned out. It was interesting to go
through the tuning process that Nikola
Tesla and other pioneers would have
had to figure out. I also learned that it
pays to give special attention to insulating everything when working with
such high voltages.
Tesla was a genius to have come
up with such an elegant way of generating extremely high voltages using
the very limited technology available
at the time.
While building a Tesla coil is not for
everyone, they are impressive devices
and a must-have in any mad scientist’s
laboratory!
In memory of
My Mum (Zina Spedalieri) was
amazed when she saw the original
article come to print. Sadly, we lost
Mum on 2nd of June 2022, It would
have been something for her to see the
second article come to print.
SC
siliconchip.com.au
Photo 14: placing the newly bought larger toroid on top of the old toroid
resulted in larger breakouts. As I was happy with the result, I eventually had
the toroids welded together, then cleaned and sanded them to maximise their
appearance and performance.
Australia's electronics magazine
February 2023 59
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