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SERVICEMAN’S LOG
Sometimes it all just falls into place
Dave Thompson
Often in the service industry, we get these weird coincidences where a
new appliance in need of repair comes in, then a few days later, another
similar unit turns up as well. Although I have no experience repairing
this type of device, I was fortunate that both had simple faults that
became apparent once I dug into them.
This sort of weird coincidence happened to me recently
when a computer-repair client mentioned they’d just
opened the packaging on one of those oil diffusers that
seem to be all the rage these days. They’d purchased it a
while back, but when they went to plug it in, they discovered it wasn’t working.
Of course, I said I could take a look at it (it’s an electronic
device, after all), though I made it clear that I’ve never
opened one up before, so this would be a new experience
for me. They were happy for me to crack it open and have
a look, as it was now out of any warranty that might have
applied, and they accepted that doing something is better
than doing nothing.
I understood completely because I know that many of
these diffusers are not cheap; some go for hundreds of dollars, a significant outlay in anyone’s money. If I plugged
in a brand-new device and it didn’t work, I’d also be more
than a little miffed about it!
I hadn’t even started on the repair yet when another client called and asked me if I’d ever had an oil diffuser in
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for repairs. I replied that, of course I had, before explaining
to them that it had only been one day, and I hadn’t even
had a chance to look at it yet! They too claimed that it had
cost a pretty penny and, while it had been working fine for
a while, it had started failing to stream vapour properly.
In the meantime, their cat had knocked it off the table it
lived on, and now it sounded like something had come adrift
inside. Could I look at it? Bemused by the coincidence, I
agreed to take the job on – I mean, how hard could it be to
repair something as apparently simple as an oil diffuser?
Before the second one arrived at the workshop, I decided
to crack open the case of the first one and see what was
going on.
Preparing for surgery
The main body of this diffuser is made of injection-
moulded plastic and consists of three sections. The base
contains the power input socket and controls. A water tank
section is mounted on top of the base, while a removable
funnel-shaped ‘chimney’ caps off the whole caboodle.
Vapour streams from the open ‘chimney’ when the device
is operating.
This diffuser has other features; a digital clock and on/
off timer are included, as is one of those sound synthesisers that can simulate rain, wind, the ocean and, in this
case, a forest with birdsong or a running brook or stream.
A row of pushbuttons and a rotary volume control (similar to what you’d find on an old transistor radio) are set
around the middle of the base part of the body. These control everything to do with the diffuser, the clock and the
sound generator.
Removing the funnel is simple enough – it is designed
to be removable and is simply press-fitted onto the middle section (the water tank). This is how water and oils are
added. The cone is then re-fitted, and the diffusing process starts. With the cone off, I could ensure that no water
was trapped in the internal components. It was bone dry.
The next thing was to separate the two bottom parts –
this would reveal all the actual components. The two parts
were fastened together with two simple PK-style screws.
There were also three clips at 120° positions around the
circumference of the body; these required a little careful
fettling to remove.
This method of clipping things together instead of screws
or other fasteners is increasingly used these days to hold
plastic cases together. The screws in the base are likely a
Australia's electronics magazine
siliconchip.com.au
Items Covered This Month
• Sometimes it all just falls into place
• Tips for fixing an LCD TV backlight
• An unfortunate series of battery chargers
Dave Thompson runs PC Anytime in Christchurch, NZ.
Website: www.pcanytime.co.nz
Email: dave<at>pcanytime.co.nz
Cartoonist – Louis Decrevel
Website: loueee.com
legal backup requirement, given that there’s power floating around inside.
I’m always very wary of breaking clips when disassembling devices – many modern laptops and monitors are
renowned for having very flimsy (possibly intended as
single-use) clips holding everything together. There’s nothing wrong with the method itself, but on many devices, it
reeks of the “no user-serviceable parts inside – not intended
to be repaired” philosophy.
Regardless, I got it open. As I suspected, a single PCB
took up the majority of the room inside the base. A short
wire lead from the tank assembly was plugged into the
PCB via a connector, and this had to be removed before the
two parts could be separated. I set the tank aside for now.
The board was screwed to the base with the external
buttons toggling standard small SMD switches positioned
around the board’s edge. Power to the device is via a phone
charger-style plugpack and a standard 3.5mm barrel connector at the end of a one-metre cable. The power supply
connects to a socket mounted into the plastic base.
The pick of the plugpack
The connections to the socket were easy to get to, so my
first task was to plug the barrel jack into the socket, plug
in the supply and test the voltage coming from the socket.
With my multimeter across the contacts, I got a reading of
exactly nothing; there was no power getting to the socket.
I re-checked that I had actually plugged the supply in
properly, and there was voltage at the power board on my
test bench (I’ve been caught before by first not ruling out
the basics!). Other devices were running from the power
board powered on OK, so it was time to check the power
supply output.
Testing barrel jacks is always a bit of an act, especially
when the meter probe is too large to slide down the centre
contact. I use part of an old dental pick that broke off years
ago; being tapered down to a point, it is a universal fit into
almost all of these smaller barrel jacks. Once in place, it is
much easier to just hold the meter probes against that and
the outer contact.
Top tip – ask your dentist next time you visit for any
old picks and probes – they are the handiest things for all
electronics tinkering, especially SMD placement and other
delicate work!
This time, I measured 5.2V, close enough to the 5V listed
on the product labels. So, power was coming out of the supply but not reaching the output of the jack socket.
I flipped the whole thing over so I could eyeball the socket
more closely. Looking at both the plug and the socket with
my loupe, the plug looked fine, but there was something
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in the socket. The plug didn’t feel secure and looked to be
protruding slightly, even when pushed as far in as I could.
With a light beamed into the socket, I could see what
looked like a piece of plastic in the way. I used another
of my handy dental picks to fish around, and the plastic
moved when I touched it. It seemed to be right around the
centre pin of the socket.
Flipping it all back over, I used the time-honoured
method of shaking things loose by holding the base in my
right hand and clapping it down into the palm of my left
hand, in the hope the sudden stop would dislodge the foreign object and gravity would do all the work for me. I did
this several times and could see the plastic was moving.
The piece came out with a bit more probing with various
picks and tweezers and a few more soft taps. After plugging the power source back in – noting this time it went
all the way in – I measured the same 5.2V at the socket
connections. The clock display lit up a very nice blue and
happily flashed 12:00, so I knew I’d found the problem and
that now it was going to work.
The debris prevented the power jack from going all the
way in, so no contact was made. I’d save trying the diffuser
part for when it was all back together.
Quality assurance backfires
On closer inspection under a magnifying glass, the plastic ring turned out to be the top part of the insulation ring
separating the two contacts of a barrel jack plug. The plug
on the supply that came with the unit was intact, so I can
only assume that a QA tester used a single power source to
quickly test all the diffusers coming off the production line.
My guess is that they pulled that power plug out, leaving the last bit of the ring behind. They might not have
even noticed it for a while, and by then, they wouldn’t
know where the piece had gone. My client had drawn the
short straw!
While it was apart, I looked at the other components. I
was most interested in the diffuser itself and had no idea
how it worked until I started looking into it. I assumed heat
was involved, which vaporises the oil and water mix, creating the stream of ‘steam’. Not so, or at least not in this one.
Australia's electronics magazine
January 2023 97
Some nebulisers operate that way, but they are usually
found only in high-end medical devices. These so-called
homeopathic diffusers for domestic use utilise ultrasonics;
no heat is involved.
An ultrasonic disc transducer is mounted in the centre at
the bottom of the water reservoir. When power is applied,
ultrasonic waves vaporise the oil and water in the tank and
the specially shaped funnel corals it all into a nice stream
of scented vapour. Safe and very clever!
Editor’s note – they are basically the same design as
ultrasonic humidifiers; the ‘steam’ generated is actually a
cloud of tiny water droplets that quickly vaporise unless
local humidity is very high.
Once I had it all back together, I filled it with water to
the embossed mark on the side of the reservoir and added
some ‘essential oil’ I’d had stored for years. I originally
used it with a different type of scented oil diffuser, which
used a simple tea-light candle to heat a ceramic bowl containing the oil.
With the funnel back in place, I hit the button and a
fine stream of mist poured from the top of the outlet. It is
surprisingly powerful, totally cool to the touch and very
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Silicon Chip
fragrant – though I think I used a few too many drops of oil.
It turns out these are very efficient and only need a few
drops for a full tank of water (roughly 200mL on this model),
depending on the concentration of the oil and the scent
itself – some scents are far stronger than others.
I set the clock and messed around with the sounds and
the timer function, and it all checked out OK. So, a relatively simple fix then; it would be interesting to see what
was happening with this other one, though, because it had
apparently been in use for quite a while but now didn’t
work ‘properly’. Plus, it had been dropped.
Diffuser #2: Electric Boogaloo
The client brought that second diffuser in a few days later
and I asked him to be more specific about how it operated
before it had been dropped. He said it worked fine at first,
but the output had reduced significantly of late. As it just
wasn’t as good as it used to be, they had stopped using it.
This model was quite a bit different than the last one; it
didn’t have anything as fancy as a clock, timer and sounds,
but it did have RGB lighting, controlled by a single pushbutton switch that toggled between the different colours
and modes. Ominously, it rattled when I lightly shook it,
so something had come adrift inside. I’d have to open it
up to see what was going on.
The funnel on this model also pops off easily for filling, and I could see a problem straight away; there was
a small plastic coin-sized disc sitting in some sludge
at the bottom of the empty water tank. I set that to
one side. The whole inside of the tank, funnel and
recessed ultrasonic transducer was covered in a
thick film of oil residue. It did smell nice, though!
I’d need to clean it out properly at some point,
but in the meantime, I used a paper towel to wipe
as much of it out as possible.
There was still something loose in the base
somewhere, so that had to come apart. This time,
I encountered three ‘security screws’ holding the
bottom to the tank stage. Fortunately, I now have
a good collection of bits that undo these fasteners,
so it only slowed me down a little.
With the screws out, the two sections came apart
Australia's electronics magazine
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easily. I also had to unplug the transducer lead from the
small circuit board inside to separate the parts fully.
I could see a fan had come loose in the base and was floating around on its wiring. It had been screwed to two plastic
posts, which had come adrift; they were still screwed to
the fan. I left it all as it was and placed the fan back where
it should be. The broken-off parts matched up very well,
so I decided to glue it back into position.
Everything else in there looked OK – there really wasn’t
much to see. A strip of SMD LEDs was mounted in a ringshaped moulding around the inside of the base and hardwired into the PCB. All seemed OK, so I plugged the diffuser
in and tried it. The fan spooled up and the lights came on
and changed colours when I repeatedly pressed the button.
I’d have to plug the ultrasonic transducer back in and
fill the tank with water to test it properly, but I felt sure it
would work after I gave it a thorough cleaning. So I went
ahead and glued the fan back in with 24-hour epoxy; I
didn’t want it moving again.
While that set, I took the tank and funnel assembly inside
and used a good detergent to clean the inside and outside
of both parts. The transducer appeared to be glued to the
bottom of the tank, so I wasn’t about to disturb that, but I
used an old toothbrush to give the recessed, visible part
of it a very good clean.
I reassembled the diffuser, filled it with water and added
a few drops of oil. I put the funnel back in place and hit
the button. Instead of a nice stream of vapour, I got water
spitting all over the place!
The sharper knives in the block among you will recall I
found a small, coin-shaped plastic piece lying in the tank.
On closer inspection, I could see where this baffle had broken away from the inside edges at the top of the funnel.
After fiddling it back into position, I tacked it with instant
glue. On testing, it worked perfectly, so I glued it properly
with epoxy. Job done then, and two happy clients.
An example is a Linden L55UTV17a TV I looked at. It has
six strips each of 15 LEDs connected in series, as shown in
the photo below. I tested these with an LED backlight strip
tester, and only three of the strips were OK.
I also looked at an LG 49LB650 TV. LG uses a higher current in the backlight strips, which causes them to go blue
after a while. This gives a blue cast to the picture. In this
case, one of the LEDs had burnt and actually damaged the
strip. With LG TVs, it is best to replace all the strips when
they fail; AliExpress has a good range.
Newer TVs divide the backlight into sectors. The Hisense
50P7 has eight sectors, and the power board that drives the
backlight is now on the serial bus, so the board is more complex. Similarly, the LG 75 NANO86 power board is also on
the serial bus and drives 12 LED strips. Due to the more
complex power boards, it is becoming more challenging
to determine if the main board or power board is faulty.
Most TV repair places deem it uneconomic to replace
backlight strips due to the time involved and the risk of
breaking the LCD panel. Still, it is worth a try if you are
doing it to fix your own TV. Up to about a 55in (140cm)
TV, you can, with care, be successful.
First, from the circuit board side, very carefully disconnect the long board that connects to the LCD panel ribbon connectors. Then turn over the TV and remove the
screws holding the retaining edge around the panel. Do
not do this from the circuit board side, as you will probably break the panel.
Remove the panel very carefully, taking care not to flex it
much. Put it aside. Then take off the retaining edge around
the sheets of plastic that diffuse the light. Put the sheets
aside, keeping them in order.
You are now at the backlights. Test them with a backlight tester (available on eBay) to determine the faulty
strip(s). See if you can buy replacement strips on eBay
or AliExpress. Re-test before reassembly.
Tips on fixing LED TV backlighting
An unfortunate series of battery chargers
R. S., of Figtree Pocket, Qld has found that LCD TV LED
backlighting can be troublesome. Still, if it fails, it generally
can be fixed, and he has some good tips on how to do that...
The change from cold cathode backlight tubes to LED
strips for LCD screens was supposed to be an improvement,
but they seem to be less reliable. Many newer TVs will not
turn on if a backlight fault is detected.
J. B., of Burpengary, Qld sent in a saga involving two
battery chargers and a seemingly never-ending series of
faults, trials and tribulations...
The chargers in question are Truecharge 20i (TC20i) models made by Statpower (now Xantrax). They are rated at
20A 12V with three stages and can simultaneously charge
two batteries of the same chemistry semi-independently.
Two small slide switches select between flooded and gel,
and three temperature ranges on the front face: cold, warm
and hot. Charging and float voltages are listed for each range
for both flooded and gel cell batteries. The charging voltage
has a range of 13.8-14.8V and float 13.1-14.2V, both in 0.2V
increments. Not ideal for some chemistry types.
An eventual upgrade to lithium-ion will need a revisit
of what to do, but I only have flooded and AGM at this
present time.
Two extras are available: a battery temperature sensor
and a remote panel. With a temperature sensor connected,
the front panel temperature switch is ignored. They connect via two RJ12 6P6C sockets.
The three charging stages are the usual bulk, absorb and
float. A hidden fourth stage (equalise) is accessed by holding down a small recessed button on the front face with
a narrow pointed object, eg, a straightened paperclip, for
two seconds.
This Linden L55UTV17a TV has six strips of 15 LEDs
arranged horizontally and connected in series.
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Australia's electronics magazine
siliconchip.com.au
There are also charging and charged LEDs and an overall
current readout in 4A steps on the front face. Short-circuit
and reverse polarity protection are built in, the latter via a
pair of 30A blade fuses, one for each battery.
I will shamefully admit I have blown more than one fuse
while using these chargers. The first charger saw service
in an ambulance. It was used while parked at the station
to keep both the start and house batteries topped up. The
house battery runs a small custom-made fridge with strict
temperature control to keep drugs in.
While going out to a job under lights and sirens, this particular ambulance caught fire in the electrical enclosure due
to a flasher unit being under-rated for the task required. The
boss was told about the flasher unit but chose to do nothing about it till this fire happened. A recall was issued so
the flasher units could be replaced.
Firefighters seem to completely disregard the fact that
electronics don’t like being doused with water. This particular charger copped an absolute drenching.
This ambulance eventually found its way back to our
workshop for repair. No doubt there was a big argument over
who would pay for the repairs. The whole electrical enclosure and other fire-damaged parts were removed and stored.
Before it was all dumped, I managed to retrieve the charger and a 12V to 240V inverter. There was also a remote
panel for the charger, but all that was left was the bare
board; everything else was gone: the solder mask, the copper tracks, even the vias.
The remote panel has a line of LEDs for each battery to
show the battery voltage in 0.5V increments and five LEDs
to show the overall current. Two LEDs also indicate the
charging and charged states.
The inverter was a modified square-wave type. I used
it only a handful of times over 14 years until it gave out.
Once home, a cursory inspection of the charger showed
that the IEC inlet socket had the melted remains of the
plug in it, and there was a small amount of fire damage to
the aluminium cover next to the socket. A screw was also
missing that held the socket to the cover. It appears that a
lot of heat was next to that screw, and it melted the plastic
housing so that the screw fell out.
The charger is mostly made from a long U-shaped finned
aluminium section that is also the heatsink. A long, thin
hat shape made of sheet steel fits over the top and ends and
has flanges to mount the charger vertically to a wall. It has a
small circuit board to hold seven LEDs, two slide switches
and a recessed push button. A ribbon cable connects this
panel to the main board near the processor.
Removing the top cover revealed that the inside was surprisingly clean. The only thing to do was to remove what
remained of the IEC plug and give it a go. It worked straight
away, much to my delight.
Some six months later, I was charging a battery in the
carport when a heavy downpour came through. I didn’t
know at the time that the carport leaked water during heavy
rain. Naturally, the charger was right under the leak, and
it protested the impromptu shower by ceasing operation.
It was time to remove the top again and see what damage
had been done. Removal of the circuit board requires the
disconnection of five clamps that hold large heat-generating
components, four screws that hold two tabs at either end,
and one Earth wire to be undone from the heatsink. The
board then slides out.
siliconchip.com.au
Australia's electronics magazine
January 2023 101
Two small-signal transistors had their sides blown out,
removing most of the type numbers. There were also some
black marks around one of the two IRF840 Mosfets, a blown
4A fuse and a slightly blackened and cracked resistor.
The first order of business was to try to get a circuit diagram. The internet revealed nothing, so I sent an email to
Xantrax. Their response was to send money plus charger
plus return postage. At the time, the exchange rate was not
in our favour; it would have cost as much as a new one to do
that particular activity. The only remaining option was to
figure out what the blown parts were and hope for the best.
Looking closely, I discovered that only two small-signal
transistor types were used throughout the whole charger:
2N2222A and 2N2907A. There was one of each type next
to the two blown ones, and the circuits appeared to be the
same as both pairs drove the gate of their associated IRF840.
So I felt sure I knew what to replace those transistors with.
There is also a UC3845A controller chip (U1) that I felt
should be replaced. There are two opto-couplers as well,
but figuring out their types was an arduous process as the
markings were very hard to see, even with my strongest
magnifying glass.
After an hour of researching possible type numbers,
looking yet again using different light sources, and getting just the right angle of reflected light, I finally found
both to be 4N25s.
After replacing all the above and the 47W resistor plus
the fuse, I fired it up only to reveal that the charger would
go through its boot-up sequence but not put any current
into the battery. Something wasn’t right.
I spent a lot of frustrating time trying to locate the problem. Measuring everything in-circuit didn’t show anything
out of order. Eventually, I gave up, put the charger away
and waited for inspiration to hit. About six months later,
while looking for something else, I came across the charger
and pulled it out again to have another look.
This time, I measured the three 0.1W 3W resistors out of
circuit. One of a paralleled pair was open-circuit, which
I very much later discovered is part of the current sense
circuit. I found a suitable resistor in an old CRT monitor.
Replacing it finally fixed the charger (again!).
Buoyed by that success, I noticed a second identical charger gathering dust in the storeroom of my then-employer.
I asked if I could have it as it wasn’t working. After fixing
one, how hard could another be?
Opening it revealed the same two burnt transistors. I
replaced all the same parts except for the 47W resistor, but
I did have to replace one of the 0.1W 3W resistors. Switching it on without a battery connected, it went through its
usual power-up sequence, and no smoke escaped.
After connecting a battery, however, it was a different
story. Much fire and brimstone issued forth as soon as the
startup sequence completed and current was applied to the
battery. “Oh, dear!” I shouted, or perhaps a slightly less
polite word to the same effect.
I was now trying to do things on the cheap by leaving parts out and powering on or not replacing parts that
I should have. It resulted in a growing pile of blown-up
silicon, much smoke venting into the atmosphere, many
sparks and damage to heavy tracks. Smarter people would
know that switchmode supplies require all parts present
and working, but Muggins here is a slow learner.
After the fifth time, I decided to replace all the silicon
parts listed above and, while I was at it, fit a socket for the
controller chip. I also replaced three 15V zener diodes.
After that, finally, the charger fired up properly. I then
reassembled it and tested it for three months by running
a 12V fridge connected to a small lead-acid battery before
declaring it fixed.
Unfortunately, on the first camping outing to the “outlaws” (wife’s parents) with this charger, Murphy found
us overnight and hit the charger with some strange ‘stop
working’ spell. “Bother!” I said quite loudly (and perhaps
not so politely).
Back home, investigations revealed that the startup resistor (220kW 1W) had gone high in value. I didn’t have one
on hand and couldn’t find one in my pile of disassembled
bits, but I made a close facsimile from two 470kW 0.5W
resistors in parallel. Once again, it worked as it should.
This charger subsequently travelled across some of the
worst roads in Australia on various camping holidays for
several years till Christmas 2011, when I went camping on
the largest sand island in the world.
For this trip, we bought a small 720W two-stroke generator from a large hardware chain. Its voltage is regulated
by adjusting engine RPM. It was backup if the sun decided
to hide during the day. It also has a dedicated 12V output
for battery charging.
Two 35L 12V fridges (actually one fridge, one freezer)
take a heavy toll on batteries. So for this trip, I set up two
batteries dedicated for both fridges and brought both chargers, figuring I could run the generator half the time.
Murphy must have followed me or disguised himself as
a dingo as there was very little sun to keep my solar panels
busy. I was forced to use the generator. Well, things didn’t
go to plan as some 20 minutes after starting the charging
process, the generator suddenly started to labour. I quickly
determined that the second charger had stopped working.
A close-up one of the
Trucharge 20i battery
chargers. The main PCB
suffered some water
damage.
102
Silicon Chip
Australia's electronics magazine
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with LEDs
• 1.75x, 2.25x & 3x magnification
• 60 LEDs with high/low brightness
• Mains powered
FULLY
ADJUSTABLE ARM
ONLY
119
$
QM3554
ONLY
2995
$
RECORD & SNAPSHOT
FEATURE FOR A BETTER VIEW
LED Headband Magnifier
• 1.5x, 3x, 8.5x 10x magnification
• Can be worn over eye glasses
LARGE 4.3" COLOUR LCD
QM3511
720P WITH
ILLUMINATION
LED
ILLUMINATION
ONLY
12
$
95
Handheld Magnifier
• 3x magnification
• Lightweight, just 200g
Inspection
Camera
• 3x magnification
• 3 x probe attachments included
• Add an SD card to record vision
or snapshots
QC8718
QM3535
ONLY
199
$
Shop at Jaycar for:
• Eye Magnifier
• Handheld Magnifier
• Headband Magnifier
• Desktop Magnifiers
• Inspection Cameras
• Digital Microscope
Explore our wide range of magnifiers & inspection aids, in stock on
our website, or at over 110 stores or 130 resellers nationwide.
jaycar.com.au/magnify
1800 022 888
Prices correct at time of publication but are subject to change. Jaycar reserves the right to change prices if and when required.
I later discovered, to my disappointment, that if the separate battery charger option on this cheap generator was used,
the AC voltage the generator puts out goes up to 265V AC.
Oh well, at least one charger was still working. I kept a
close eye on the output voltage and managed the RPM for
the rest of the time on this island.
Once back home, I discovered that everything inside the
charger looked pristine. The generator didn’t have the wattage to blow the fuse or let the smoke out. Investigations
revealed that the IRF840s were both shorted, as were the
gate driver transistors and the UC3845 switchmode controller. I also decided to replace the opto-couplers and the
zener diodes.
I checked the resistors and the capacitors in-circuit with
my multimeter and they all appeared to be OK. However,
upon firing it up after replacing the semis, nothing happened whatsoever. I then spent several weeks trying to find
out why and replacing many components all over the high
voltage section, none of which helped.
I finally made voltage comparisons with the other charger
on each pin on the UC3845. All voltages were very close to
each other except pin 7, which measured 10.5V. This pin
is fed directly from the startup resistor and a winding on
T2 via a simple regulator. It should have been above 12V.
Was it a load or supply problem? Around this time, I
drew up a circuit diagram to work out what was going
on (reproduced below). I discovered that the two high-
frequency transformers are identical, but only one has its
feedback winding connected.
I swapped U1 over, but again, it made no difference.
Replacing C27, C28 and C29 made no difference. Replacing
R5 and R26 again drew a blank. In desperation, I fed 12V
from a small battery directly to pin 7 of U1. To my surprise,
the charger fired up and proceeded to work as it should.
I could remove the small 12V battery once current was
supplied to the battery, and the charger would keep going.
Every 15 minutes or so, the charger would stop for about
five seconds to, I assume, read the battery terminal voltage before continuing to charge it. It was at this point that
the charger would stop dead. Feeding 12V to pin 7 would
once again bring the charger back to life.
This proved that the feedback from T2 was working, but
the startup resistor wasn’t supplying enough current. Or
was it? Once again, I replaced R5, but it made no difference. In desperation, I started to replace the small capacitors
around U1. C21 broke apart while removing it. Replacing
it was the answer to all the troubles. But why?
The UC3845 (IC1) has a 5V reference available at pin 8.
It appears that C21 was drawing more current that the 5V
reference could supply, and at startup that was keeping
the supply voltage below the threshold required to start
the chip. During charging, extra current from the feedback
winding provided the current required.
We gave away that generator and now have an inverter
generator to run the chargers. Both ran flawlessly for over
10 years. The first charger recently developed a problem
where it would go through its startup sequence, then reset
and repeat in a continuous loop. Even activating the equalisation mode didn’t stop this behaviour.
I just hoped it wasn’t the processor, so I swapped it from
the second one. The problem stayed with the first charger.
Looking closely, I could see a white film all around the processor but couldn’t get in there to clean it. Removing both
RJ12 sockets revealed a white film under them. A good clean
and reassembly was the fix. It appears that the drowning
SC
close to 20 years ago finally showed itself.
A reproduction of the selfmade circuit diagram for
the battery charger
104
Silicon Chip
Australia's electronics magazine
siliconchip.com.au
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