This is only a preview of the June 2023 issue of Silicon Chip. You can view 38 of the 112 pages in the full issue, including the advertisments. For full access, purchase the issue for $10.00 or subscribe for access to the latest issues. Items relevant to "Basic RF Signal Generator":
Items relevant to "Loudspeaker Testing Jig":
Items relevant to "WiFi Time Source for GPS Clocks":
Items relevant to "Wideband Fuel Mixture Display, Pt3":
Items relevant to "Servicing Vibrators, Pt1":
Purchase a printed copy of this issue for $11.50. |
servicing, repairing and replacing
While this article is primarily concerned with servicing a V6295-type vibrator, the
general advice would apply to many mechanical vibrator units found in vintage radios
and other contemporary equipment, mainly those with three sets of contacts. I will also
present a straightforward Mosfet-based circuit that acts as a solid-state replacement for
a vibrator. It even fits in an original-looking can!
Part 1: by Dr Hugo Holden
T
he inspiration for this article was
my NZ-made ZC1 Mk2 military
communications radio, designed to
run from a 12V battery.
Like many battery-powered radios,
the HT supply was provided by an
electromechanical switching device
with a vibrating reed and contacts
known as a split-reed synchronous
vibrator (or just ‘vibrator’). In this case,
it is a 7-pin unit, type V6295. The circuit of the “vibratorpack” power supply is shown in Fig.1. The vibrator is
within the circle; the other components are external to it.
The V6295 has a pair of contacts to
switch the primary winding of transformer T3 and another pair to switch
the secondary winding for synchronous full-wave rectification. One extra
contact in the unit is used to switch
the magnet coil on and off, to sustain
mechanical oscillations of the vibrating reed at around 100Hz.
This system was quite efficient, as
the coil in the unit only consumed
about 2W, and the contacts, when
closed, had very low resistance. However, in common with all mechanical contacts which switch an inductive load, the contacts wear and burn,
degrading after tens to perhaps 100
hours of use. Another significant problem is due to the latex rubber inside
the unit, described later.
There are numerous articles on how
to repair the V6295. It involves cleaning the contacts of all oxides, ensuring
their surfaces mate in perfect opposition when they close, and adjusting
the contact gaps.
The small contact for the vibrating
reed is usually adjusted for maximum
oscillation amplitude, consistent with
good starting; however, it also has a
role in very fine adjustment and contact switching symmetry.
If the primary side contact gap is too
Fig.1: the ZC1 Mk2 radio power pack with the V6295 vibrator
in the centre. The 12V DC supply from the battery at lower
right is converted to a 200V+ HT output on the left, mainly
due to the interaction of the vibrator and transformer T3.
86
Silicon Chip
large, the power pack output voltage
drops off as the duty cycle is reduced.
If too narrow, the contacts arc over. In
addition, if the contact gap is too large,
there is an excessive voltage overshoot
on the leading edges of the transformer’s primary winding connections.
The primary contacts must also have
a slightly longer duty cycle than the
secondary contacts and overlap when
the secondary contacts are closed –
see Fig.2.
Thus, there is a brief time when no
contacts are closed, and the transformer’s field is collapsing. The transformer’s tuning capacitors are chosen so
that the voltage overshoot is as low as
possible, thereby minimising the contact arcing and voltage spikes.
Restoring an original V6295 vibrator (or a similar type) involves four
main steps. The first is checking its
mechanical integrity and, if necessary,
performing any repairs. The second is
Fig.2: the secondary contacts are closed for a shorter
duration than the primary contacts, and there is a gap
between one set of primary contacts opening and the
other set closing. Correct timings and symmetry are
essential for reliability and low output ripple.
Australia's electronics magazine
siliconchip.com.au
Photo 1: an extension socket like this is
invaluable for checking and adjusting
vibrators. The loops in the wire make
it easy to attach oscilloscope probes.
Photo 2: the vibration-dampening natural rubber parts of the V6295 are its
downfall. They degrade over time, fouling the contacts.
static contact adjustment, while the
third is dynamic contact adjustment.
The final step is using an oscilloscope
to check that it works perfectly. Let’s
take these one by one.
metal surfaces of the contacts oxidise
from being exposed to air, and metal
oxides are insulators. Also, any contact
arcing produces very corrosive gasses,
which are trapped inside the housing.
#1 mechanical considerations
Restoration
Suppose you don’t have an extension plug/socket to support the unit
while out of its housing and making
adjustments, simultaneously giving
you access to the electrical connections. In that case, you will need to
make one. Mine is shown in Photo 1.
The V6295 needs to be in a condition where it can be disassembled and
reassembled without damage.
Surprisingly, the main reason a
V6295 will not run after a period of
storage is due to the latex rubber inside
the housing, not contact oxidation.
However, the latter is also a factor over
longer time frames.
As latex (natural rubber) ages, it
melts and turns into a tacky brown
liquid, then a vapour – see Photo 2. In
a closed container such as the metal
housing, the liquid goes into equilibrium with the vapour. The vapour is
deposited as a sticky brown liquid on
the contacts as months and years pass.
High storage temperatures speed up
this process.
For example, an immaculately
cleaned and adjusted V6295 was put
into storage. Two years later, it would
not run. Taking it out of its housing
again, brown deposits had appeared
on all the contact surfaces, insulating them and causing them to stick
together. This material is identical to
the areas of melted latex. Therefore,
all this old latex needs to be replaced.
Even without this latex problem, the
The best way to remove a V6295 or
similar vibrator from its housing is by
gently prising up the zinc material,
working around the can very slowly
until the lip is unfolded. Next, carefully smooth it to remove any marks.
You can replace the rubber inside
the unit with various soft, rubber-like
products that do not break down as
quickly. One example of a very stable,
soft material that can withstand high
temperatures without breaking down
is silicone. It isn’t rubber (which comes
from a tree), even though people often
refer to anything with similar properties as ‘rubber’.
One thing to note is that the zinc
canister is a little short, and there
is only a minimal amount of room
between the mechanism’s top surface
and the inside of the zinc case top area.
A 1-1.5mm thick silicone rubber sheet
is suitable for this top area. For the
remainder, the material from an ordinary 4mm-thick soft Yoga mat (usually
PVC foam) is suitable and easy to get.
When the old latex is removed
around the base area, it frees up a
siliconchip.com.au
metal washer that can be separated
from the base by a new felt washer
(green) shown in Photo 3. When the
unit is reassembled, it is important that
you can feel the mechanism shaking
back and forth in the housing when
held upright.
Excessive mechanical coupling of
the mechanism to its housing results in
mechanical vibrations being coupled
to the entire radio, making it noisy.
#2 contact cleaning and static
adjustments
First, clean any latex deposits off
with contact cleaner, passing paper
strips between the contacts. Clean
them further with a fresh piece of
15mm-wide 800 grit abrasive paper
folded in half, with a sharp fold, placed
between the contacts. With gentle pressure closing the contacts, both faces
are cleaned simultaneously. A final
wash with contact cleaner is required
to remove any fine debris.
Never file the contacts under any
circumstances, as this ruins their flat
faces, and it will not be possible to
have a unit with good output and any
longevity after that.
It is essential that the mechanical
alignment of the contacts is such that
when their faces meet, their entire surface areas are touching, and the faces
are parallel, as shown in Photo 4.
Felt washer between
metal washer and base
Australia's electronics magazine
Photo 3: a silicone
rubber disc and pieces
cut from a PVC yoga
mat replace the natural
rubber and are much
more stable over time.
June 2023 87
Photo 4: before adjusting the contact
gaps, ensure the contacts are clean
and close to perfectly parallel.
Photo 5: here I am operating the
vibrator in the radio (in this case, a
ZC1 Mk2 communications receiver)
to test it before replacing it in its
metal can.
You can now make the static adjustments. A first approximation of contact settings is achieved by setting their
gaps to 0.1-0.15mm for the primaries
and 0.22-0.28mm for the secondaries.
#3 dynamic contact
adjustments
The best results can only be obtained
from the V6295 after a dynamic contact
adjustment. This involves running the
unit out of its housing while monitoring three things with an oscilloscope
and voltmeter. The points to monitor
are the primary connections on the
transformer, the DC output voltage and
the ripple voltage at the filter output
(the left end of filter inductor L9B in
the case of the ZC1; see Fig.1).
Photo 5 shows a V6295 running via
the extension, taken at a moment when
the vibrating arm was deflected. A pair
of secondary contacts can be seen to be
closed, with the other pair wide open.
When the primary contacts are correctly set, each contact is closed for
a nearly identical period. You can
place a slight bias pressure on the
contact (with a plastic tool, be mindful of the voltages) to check the effect
while viewing the scope. It is important to only deflect them close to their
bases, to keep the contacts as parallel
as possible.
If both the primary contacts are too
closely or too widely spaced, arcing
will be seen between them. If there
is asymmetry, one will have a slight
arc and the other not. A minor adjustment on the vibrating reed contact can
correct the centring of the mechanical motion. More significant corrections must be made by moving both
contacts.
There are the contact gaps to consider, plus the symmetry of opening
and closing comparing one contact
to another. Scope 1 shows the waveforms with correct primary contact
adjustments, with the scope probes
connected to pins 6 & 1 on the V6295,
effectively across the transformer
primary. The time that each contact is
closed, t1 & t2, is in the order of 4ms.
When the primary contacts are
closed, the voltage on the corresponding trace is 0V. You can see that the
periods are very close to equal in this
case (t1 = t2).
Scope 2: if the secondary contacts
are not adjusted correctly, the ripple
on the DC output will vary on every
second pulse like this.
Scope 3: when the secondary contacts
are correctly adjusted, the DC output
ripple will be reduced in amplitude
and more consistent, as shown here.
Secondary adjustments
The secondary contact spacing and
symmetry profoundly affect the ripple
voltage superimposed on the DC output (as well as the DC value itself). If
the secondary contacts are too closely
spaced, arcing and flash-over occur.
Again, the effect on the ripple voltage
can be seen by placing a slight bias on
the contact with a plastic tool while
the unit is running.
Scope 2 shows when the secondary contacts are out of adjustment,
resulting in a very asymmetrical ripple voltage. That is with 11.6V DC
into the vibratorpack’s input, the
sender switched on and the ZC1 in
receive mode RT. Scope 3 shows the
t1
t2
Scope 1: probing the two primary
contacts in the vibrator (which
connect directly to either end of the
transformer primary) should reveal
a symmetrical waveform. If it’s
asymmetric, adjust the contact gaps.
88
Silicon Chip
Australia's electronics magazine
siliconchip.com.au
Scope 4: with the two transformer primary waveforms
(middle and bottom) along with the DC output (top), we can
see that the secondary contacts close for shorter periods
than the primary contacts.
correct adjustment of the secondary
contacts, resulting in a symmetrical
ripple voltage.
Scope 4 is a triple trace, showing
both the primary voltages and the output ripple with a well-adjusted V6295.
Note how the time that the primary
contacts are closed is a little longer
than the secondary contacts due to
the wider secondary contact gaps. The
multiple overlaid traces is an artefact
of the photographic timing.
Scope 5 shows an electronic V6295
replacement plugged in place of the
mechanical V6295. This unit runs at
60Hz rather than 100Hz and makes
for an interesting comparison. Notice
the absence of spikes and transients
in the electronic unit and the differently shaped ripple voltage, which is
still about 2V peak-to-peak.
Scope 5: with a Mosfet-based vibrator replacement instead
of the mechanical V6295, the waveforms are somewhat
cleaner (at 66Hz rather than 100Hz), but the DC ripple on
the output is similar in magnitude.
two Mosfets, is among the easiest to
build, works exceptionally well and is
quite efficient, being slightly more efficient even than the mechanical type
(which has a standing power draw of
around 2W).
If you don’t have an existing housing suitable for this device (eg, taken
from a failed mechanical vibrator),
you can use a readily-available round
aluminium housing. This commercial
air intake pipe joiner, 75-76.2mm (3in)
long and 38mm (1.5in) in diameter,
is available on eBay – see Photo 7. It
uses a standard Amphenol 7-pin base,
also usually available on eBay, shown
in Photo 8.
This unit produces very clean
switching waveforms and will start
from voltages as low as 8V, even when
the supply is loaded. Unlike units
driven by independent oscillators, it
does not require a tuning capacitor
on the transformer primary. Also, it
is intrinsically short-circuit protected
because if the supply is overloaded
and oscillations stop, both Mosfets
turn off.
The circuit is shown in Fig.3. Two
Mosfets replace the primary contacts of the vibrator, while pairs of
series-connected BY448 1500V diodes
replace the secondary contacts.
This might seem like overkill, but it
#4 reinstallation
You can solder a brass wire ring into
position to re-fit the unit to the housing, as shown in Photo 6. This way, it
can easily be removed later for more
repairs/adjustments. Do not re-crimp
the zinc can, or it can only be cleaned
and repaired once, as the zinc casing
will fracture.
Solid-state vibrator
replacement
I have built several different solid-
state circuits to replace a mechanical
vibrator, including two using Mosfets, one using Darlingtons and one
using bipolar transistors. The one
presented here, using little more than
siliconchip.com.au
Photo 6: the vibrator can be held in its
can using a C-shaped piece of brass
wire. This makes it much easier to
open again later.
Photo 7: the vibrator replacement
looks very similar to an actual
vibrator, but is made from all-new
parts. If you have a defunct vibrator
in a suitably-sized can, you could
possibly reuse it (and maybe its base).
Australia's electronics magazine
June 2023 89
OD = 35.3mm
ID = 29.4mm
Height = 8mm
Photo 8: the spacer is held in the centre of the base/plug with a 10mm CSK M3
screw, and the PCBs are, in turn, held to the spacer using two M2 machine
screws through holes drilled in it. The cylindrical spacer is used to attach the
can to the base.
Scope 6: the Mosfet-based vibrator
replacement generates waveforms
with rounded edges, as they do not
switch super fast (to avoid RFI).
is necessary to have a very high PIV
(peak inverse voltage) diode rating. If
the unit is unplugged while running
(or there’s a bad connection to one of
its socket pins), the undamped collapsing field of the main vibrator transformer can produce a peak voltage high
enough to break down and destroy a
single 1N4007 rated at 1000V.
Each Mosfet is switched on by a positive spike coupled from the opposite
end of the transformer when the opposite Mosfet switches off. This pulse is
coupled via a 470nF capacitor with
a 1.6kW series resistor. The Mosfets
switch off after a defined time due to
the gate discharge resistors; the result
is alternating oscillation.
10nF gate-drain capacitors and
300W gate resistors slow the switch-on
and switch-off times of the Mosfets to
prevent RFI, while 18V zener diodes
prevent the gates from exceeding their
±20V Vgs ratings.
When one Mosfet switches on, the
rapid drop in its drain voltage will
couple through to the gate of the other
Mosfets switch more-or-less simultaneously.
The fact that the coupling capacitor
values are relatively low (under 1µF)
assists in making a unit that will slide
easily inside the pre-made 38mm aluminium tube, a similar size to a standard vibrator can.
Mosfet via the 470nF capacitor and
1.6kW resistor, ensuring it switches
off simultaneously. The exact oscillation frequency will depend on the
transformer characteristics.
Scope 6 shows the drain voltages
with the unit in operation in the ZC1
in receive mode, while Scope 7 shows
the gate voltage of one of the Mosfets
when conducting. The 470nF capacitor charges via the fellow Mosfet’s
drain voltage (24V) and 10kW gate
resistor until the charge current drops
off and the gate voltage approaches the
threshold Mosfet’s voltage.
By that time, some transformer
core saturation is beginning, so the
feedback rapidly falls away, the Mosfet turns off, and the fellow Mosfet is
driven into conduction. The unit runs
at 66Hz in my set.
Looking closely at the switching
transitions on the transformer primary
(drain connections) at 10V/div (Scope
8), they are free from radio frequencies and excessive voltage overshoot
with this circuit. You can see how the
Construction
Various Mosfets will work in this
circuit. While I used TO-3 case versions, TO-220 case versions could be
used with some lead bending, such
as the ubiquitous IRF540N, available
from Jaycar and Altronics. Suitable
TO-3 case Mosfets include the IRF130,
IRF230, IRF350, 2N6756 and 2N6758.
The 2N6758s made by Harris, available on eBay, are particularly good
quality.
It is based on two small, simple
PCBs that sit back-to-back, as shown
in Fig.4. They are not identical but
very similar, with the only difference
being the routing of one track. The
holes for the components all fall on a
Fig.3: this self-oscillating
Mosfet-based replacement for
the vibrator is nice and simple,
needing just two Mosfets, four
regular diodes, two zener diodes
and 10 passive components.
The properties of the external
transformer set the oscillation
frequency to around 66Hz.
Note that the 18V zeners were
20V types in the original design
but the voltages have been
lowered slightly to allow for
part tolerances.
Photo 9: the base with the tapped spacer,
BY448 diodes (note that the other two diodes
are hidden inside the holes in the plug pins) and
tinned copper wires already attached.
90
Silicon Chip
Australia's electronics magazine
siliconchip.com.au
Scope 7: a Mosfet drain waveform (top) and its
corresponding gate waveform (bottom). You can see how
the gate voltage decays during each cycle until the Mosfet
switches off and the opposite Mosfet switches on.
2.54mm grid, except for the TO-3 transistor holes, which do not land exactly
on the grid due to the geometry of a
TO-3 package.
Assembly of each PCB is straightforward, with just six components on
each board. Use Fig.4 as a guide to
mounting the components on both,
including the TO-3 Mosfets, which
should be bolted down before soldering and trimming the leads.
Solder the BY448 diodes directly to
the base, as shown in Photo 9, with the
second diode in each pair down in the
appropriate pin recess.
You will also need to cut and drill a
metal hexagonal tapped spacer, as seen
in Photo 8, plus a 3mm countersunk
hole in the centre of the base to attach
this spacer later. To ensure the 3mm
diameter hole in the plug is drilled
on-centre, a temporary 3mm spacer
can be placed in the ¼in recess to
guide the drill. The hole is then countersunk from the pin side of the plug.
The hole for the 3mm countersunk
Scope 8: a close-up of the Mosfet drain waveforms, showing
how one Mosfet switches on (rising gate voltage) just after
the other (with a falling gate voltage) switches off.
screw needs to be centred in the well
in the plug where the hex brass spacer
fits and it is easiest to drill it from that
side (opposite side to the pins). With
the temporary spacer in the well to act
as a guide, run the 3mm drill down the
centre of that spacer to make the hole.
Then once that hole is made, flip the
plug over and use a countersinking
tool on the material for the head of the
screw. A larger sized drill should not
be used as the drill could pass through
by accident.
The spacer’s end needs to be
rounded off a little to fit into the deep
hole in the UX7 plug.
Additionally, a cylindrical spacer is
needed to help fit the finished unit into
the aluminium tube. This has an outer
diameter of 35.3mm, an inner diameter
of 29.4mm and can be 8-10mm tall. I
cut the one shown in Photo 8 out of a
piece of phenolic plate with two hole
saws, then trimmed it to size. This
spacer can also be made of metal, like
aluminium.
Attach the drilled, tapped spacer
to the base as in Photo 9, and solder
three solid-core wires to pins 1, 6 & 7
to connect to the PCBs later. You can
use 0.7mm diameter tinned copper
wire with insulating tubing slipped
over the wires. Glue the cylindrical
spacer to the Amphenol base using
24-hour epoxy (eg, Araldite).
The two PCBs are mounted with a
5.4mm gap between them. The wire for
the Earth connections passes between
the PCBs. Two other ‘crossing’ wires
are required, visible in Photo 10. These
Fig.4: the two PCBs are
similar but with some parts
rotated or swapped as they
mount back-to-back. Points
X & Y on the two boards are
joined (X to X and Y to Y),
while both GND points are
wired to pin 7 on the socket.
Pins 1 & 6 are wired to the
metal cases of the two TO-3
package Mosfets (not shown
here).
Photo 10: the vibrator replacement is now operational, with the two PCBs
assembled, wired up and attached to the base via the vertical spacer.
Australia's electronics magazine
June 2023 91
Pin 7 (Earth)
Pin 1
Pin 6
Photo 11: a short spacer over the top
screw that holds down the two TO-3
Mosfets (insulated from their cases)
keeps the PCBs apart.
Photos 13 & 14: views of the finished vibrator replacement sans can.
are Teflon-covered wire wrap types;
however, any light-duty hookup wire
would work.
Ideally, the PCBs should have plated
through holes. In the absence of those,
for this hand-made prototype, I used
small brass eyelets for the connections
between the PCBs.
Use a screw and nut to secure the
Drain connections from pins 6 and 1 of
the Amphenol base to the lower TO-3
transistor mounting holes. Rotate the
PCB assembly so that the gap between
the PCBs is over pin 7. This allows the
wires from the base to pass in a very
direct and orderly way to the Earth
and two drain connections.
Secure the upper mounting holes
between the transistors with a spacer
and some insulators, as shown in
Photo 11.
The two boards are joined at the
top by using two transistor insulators, a 5.4mm high and 3.5mm diameter spacer, a wave washer and M3
nut plus a 4-40 UNC by 3/4-in (or M3
20mm) binder head screw (shown at
the end of the article); Photo 12 shows
the result. Photos 13 & 14 show the
finished assembly.
The final procedure is to fit the
completed unit into the pre-made
aluminium tube (it might be a good
idea to check that it works first!). The
top of the tube can be sealed with a
35.3mm diameter, 6mm-thick disc
glued into place. This is a firm press fit.
I made the disc shown in the photos from Bramite, a fibreglass-like
insulator; however, it could be made
from aluminium, Paxolin or any other
material.
The base is a firm fit into the tube.
You could glue it in, assuming you
have already tested it, because it is
unlikely ever to require repairs. However, it can be retained with a 1.21.4mm spring clip made from spring
1.4mm spring
wire clip
Photo 12: the assembly is a relatively
tight fit in the can, but it does fit. If
you’re having trouble inserting it, try
slightly filing the edges of the PCBs,
careful that you don’t encroach on the
copper tracks.
92
Silicon Chip
Photo 15: like the real vibrator,
the best way to retain the vibrator
replacement in the can is with a
C-shaped spring wire clip. It can be
made by bending a piece of spring
wire around a cylindrical former (the
outside of the can, if necessary).
Australia's electronics magazine
Photo 16: the replacement (right)
doesn’t look exactly like the original
(left), but a casual observer probably
wouldn’t notice the substitution.
siliconchip.com.au
steel wire. The clip engages the existing groove in the aluminium housing,
then varnish is applied. This allows
disassembly if required one day (see
Photo 15).
Photo 16 shows the finished replacement unit next to an original V6295.
The air intake coupler is about 1.5mm
longer than the original housing, so I
trimmed 1.5mm off the lower edge (at
the base end), but this is not necessary;
it still fits well in the socket without
doing that.
Efficiency
I measured the output voltages and
efficiencies of the original V6295, this
design and several other replacements
(some of which will be described in
upcoming issues). I made these measurements with a 12V DC supply, a
3.75kW load and a 47µF capacitor
across the load resistor.
The original unit delivered 267V
DC at an efficiency of 66.6%, while
the Mosfet replacement unit described
here managed 276V DC at 67% efficiency.
The most efficient unit with the
highest output voltage is the somewhat
more complicated oscillator-driven
Mosfet version, at 72.7%. That is to
be expected because of the low power
drive requirements for the Mosfet gates
and the low RDS(on) figure of the Mosfets used in that design. That is one of
the designs to be described in a future
issue, likely later this year.
Positive-ground radios
For positive ground radios, it’s possible to use the same design by using
complementary devices (ie, P-channel
Mosfets instead of N-channel Mosfets) and reversing both zener diodes.
No other components in this design
are polarity-sensitive. That is a great
advantage of circuits using discrete
parts rather than ICs; they are easily flipped to the opposite polarity if
SC
necessary.
Some of the hardware used to
assemble the vibrator replacement.
siliconchip.com.au
Parts List – V6295 Vibrator Replacement
1 Amphenol 7-pin base [eBay 115461595962]
1 76.2mm-long, 38mm diameter air intake pipe joiner [eBay 261366805060]
1 35.3mm diameter, 6mm-thick disc (eg, made from aluminium or FR4)
1 35.3mm OD, 29.4mm ID, 8-10mm high spacer (see text and Photo 8)
1 100mm length of 1.4mm diameter spring wire
1 double-sided PCB coded 18105231, 34 × 53mm
1 double-sided PCB coded 18105232, 34 × 53mm
2 TO-3 package N-channel Mosfets (eg, IRF350, IRF130, IRF230, IRF350,
2N6756, 2N6758) [eBay, AliExpress etc]
2 18V 1W axial zener diodes
4 BY448 1.5kV 2A axial diodes
2 470nF 63V axial plastic film capacitors
2 10nF 400V axial plastic film capacitors
2 10kW miniature ¼W axial resistors
2 1.6kW miniature ¼W axial resistors
2 300W miniature ¼W axial resistors
1 24mm+ M3-tapped metal hexagonal spacer (cut to 23mm long)
1 M3 × 20mm panhead machine screw
1 M3 × 10mm countersunk head screw
2 M3 × 5-6mm panhead machine screws
3 M3 hex nuts
1 M3 copper crinkle washer
2 transistor insulating bushes (the type used for TO-220 package tabs)
2 M2 × 10mm panhead machine screws
2 M2 hex nuts
2 solder lugs
1 5.4mm untapped spacer, 3.2mm inner diameter
1 300mm length of 0.7mm diameter tinned copper wire
1 200mm length of 1.5mm diameter heatshrink or insulating tubing
1 100mm length of light-duty hookup wire
1 small tube of 24-hour epoxy
The NZ-made ZC1 Communications Radio
The photo below shows the New Zealand-made ZC1 Mk2 Military Communications Radio. This radio was a masterpiece of electronics and mechanical
engineering. The ZC1 Mk1 was created by the Collier & Beale Company of New
Zealand, while the Mk2 upgraded design is attributed to J. Orbell of Radio Ltd.
I’m very proud that this extraordinary radio was created in New Zealand, my
original home.
Practically every person in New Zealand learning the art of electronics &
radio in the post-WWII period would have come across this radio, because
they turned up in great numbers in the 1950s, ‘60s and ‘70s in surplus stores
throughout New Zealand.
They formed a structure on which the radio enthusiast could experiment
and modify and, at the same time, learn about radio reception and radio transmitting. As a result, many of these sets were subjected to extreme modifications. It got to a point where unmodified and original units became quite rare.
Many of the parts from them formed the cores of other electronics projects.
The 6.3V tube heaters were connected in series pairs. As there are 11 valves
in the set, one required a series resistor for its heater ballast.
A photo of the
front panel of the
ZC1 Mk2 from the
Author’s collection.
For more photos
of the ZC1, visit:
www.radiomuseum.
co.uk/zc1inside.
html
Australia's electronics magazine
June 2023 93
|