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SERVICEMAN’S LOG
All washed up
Dave Thompson
It’s always difficult when an appliance in the household breaks down
because we are obliged to at least take a look, even if we have no idea
what we are doing. It’s the Serviceman’s Curse, and I’m guessing we all
suffer from it to some extent.
So of course, when our washing machine chucked a
wobbly, I felt that I had to troubleshoot it, to see if I could
do anything before calling in an actual (and likely really
expensive) repair person to have a proper look at it.
I’m sure you are all aware that I am not an expert on
washing machines. I mean, I know basically how they
work: water, soap of some type, agitation, rinse, repeat and
then they shake themselves all over the floor while they
turn into a huge salad spinner. The rest is timers, valves,
sensors, solenoids and motors; how many of each usually
depends on the complexity of the individual machine.
Ye olde clothes washer
I’ll always have an image of my mother standing in our
laundry in the 1960s, working on what was then a pretty
modern machine. I can’t recall the brand exactly, but it was
likely a Fisher & Paykel wringer type, popular at the time.
It was basically a big round basin with a motor underneath and a spindle in the middle, or, and I’m going out on
a limb here, an ‘agitator’. The agitator went backwards and
forwards and shredded the clothes and sheets, or whatever
was in it. A big lever on the side engaged the thrasher and
meant you could load it and get everything ready before
kicking it into gear.
Mounted on top was a fearsome ‘wringer’: two rollers that
were driven by the motor and engaged by that lever on the
side, which disengaged the agitator. Those rollers could be
tensioned with a large, cast-iron knob at the top. A shaped
drain at the bottom of the rollers guided any water wrung
from the washing back into the main tub.
The whole wringer assembly also had a safety mechanism
built into it so that when dumb kids like my brother put
his hand in there, it would pop open. That would release
the downward pressure on the rollers, allowing him to pull
his hand or arm back out.
As a system, it was a simple and actually brilliant design.
The machine worked well, aside from ruining just about
anything washed in it finer than denim. Still, this pressure-
sensitive wringer safety system used to trip all the time with
mum just putting things like sheets or heavier wet fabrics
through it. So in the end, she cranked that thing down so
tight that it wouldn’t trip at all.
The obvious concern is that your arm would come out
like a pancake if you were silly enough to get it caught in
there. And going by anecdotal evidence at the time, plenty
of people did! I was always too afraid to get anywhere near
it, but mum was braver and fed the clothes and linens
through it, with her fingers ending up dangerously close
to the rollers! I suppose she knew what she was doing,
having worked the thing every other day for a long time.
Of course, things have moved on a lot from those days.
Aside from the Hoover-matic style twin-tub horrors of the
1970s, most subsequent machines have been more efficient
and more reliable. Indeed, some appear to have lasted forever, if the washers I came across in flats I rented were
anything to go by!
Not to be sexist, but housewives of the day wouldn’t
put up with something that didn’t work properly or would
make their lives harder, preferring to utilise tools that made
their lot easier.
Front vs top loaders
We now use a front-loading style of washing machine in
our household. These use a lot less water than top loaders and are generally more efficient with power and soap
use. Most European countries use front loaders, and as my
wife is from Europe, we went with what she knows. Happy
wife, happy life!
The reason for this in Europe is water usage (households
there pay for the water they use, something most cities in
New Zealand do not do). Moreover, there’s the simple and
practical fact that many people living in apartments have
the washing machine in the kitchen, and it sits under a
counter or bench like a dishwasher, so top loading is not
typically an option there.
Our machine is from a well-known Korean manufacturer of home electronics, smartphones and whiteware. It
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is the second model we’ve had from that maker in the past
25 years, so I’d call that reliable (although I’d like to think
mum’s first F&P is likely still going somewhere!).
The first machine simply wore out, and as is typical, was
too expensive to replace all the bits that needed replacing
– at least, those that were still available.
So, we invested in a flash new model with a few other
bells and whistles on it, not that it turns out we use any
of them anyway (marketing works!). We basically use the
same program for everything we do.
I didn’t know we had a pool
This has been a very good machine too. Except one morning, I got up to go and hang out the washing we’d done the
night before, and there was a swimming pool in the laundry.
Great! Just what I needed. I also could not open the door of
the washer, an electronically applied safety feature designed
to prevent, well, swimming pools on the laundry floor.
Usually, the last thing you want with a front loader half
full of water is to open the door! This is one of the few
advantages of a top loader, in my opinion; you can stop it
mid-cycle, open the top and do what you need to do without a disaster in the laundry.
My first thought for the water egress is that the big, circular door seal had gone. These seals work like an oil seal in
the gearbox of a car (or the diff, you choose). The pressure
and weight of any water behind it ensures a decent seal
on the surface, in this case the glass front window, which
of course is opened and closed all the time
to load and unload the washer.
That opening and closing can wear it
out. Any grit or anything else that gets
through the filters can damage the fragile
seal as well.
Usually, the door will not open until the
pump has evacuated all the water, and only
then does the door lock deactivate. In the old
days this was a simple mechanical lock, but
now, of course, is a much more complex electronic type of arrangement utilising sensors and
solenoids and likely smoke, mirrors and ball bearings, knowing modern designers.
Maintaining that seal on the door glass is likely
where millions of research dollars were spent (and
probably more than a few buckets and mops!).
They do seem to have gotten the hang of it though, as our
machines have never leaked from there.
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But leak this one has. And cleaning up water spills is
time-consuming; there’s also the potential damage to all
the cabinetry in the laundry to worry about. The Weet-Bix
wood this stuff is made from is like a sponge and will soak
up any moisture it comes into contact with, despite the
rock-hard melamine laminate on the outside.
Once the lake was dealt with, I turned my attention to the
machine itself. The water didn’t seem to have come from the
door – there were no tell-tale watermarks. In fact, the whole
cabinet appeared to be stain-free. My amateur washing-
machine repair brain thought the obvious: a clogged filter?
Fortunately, this is something the owner can usually
fix without too much difficulty, with panels provided for
access to the filter(s).
The problem here was that the panel was very tightly
fitted, and I had to prudently use a spudger type tool to
pop it clear. Once off, I could clearly see the filter assembly
and it was dry all around it, so I guessed the water didn’t
come from there.
I still opened it, took the filter out and cleaned it. We have
three cats (I know) and though short-haired, they still drop
a large amount of hair. Relentless vacuuming and sweeping typically keeps it at bay, but clothes love gathering
hair, and that is what filters are for in washing machines
(well, that and the tissues or bits of paper you might have
forgotten in pockets).
There was surprisingly little detritus in the filter, but I
cleaned it out anyway and replaced it. The cover popped
back in with a satisfying click, and I could see there was
no chance of it falling off even with the most unbalanced
of washing loads.
So, not the filter then. This was fast becoming something
beyond my scope of abilities. Time to bite the projectile and
get in someone who actually knows what they are doing.
Getting some help
The next challenge was finding a repair provider who
knows these machines. Several I called told me they weren’t
familiar with them, which is madness because the brand
is one of the most famous in the world.
I guess the manufacturer might have a watertight (har!)
service policy with repair agents, a la Apple and their guys,
but I got the impression that these
people just hadn’t worked on
one of these types before;
Australia's electronics magazine
December 2024 89
Items Covered This Month
• Treading (un)familiar water
• Faults take many shapes and sounds
• A rattling fan bearing
• Repairing an automatic HDMI switch for PVRs
Dave Thompson runs PC Anytime in Christchurch, NZ.
Website: www.pcanytime.co.nz
Email: dave<at>pcanytime.co.nz
Cartoonist – Louis Decrevel
Website: loueee.com
not an ideal situation. I finally did get hold of one outfit
that was an official repair agent for these machines, and
he said he had a good idea as to what might have caused
this problem.
I wasn’t going to be presumptuous and ask him what
that might be – even I respect a serviceman’s right to make
a living! The fact is, I was happy to pay for someone who
knew what they were doing to come and fix it. It seemed
to me the water was coming from inside somewhere, and
I wasn’t about to break open the sides and covers just to
find out I couldn’t fix it anyway.
So, I made a time for this guy – which exposes another
annoying aspect of this type of repair. Afternoon or morning? I mean, when I had vans on the road I would nail a
time down on the phone long before we got there, and
unless something like a natural disaster happened, we’d
be there at that time.
These people seem to operate in half-days. You’d think
that after years of repairing whiteware, they’d have a better idea of time management. This would mean I’d have to
sit around waiting for the guy to turn up any time between
1pm and 5:30pm.
Being self-employed, taking time off work is not a huge
deal, but imagine if I had to come back from my job and
take time off just to accommodate a repair guy? That doesn’t
seem right to me. These days, they can always text when
they are on their way, but it is still disruptive and generally why I dislike relying on third parties.
Still, he arrived with his toolkit and started with the usual
troubleshooting procedures. He also asked what detergents
and additives we used. I showed him the liquid soap and
softener we used in the machine. We’ve used them since
day one, so I couldn’t really see the relevance as far as the
soap goes, but we’ll come to that later.
I was more concerned about a sensor that wasn’t detecting water levels or a valve that wasn’t closing properly,
something along those lines anyway.
Well, this guy seemed to know what he was doing, so I
left him to it. I know how annoying a hovering customer
can be! He pulled the machine out (easy enough to do on
the two wheels in the front) and whipped the case off with
practised ease. I was keeping a little look-out, but it all
looked alien to me inside it.
A simple resolution
After having a good look around, he dismantled the soap
dispenser and discovered it was completely gooped up. I
know this is a technical term, so bear with me. It seems that
some detergents and washing powders don’t break down so
easily with the water in our pipes and the residue builds
up over time, causing problems.
The guy showed me the soap tray. It’s just a plastic thing
with many holes in it, and usually the soap and water mixture drains through it. This one, however, was coated in
a thick slime of residue. The holes were blocked and, of
course, nothing could get through them.
The water fills up as part of the wash cycle and should
drain through this assembly. However, if the holes are
blocked, it just fills up and pours over the top, then down
through the appliance until it floods the floor. Because this
fills up with water several times a cycle, and it has nowhere
to go, it just pours over the top of the dispenser and ends
up on the floor of the laundry. So that at least explains why
we had a lake in the laundry.
Then what is the answer to this problem? Different detergents? Removing and flushing out the dispenser regularly?
You would think that the manufacturer would be well aware
of these problems, but there are no alerts or advisories, no
cautionary tales on their social media.
I guess it all comes down to the different water in certain
countries, whether it is ‘hard’ or ‘soft’ and how it reacts
with the various products and soaps that are available.
At the end of the day, it was a simple fix: clean out the
gunk. However, when I was looking at the machine, I was
thinking all manner of potential problems; the Serviceman’s Curse was at play again.
Overthinking it is typical for me. The thing is I don’t really
know how these things work, and blocked drain holes in
the water/soap dispenser is not really a logical thing for
me to think of if the machine starts leaking.
The repair guy knew (I think) pretty much right away
what was likely to be wrong. He basically told us to avoid
a certain brand of fabric softener that is known (in this
machine in this country at least) to cause problems. If it
doesn’t break down completely in water, it can’t be all that
good for clothes anyway, which is something else he hinted
at. I guess we won’t be using it any longer.
A good enough ‘fix’ then, and well worth getting a professional serviceman in – I would have never known of
this problem unless he’d told me.
Faults have many causes
I recently repaired a studio monitor speaker. These are
fairly common items for home studios and often have a
6-inch (15cm) or 8-inch (20cm) woofer and a dome tweeter.
The more expensive units are bi-amped, meaning they have
separate amplifiers for the two drivers. Often, the amplifiers
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are built around power amplifier ICs to simplify construction, as was the case with this unit.
The fault was no sound, but the power indicator was
lit. Given that it has separate amplifiers for the woofer and
tweeter, it seemed unlikely the fault was there. However,
they are usually connected to a common mute circuit, so
the fault could be there, or in the preamp or power supply.
The first thing I noticed on opening it up was glue covering a lot of the circuit board. This is put there by the
manufacturer to secure the large capacitors to the board.
I checked the +15V and -15V supplies to the preamp and
discovered the +15V rail was slightly negative. So there
was a problem with the series regulator feeding this rail.
A quick check showed the resistor feeding the base of the
regulator transistor was open-circuit.
Pulling it from the board revealed why. The underside of
the resistor was covered in glue, which limited its ability
to dissipate any heat. The resistor was a 0.5W type, and a
quick calculation showed it was dissipating about 0.3W. I
replaced it with a 1W type and stood it up off the board a
little to help get some air around it.
I also replaced the resistor doing the same function in
the -15V regulator, the underside of which was also covered in glue. I removed as much of the glue from the board
as I could while doing so.
In other units, I have found the same glue, which starts
life as a honey colour, has turned dark brown or black with
heat and becomes conductive and corrosive. In some cases,
the glue gets into the through-hole vias on double-sided
boards and corrodes the connection. Such faults are not
easy to find. In this case, just two replacement resistors
restored normal operation.
My next repair relates to the Styloclone project in the
August 2024 issue (siliconchip.au/Article/16415). I was
aware of the original Stylophone as I owned one; it was a
horrible beast. The sound it produced was basically square
waves and the noise becomes grating after a short while. I
note the Styloclone has a capacitor filter to help with this.
The unit pictured here is called “Wasp” and was made
in the late 1970s by an English company called Electronic
Dream Plant (EDP). I have been servicing music electronics for more than 50 years, and I have never seen one of
these before.
This unit does not use a stylus; instead, the keys react
to touch. I thought it was somewhat of a toy at first, but
once I got it going, I found it to be a capable synthesizer
with nice tone.
The customer helped me find the first fault as he said
there was a wire off inside and he was right. The filter section has a rotary switch to select between HPF, LPF or Band
Pass Filter and this switch had worked loose, allowing it to
rotate and break wires off. Only one wire was broken, which
should have been connected to the wiper of the switch.
With the wire repaired and all the switches and pots tightened to the board, we now had sound. The controls were
all noisy; a small squirt of switch cleaner in each fixed that.
All was looking good until I tested all the functions and
found the Filter Envelope Generator was not working. To
my surprise, an internet search located a service manual.
The circuit diagram was hand-drawn, difficult to read and
rather complicated. Further on in the manual, parts of the
diagram had been redrawn nicely, including the part I was
interested in.
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The studio monitor PCB with glue on the capacitors.
An internal shot of the “Wasp”.
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December 2024 91
The Envelope Generator uses three ICs to do its job: a
4013 flip-flop, a 4016 quad CMOS switch and an LM3900
Norton (current feedback) op amp. They are not commonly
used anymore. I was aware of them but had to look up a
data sheet to refresh my memory how they work.
A few measurements allowed me to determine the
LM3900 was the culprit. I remember having some in stock
decades ago but figured they are probably obsolete. A deep
dive into several parts boxes uncovered a bag with one left
in it. This solved the problem and this instrument was
ready to go.
The customer also had the matching sequencer for this,
called The Spider, which was dead. I found a faulty 5V regulator, but it still would not work properly after replacing
it. I had to give up on that, as it appeared the RAM was
faulty and was also obsolete.
P. M., Christchurch, New Zealand.
Fanning out troubles
I have had a Vulcan Tangi fan heater since 1974. I bought
it when I joined the RAAF as some of the base accommodation at the time was poorly heated. It has served me well over
the years but has not seen continuous use. The fan motors
in these are small shaded-pole induction types with bronze
bearings, which tend to wear, causing the fan to rattle.
I purchased a spare motor in the 70s, replacing the original in 1989. That motor developed the same rattle, but
by 2020, spares had become impossible to find, so I just
put up with the noise until I could find a replacement. As
luck would have it, I was perusing some exhaust fans on
display at my local Mitre 10, and one looked like it had
an identical motor.
It was worth a punt for the bargain price of $16. On removing the old motor, it was apparent that this was an exact
replacement, except that the drive shaft was 2.5cm longer
and the diameter was 2mm larger. Neither was a problem,
as the fan connects to the motor by a grommeted hole that
could accommodate the diameter. The extra length would
be hidden within the tangential fan.
This worked well, with the bearing rattle gone, but an
occasional different rattle remained, and I could not determine the source. Then, one day recently, there was a bang.
The fan stopped immediately and a burning smell emanated
until the over-temperature cut-out operated.
The selector switch has a couple of RFI suppression
capacitors on it, and I suspected one had failed, but that
didn’t explain the stopped fan.
Dismantling the heater showed that a fan blade had
separated and had stopped the fan while the capacitors
were intact. I checked the internet for spares but none
were available. There was a fan for a Westinghouse oven
that looked identical, but the supplier did not return
my requests for dimensions, and at $95, it would not be
worthwhile.
Could it be repaired? The fan was made of aluminium
and was attached to the steel drive disc by mechanical
straking. The broken blade had separated at the joint. It
was a weak point and impossible to weld, so I tried some
JB Weld epoxy resin around the blade. To keep the fan in
balance, I applied some around the other blades at that end.
A coat of sprayed black paint and the fan was more rigid
than when new. After reassembling the heater, test runs
showed no signs of rattling at all.
This heater is nearly 50 years old and undoubtedly has
The “Wasp”
styloclone
made by
Electronic
Dream Plant
(EDP), this
time with its
case on.
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exceeded the life that the designers at Vulcan intended.
It is a testament to the quality of goods we made here in
Australia at the time.
R. W., Hadspen, Tasmania
Automatic HDMI switch repair
We have two personal video recorders (PVRs) in our
lounge room. Each can record two channels at the same
time. The main one is used for most of the recording and
playback, while the second one is used for the odd occasion when there might be three programs on at the same
time that we want to record.
Several years ago, when I set everything up, I bought an
automatic HDMI switch on eBay. It automatically switches
the video and sound from the active HDMI cable input to
the TV. So, when one PVR is on, the signal is routed to the
TV automatically.
This works well; the only time the switch needs attention is if the second PVR happens to turn on while using
the first or vice-versa. In that case, it’s necessary to push
the button on the switch to change back to the other PVR.
This system worked well for several years until the automatic HDMI switch stopped working. At first, I was not
sure why I was not getting a signal to the TV, but when I
looked at the HDMI switch, I could see that the LED was
not illuminated. I replaced it with a remote-controlled
HDMI switch I’d picked up recently, but it was unreliable.
So I decided to have a look at the automatic HDMI
switch to see what was inside it. It comes apart easily
by removing four screws on the back and lifting it apart.
Then the circuit board just comes out, as it’s held in by
both case halves.
I was unsure if the main IC had failed, so I decided to
test the two 100µF 10V electrolytic capacitors and sure
enough, one had an ESR of 9.2W. I looked in my salvaged
capacitors, but I could not find one that was tall and thin; I
found a shorter, larger diameter one that I fitted to the board
(the one in the lower-right corner of the board).
Sure enough, this put the HDMI switch back into working
order, so I could ditch the unreliable remote-controlled one.
SC
B. P., Dundathu, Qld.
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Read the articles in the April – May 2022 issues of Silicon Chip: siliconchip.com.au/Series/380
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December 2024 93
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