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SERVICEMAN’S LOG
The Dogs’ Collars
Dave Thompson
Our resident Serviceman recently replaced some failed GPS modules and
dud batteries in numerous dog collars for a local hunter. It turned out to
be a pig of a job!
A while back, I did some electronics repair work for a
local hunter. I’m not big on the hunting ethic, but I understand its appeal, especially if one (or one’s family, friends
etc) will consume what gets taken. And there is often a valid
reason for hunting (and fishing): clearing stocks, keeping
wild herds down to manageable numbers, reducing the
impact of pests on arable land and so on.
I used to go out with Dad as a lad to help rid farms of
rabbits, but that is about the extent of my hunting experience. The roughest it got was if we had to four-wheel-drive
into some light bushland.
This hunter, however, is one of those guys who gears
himself up, takes half a dozen very large dogs and walks
20km into dense New Zealand bush to hunt wild pigs.
I must admire his fitness and tenacity, especially as he
has to carry anything he catches back out, and those are
heavy beasts.
His dogs are all fitted with heavy-duty GPS tracking collars because they are easily lost in the bush. He carries a
handheld Garmin GPS and tracks his dogs’ positions using
it. He can also train them remotely, because some of the
collars have a built-in shock-training feature.
It’s all very clever stuff, and the collars need to be heavyduty because if these dogs encounter wild pigs, things often
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get bloody! The collars that arrived had antennas ripped
off, teeth marks in the heavy plastic mouldings and some
of the rubberised bits torn off too.
The GPS module is embedded in a plastic moulding at the
end of a hard-rubberised collar. It connects via a shielded
wire with a soldered joint inside the main body of the collar,
which also holds a battery and the rest of the electronics.
While this wire is embedded into the collar material, it is
still vulnerable, and several had been ripped out.
All the collars I received had stopped being recognised
by the handheld unit. New GPS modules are difficult to
get for these older collars, but a colleague found some for
sale from Russia and ordered them.
Gutting the faulty collars
In the meantime, I set about disassembling these ones.
Each main module is held together with five long screws
and one shorter one. The heavy antenna cable, which is
usually wrapped into and constrained by a rubberised
moulding around the circumference of the collar, is also
bolted to the main housing with a larger M3 screw.
This doesn’t have to be removed to swap a battery, but
as I would have to take the PCBs out, it was much easier
to do that without the antenna springing about the bench.
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September 2023 73
Tearing most of the collars down was a matter of routine, and usually, the two parts of the main housing separated quite easily once the bead seal around the inside
of the case was broken by using a gentle side-to-side rocking motion while pulling the smaller ‘half’ away from the
main body.
One thing that’s hard to describe is how they smell, not
just of dog, but all manner of dried fluids (that I don’t want
to think about) trapped in the nooks and crannies of the
collar and modules. It’s quite a grubby job!
Aside from that, a couple of the collar modules had cases
that had been distorted slightly – by pig bites if the teeth
marks were anything to go by – enough to make separating them a bit tougher. That could also affect the weatherproofing, so I’d have to consider that when I got to putting
them back together.
Two small inline plugs must be removed from the main
PCB so the two halves can be fully separated. The space
inside is tight, and the cables from the battery and the indicator LED PCB that live in the main part of the housing
are very short. Some positional juggling is required to pull
the plugs from their sockets cleanly. Getting them back on
later would be just as much fun!
The first thing I did was get all the weatherproofing
o-rings and seals out of the housings, very carefully because
they’d have to go back in. I then used an old toothbrush
to remove the dried whatever-it-is, dust, and dirt from the
edges and other obvious places. I didn’t want that all over
my workbench or dropping into the work or joints as I soldered them.
A bit of a faff
Two of the collars were the shocker types. These are easily distinguished by the two metal-tipped probes poking
out of the main module into the collar’s neck area. Aside
from being able to shock the dog, just wearing these types
of collars cannot be that comfortable for the poor pooch
running around the countryside!
The issue with replacing the GPS module on this type
is that those prongs are hard soldered into the PCB inside
the module, and I was going to need to flip the board over
to access the GPS module’s signal wires underneath.
The boards are held down with four small screws, but
to get the board off, I’d have to simultaneously heat two
large soldered joints (about 3mm across and 30mm apart)
on one edge of the board, as well as four PCB-mounted
transformer leads on the other side (I assumed this was
the step-up transformer for the shocker side of things) or
completely desolder all of them to the point that I could
lift the board.
I knew this would be unlikely to succeed because of
the size and number of the joints and their locations. The
transformer’s core was physically glued into the case and
couldn’t be lifted with the board, so I had no option but to
free its leads. What to do...
What I used was a combination of both strategies. I
desoldered the posts and transformer leads as much as I
could, using suckers and solder wick. Then, with the soldering iron heating one large terminal, I very gently lifted
the board a fraction of a millimetre using a hard plastic
spudger. I found a spot to pry between a tiny bare section
of the board and the plastic moulding below.
Twisting the spudger would give about 1mm of lift at
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full turn, so I could control the amount the board moved.
The PCB was very thin, so I had to be very careful not to
use too much pepper. I ensured the part of the PCB I could
lever on had nothing on it and no tracks near it. After moving the first one a smidgen, I then let everything cool and
did the same on the other terminal.
Once I had it a millimetre or so up on this side, I had
enough room to do the same on the transformer leads. I then
repeated this process until I could lift the board clear. It
was a real faff to do, but there was no other practical way
for me to do it with my limited soldering tools.
The trial wasn’t over once I had the PCB flipped. The
GPS signal cable feeds through the main module body and
is soldered onto the board. This whole area, including the
aperture through the module and the adjacent area on the
PCB, is covered in a very strong sealant for weatherproofing. It all had to be removed before I could access the cable
and the solder joint on the board.
I’m not sure what this stuff is, but it is hyper-strong and
very adhesive. Since I was replacing the GPS module anyway, I simply cut the cable as close as I could and used
my various dental picks and tweezers to pry the goop out.
I had to be especially careful on the board because of the
adhesion to all the SMDs underneath and the fact that the
tracks are very fine; the solder pads are surprisingly easy
to peel, as I discovered with the first one I did. It is incredibly finicky work, and I made good use of my headset and
illuminated desk magnifiers.
Spare parts that come with fixings
Once all the goop was off, installing the new GPS module was a simple job. It comes with a short length of collar
attached, along with the signal cable, and these new ones
differed in that instead of a tough rubberised compound
for the collar part, they had braided Nylon; no doubt just
as tough, while being more flexible.
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To start the reassembly, I first threaded the new collar’s
cable through the gap in the main module housing, now
cleared of resin, and screwed the Nylon part of it (using
holes burned into it) onto the module’s housing with three
new small PK-type screws that came with the kit.
Even this was difficult, because of the location of the
screws and the need to hold three different assemblies in
such a way that I could get to the screws and wind them
in. By the last collar, I had this process down pat!
With the new collar screwed on and not moving about
(much), I could then position the new cable, which was
about 15mm too long, near the solder pads on the PCB. I
cut it to length, stripped it back and soldered it onto the
pads I’d cleaned earlier after removing the old bits of cable.
All pretty straightforward, just challenging due to the size
and position of everything.
And as I mentioned earlier, I had an extra repair step
because I’d lifted one of the solder pads and a little of the
track while trying to take the sealant off the first board I
cleaned. I had to now get this under the scope to see what
damage I’d done and how I could repair it.
The missing pad was the ground to which the shielding
foil from the GPS signal cable was to be soldered. Luckily,
there was enough copper on the board right next to where
it used to be. This rang out as part of the ground plane
layer, so I carefully scraped off the lacquer and green mask
until I had bright copper. I fluxed and tinned that, creating
a new pad, and then soldered the signal wire in as usual.
Disaster averted!
Replacing the goop
Before replacing the PCB into position, I had to put some
new goop on it. The new parts came with a large syringe
filled with clear replacement sealant, the problem being
that once opened, this would go off within a day, even
the stuff in the syringe. To mitigate this, I prepped all the
boards on all the collars this same way so that I could do
all the sealing and then all the reassembly at the same time.
The process went well, and I cleaned up what runoff
there was on each collar as I
reassembled it. Once the
sealant had hardened,
I tested each one
before putting the
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Items Covered This Month
•
•
•
•
•
Hunter-gatherer serviceman
Repairing a Simpson washing machine
Putting a TV on ice
A mixed bag of coffee machines
All good repairs come in threes
Dave Thompson runs PC Anytime in Christchurch, NZ.
Website: www.pcanytime.co.nz
Email: dave<at>pcanytime.co.nz
Cartoonist – Louis Decrevel
Website: loueee.com
final covers back on, using a known charged battery to try
all of them. I don’t get a good GPS signal in the workshop,
so I sat them outside and waited until the GPS signal light
turned green to indicate satellites were acquired.
At this point, I made a rookie mistake. I’d used one module to test all the collars and then reassembled them back
with their own module halves and batteries. I bet you can
see where this is going...
Before that, though, I had to reinsert all the o-rings and
rubber gaskets I had removed earlier. I also had to straighten
some of the plastic mating surfaces that had been distorted
by pig bites, so they made a better-sealed contact. I used a
sharp hobby knife to tidy up those faces that were a little off.
This part of the reassembly, putting the two ‘halves’ of
the main module back together, is another juggling act. I
needed to position the two parts of the module in such a
way that I could reattach those two very short inline plugs
from the battery holder half of the module to the PCB part
on the collar, while keeping the very flexible collar in a
position that isn’t fighting against me with gravity.
I ended up sitting the bulk of the collar on a stack of
boxes on my workbench, to take the weight, and used a
strong pair of tweezers to connect each plug to its socket.
I needed to take care as the plugs are easily inserted at an
angle into the sockets, which would bend one or more pins
out of the way. That would be a nightmare to fix.
Dropping the ball
Once assembled, I returned the collars to the customer,
not realising that some had dead batteries from sitting
unused without being charged. I just thought they were
flat and assumed they’d been working beforehand, as nothing was mentioned about that. I’ll certainly be more thorough next time.
The collars also use a weird charging clip that I didn’t
have, and I assumed the owner would just charge them up
and go. So, of course, back they came; how embarrassing.
This time, I was also provided with brand-new batteries to
be fitted, a set of charging clips and a nice new handheld
unit so I could test them all properly. Something fun to
play with! But first, it’s back to the workbench!
What I like about these parts is that they come with
everything I need to do the job. For example, the battery
in each module is held in by a form-fitted and quite heavyduty metal bracket, screwed into the moulding using four
tiny PK screws. The new battery came with a new bracket
and a tiny bag of screws. I like when manufacturers think
things through.
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September 2023 75
Getting the battery out was as simple as undoing those
screws and tipping everything out. One thing I didn’t think
to do was to check the position of the lead on the battery before I removed it. It transpired that the pre-welded
lead is offset slightly, and is so short that if the battery is
installed rotated toward the bottom, it will be a real pain
to connect to the PCB.
While forcing the cable to reach the PCB with the battery
mounted the wrong way is possible, I wasn’t about to make
things harder for myself! I double-checked my positioning
theory against the factory-installed batteries and performed
the same battery replacement in all the others (including
dropping two of the screws I was taking out; thank the servicing Gods that spares were provided).
When I was sure everything was good to go, I reassembled them as outlined above. This time, things went a lot
smoother. Once charged, all lit up and tested fine in the
handheld. Now convinced, that all were ready for the rough
and tumble of the hunt, I returned them to their owner, and
imagine they are out there, deep in the bush somewhere,
doing their jobs.
Simpson washing machine repair
S. S., of Strathfield, NSW decided to try a repair himself
rather than pay for an expensive service call. That was a
good decision...
I ran the washing with my usual deep rinse cycle for
one hour and 17 minutes. I went off and did other chores,
but when I checked it a little while later, I noticed that
the machine was off with no lights or display. The power
point was still on, and the room lights were working, but
after switching it off and on a couple of times, there were
still no lights or display.
I unplugged the Simpson SWT704 machine and plugged
in a radio, which worked, so the washing machine had died.
I thought it was about eight to 10 years old; I asked my wife
when we bought it, but she couldn’t remember exactly.
I considered putting in a service call to Simpson, but
after Googling “dead Simpson SWT704”, I found that a
few others had this problem due to a failed control board.
After more reading, I figured that’s probably what had happened to ours. So I decided to give myself a few days before
arranging a service call.
I undid a few screws at the back and was surprised at
how easy it was to remove the top control panel; it just
dropped forward. I must give Simpson five stars for this.
There was a 2012 date on a sticker, so we were probably
right that it was about 10 years old.
The control board has mains coming in and a couple of
other plugs, with one going to the display board. I took the
front panel knob off and removed the control board. The
whole board was potted with a rubber gel and designed not
to be repaired. I noticed a few spots that were browned,
but not greatly.
It looked like a low-power switcher with an LNK306
control chip and, surprisingly, no fuse. A few resistance
checks didn’t reveal anything.
So I looked up the control board and found it available at
a few places, some overseas (China) and a few local ones.
The local ones were more expensive, but I decided to go
with a local supplier as I could get it quicker and, should
there be a warranty claim, it would be easier.
I settled on Genuine Appliance Spares in Melbourne at
a cost of $188, including postage; still cheaper than a service call. It was in stock; I ordered it on a Sunday night,
and it arrived on Tuesday. I checked it against the original and it all seemed OK; hats off to Genuine Appliance
Spares for super fast service.
I compared the new board to the original one and saw that
the brown spots could be where it failed. After replacing
the control board, I connected it up and left the assembly
dropped down while I tested it. I turned it on, and bingo, it
beeped and the display was back on. I checked the selector
switch and other buttons, and they all worked.
I turned it back off and screwed the whole thing back
together. I put a small load on and ran a quick cycle, and
it was up and running again. I was happy with another
successful repair for a reasonable cost. It has now been
four months, and it is still going; I hope we get another 10
years out of it.
The early days of pay-to-view TV
J. B. of NZ worked for a national TV rental company
back in the 1960s, a time when servicing was thriving and
employees had to deal with a wide range of people...
In those days, renting your TV was more usual than
buying it. TVs breaking down was common, so the cost
of repairs was a major factor driving the rental market. If
the family had a poor credit rating, the TV would be fitted with a coin slot mechanism; that was the early form
of ‘pay to view’.
There was one particular address where the man who
Both sides of the replacement control board for the Simpson SWT704 washing machine.
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emptied the slot meters never found any money in the
mechanism and the TV was never on or warm when he
visited. I happened to be servicing in the area and phoned
into the local shop to ask if they had a particular valve in
stock. This led the local branch manager to request that
I pop around the corner to check the offending address.
From the front door, I could hear the TV was on, so I
knocked to gain entry. The household was dirty and smelly
(I am sure all TV techs know exactly what I mean). I was led
into the front room by two scruffy kids about eight years old.
I examined the slot mechanism and found it empty, so I
asked the children how they got the TV to work. The answer
was to get the money from the refrigerator. I said, “Show
me how that works”, and they promptly returned with a
tray from the freezer that had coin-sized indentations filled
with ice. These were the coins to operate the TV!
I reported my findings after I finished for the day to avoid
having to ‘pull’ the set myself.
A tale of three coffee machines
The COVID-19 lockdowns had some unexpected effects
for D. T., of Sylvania Southgate, NSW…
For my wife and me, one was that we missed good coffee – for a while, the cafes were all shut, and when they
opened, you couldn’t sit down and/or they gave you coffee
in a takeaway cup like you were buying it from a service station. So we decided we needed a home coffee machine and
promptly bought a Breville machine at an estate auction.
Estate auctions are a real mixed bag – they’re often a third
party selling the contents of a deceased estate, so no one
knows the history of any of the items. In my experience,
many of the items on offer have faults, especially electrical
items. Ironically, this works really well for me since I get
such a kick out of fixing things, but you wouldn’t want to
pay too much money for anything you find there.
This machine was no exception; when we got it home
and tried to make our first coffee, we found it didn’t work
properly – little or no water came out to brew the coffee.
Luckily for us, the Breville is pretty popular. With the help
of a few YouTube videos, I soon had the covers off and all
the good bits exposed.
I was pleasantly surprised at how serviceable the Breville
machine was. All of the water connections after the pump
are made with o-rings and removable/reusable metal push
clips that enable disassembly and reassembly without the
need for replacement parts.
The two valves can be disassembled and cleaned without any special tools, the chassis comes apart without any
magic tricks, and when it is open, it can be tested without
putting it all back together. The only consumables are the
cable ties that secure each pipe connection to the pump
inlet. Overall, it is quite a good machine for those of us
who like to fix things ourselves.
Before too long, I managed to clear a blockage in the valve
set, and I was soon making passable cappuccinos at home.
Having experienced one of my cappuccinos, my son
mentioned that he wouldn’t mind his own coffee machine,
so my wife duly bought another machine at auction. This
one turned out to be an older model, but very similar in
most respects. That one worked pretty much out of the box
after a bit of cleaning.
However, a couple of problems remained – the grinder
didn’t grind very well, and there was no ‘group cup’. Fixing
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Australia's electronics magazine
September 2023 77
Servicing Stories Wanted
Do you have any good servicing stories that you would like
to share in The Serviceman column in SILICON CHIP? If so,
why not send those stories in to us? It doesn’t matter what
the story is about as long as it’s in some way related to the
electronics or electrical industries, to computers or even to
cars and similar.
We pay for all contributions published but please note that
your material must be original. Send your contribution by
email to: editor<at>siliconchip.com.au
Please be sure to include your full name and address details.
the grinder requires a new ‘core’. You can get away without a grinder simply by using pre-ground coffee; however,
the group cup is the thing that holds the coffee while it’s
brewing, so it’s vital.
All testing had been done using the group cup from the
first machine. They proved elusive when we tried to buy
one for the new machine. New ones cost more than the
machine had cost us, and used ones were nowhere to be
found. After searching for a good while, we gave up, and
the second machine was packed up and stashed away.
My wife is tenacious; she was straight on to looking for
another one. It took a while, but recently, one came up that
was shown with the group cup and some other cleaning
items. She walked in triumphantly last week with a third
Breville coffee machine, almost identical to our original.
Unsurprisingly, this machine was also faulty. It powered
up OK and made all the noises like the others did, but virtually no water came out when we tried to make a coffee.
Having been down that road, I quickly had it apart on the
dining room table and first attacked the valve unit. Unfortunately, while the valve unit was a little grimy, there was
no distinct blockage, and it was no better after cleaning.
The pump was my next target, but it wouldn’t be easy
to get out, so I started looking at all the other pipeware to
see if I could find a blockage. While I was at it, I drew a
schematic for the plumbing, hoping it would help me figure out where the fault could be (see Fig.1).
The pump outlet was pretty accessible and seemed like
a convenient point to test, so I decided to see if I could test
the pump in situ. When you power on the machine, it runs
the pump for about a second, presumably to ensure there’s
water in the heater unit before it turns on.
I pulled the other machine out of storage and fed its pump
outlet into a coffee cup. If I powered up the machine four
times, I ended up with about half a cup of water. I got virtually no water when I did the same thing with the new
machine.
So out came the pump. It’s a bit hard to get to, but not
impossible. Once out, it can be disassembled without any
special tools. It consists of a piston pump with springs and
valves, and I was disappointed that I couldn’t find anything
wrong with it either. So I installed the pump from the parts
machine into the new one and reran my test with the same
result – minimal water output.
Looking at the schematic, there wasn’t much left to go
wrong – a flow meter and filter, the pump solenoid and the
drive to the solenoid. Both solenoids measured roughly the
same resistance and made similar noises when activated.
I could easily pop the top off the flow meter, so I looked
inside – it was nice and clean, and the impeller spun freely.
So I cut off the cable tie holding the filter pipe to the flow
meter and blew into the pipe. I was encouraged to find that
Fig.1: a rough ‘schematic’ diagram for
the plumbing section of a Breville BS870
coffee machine.
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it felt partially blocked, but it was hard to know if that was
normal. To confirm, I did the same thing to the filter from
the parts machine, and was relieved to find it was much
more open. I quickly connected the machine up with the
spare filter and made us two coffees to celebrate.
After the coffee, it was just a matter of picking up the
pieces, of which there were many, and rebuilding the
machine. In the process, I returned the original pump to
its rightful machine since it was in slightly better condition. Then it was a matter of putting it all back together and
making another cup, just to be sure it was still working.
I gave it to my son, who is now making his own coffees.
Chalk one more up for my wife.
Tri-servicing: toaster, TV & soundbar
S. M., of Learmonth, Vic went away for a couple of weeks,
and when he got back, three different appliances had given
up the ghost. Luckily, all turned out to be fixable...
My wife and I went on a two-week interstate holiday that
we had booked over two and a half years previously, but
COVID had intervened. We were deciding what to do about
the pets in our absence when a neighbour recommended a
house-sitting group that worked very well for them.
We were a little apprehensive, especially after having
watched Rowan Atkinson in “Man vs Bee” with the grandchildren. Still, we went ahead, and the whole experience
was very positive. The dog and cat seemed very happy,
seeing the photos sent to us frequently.
About a week into the holiday, we had a message from
them saying our Smeg retro toaster had stopped working;
when switched on, the circuit breaker tripped. They said
they had one in their caravan, and it wasn’t a problem.
A day or two later, we had another message to say there
was a popping noise and the Toshiba 47VL900A TV stopped
working. We had owned this for getting on to 10 years without a problem. They said they could cope and use the one
in the kitchen area. All else went well from then on, and
a good time was had by all.
On our return, I pressed into action an old Russell Hobbs
toaster that still worked but was somewhat intermittent
with the toast level. We decided to replace the TV, as I
wasn’t sure when I would get to look at it and had doubts
if it was repairable.
Sometime later, I got the toaster into the workshop to see
what had happened. On first inspection, it looked fine, so
I dug deeper. That was not so easy as the outer cover not
only had screws but quite a few of those hidden plastic
clips that won’t let go without a fight, then more screws,
and finally, pressed metal plates that locked into each
other with tabs that break off when bent more than twice.
Eventually, I reached the elements to reveal the problem. One of the outer elements, mounted on a mica-like
substance, had a riveted link that had come off one end
and sprung out to touch the case. This link contacted the
element wire on the other side to connect to another part
of the element.
The end that had come off was a little burnt and had obviously not made good contact, causing arcing and eventually
burning off part of the rivet. I could see the element was
not replaceable as all the connections were spot welded.
I eventually decided that the best option was to carefully
drill out the rivet (or what was left of it) and use a very
small brass bolt to hold it all together. It was very tricky, as
the mica-like material was very fragile. After clipping the
excess length off the bolt, I reassembled it. It is still going
strong after some months without a problem.
Even later, I had a quiet afternoon and decided to look
at the TV. I laid it out on the bench face-down on a blanket to try to access the power supply. I removed about 25
screws and, to my surprise, it came apart quite easily. I
looked over the board, particularly the power supply section, and saw no apparent problems.
However, there was a tiny soldered-on fuse that measured
open circuit. The surrounding components checked OK.
It was somewhat dusty inside, so I gave it a good blowout
and removed the odd cobwebs.
I decided to replace the fuse and give it a go. To my surprise, it started up fine, and I ran it for some days without a problem. My son’s old TV had just died, so I passed
this one to him, and it hasn’t missed a beat since. My only
conclusion is that the dust and cobwebs in the very damp
conditions caused a short and blew the fuse.
After installing the new TV, I was checking some things
and noticed that the subwoofer attached to the Yamaha
soundbar was dead. It is not immediately obvious when
it is working, as the only light is an LED at the rear that
comes on when it has a wireless connection.
Out to the workshop it came and, upon opening it, it was
clear what the problem was. These subwoofers have a side
sound vent hole in the case which is very convenient for
mice to come in and live. Urine had shorted the board and
blown the fuse. I cleaned it all up and replaced the fuse,
and it worked again. I put a small car speaker grille over
SC
the hole to stop the re-occurrence of this fault.
Raspberry Pi Pico W BackPack
The new Raspberry Pi Pico W provides WiFi functionality, adding
to the long list of features. This easy-to-build device includes a
3.5-inch touchscreen LCD and is programmable in BASIC, C or
MicroPython, making it a good general-purpose controller.
This kit comes with everything needed to build a Pico W BackPack module, including
components for the optional microSD card, IR receiver and stereo audio output.
$85 + Postage ∎ Complete Kit (SC6625)
siliconchip.com.au/Shop/20/6625
The circuit and assembly instructions were published in the January 2023 issue: siliconchip.au/Article/15616
siliconchip.com.au
Australia's electronics magazine
September 2023 79
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