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SERVICEMAN’S LOG
The things we do for our pets
Dave Thompson
Serviceman’s log, stardate 2023.12. We have encountered strange furry
creatures that are demanding to be fed. It’s almost as if they believe they
are our masters. I have beamed down to the planet to see if I can open a
dialog with the three famished felines.
The serviceman’s curse is indeed a curse! It is, of course,
tied in with our peculiarly Antipodean DIY ethos and the
‘number 8 fencing wire’ lore of Australia and New Zealand. If we think we can do it ourselves, we will at least
have a good go! Still, I like to think that most of us know
our limits. I, for example, would not try my own dentistry
or brain surgery.
For one, I’d need someone to hold the mirror and/or
torch, which precludes doing most common dental and
medical procedures. I think that sort of thing is better left
to the professionals.
With just about everything else, though, I’m willing to
give it a go. Whether it is building a guitar, installing an
alarm system or replacing the main bearings on my car,
I’ll give it a shot. I mean, what could go wrong? The guitar
could be rubbish (I have made many, but only the first one
was rubbish), or the engine overhaul doesn’t go as planned.
They’re all pretty minor problems in the greater scheme
of things, and there’s always the option to call in a professional, hopefully without them being annoyed that I have
‘had a go’ before bringing them in.
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I encountered this all the time in my line of work. Most
people would only bring their computers in for repair after
they’d had a go following some ‘tutorial’ on YouTube on
how to fix it themselves. When I was trying to run it on
the bench, they’d often chime in to say, “I tried that” or,
“I’ve already done that”.
I responded that I had my own troubleshooting processes,
and I might very well replicate what they’ve already done.
However, as they had brought it to me to fix, we could chat
about what they’ve tried, or I could get on with my process
for finding the cause of the problem.
As we all know, there is so much misinformation on the
web that it is almost impossible to find answers to even
the simplest of questions without spending hours trawling
through the clickbait, scams and people posting the same
old erroneous rubbish just to scrape out some ad revenue.
Hard drive on the rocks
As an example, once upon a time, there was a data recovery strategy that required putting dead mechanical hard
drives in the freezer to rejuvenate them just long enough
to get the data off. In very specific and extremely limited
circumstances, that method might work if the drive motor
was seized.
However, the way it was promoted on hundreds of sites
was as if every failed drive could be recovered by doing this
simple ‘hack’. As someone who has recovered data from
thousands of drives over the years, I can say that it is not
a reasonable strategy for recovering data. Yet, the number
of people who brought drives in saying they’d tried that
method was staggering.
It is just one tiny example of how misinformation can
spread and how it can also dramatically reduce the success of proper data recovery by messing with things
people don’t understand.
Many of those doing their own computer surgery are
unaware that even tipping a drive over from standing
on its edge to landing flat on the benchtop could cause
platter damage. Handling drives and putting them in
the freezer often precluded me from recovering any
data from them because those people didn’t realise
how fragile the drives were.
Nothing in those tutorials mentioned static protection or physical vulnerability, so often, by the time I got
them, they were already ruined. One guy drove hours to
get to me with his hard drive floating around unprotected
in the tray of his ute!
Australia's electronics magazine
siliconchip.com.au
Items Covered This Month
•
•
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What we do for our pets
Repairing a Whirlpool washing machine
The clock that was running fast
Dave Thompson runs PC Anytime in Christchurch, NZ.
Website: www.pcanytime.co.nz
Email: dave<at>pcanytime.co.nz
Cartoonist – Louis Decrevel
Website: loueee.com
Alas, such is the DIY ethos we all have. It also encompasses devices that are often not really worth the time and
effort to repair, and it is simple bloody-mindedness that
keeps us trying to fix such things. I’ve spent hours repairing cat toys when it would be much more sensible to just
go and buy another one.
For me, it’s the principle of the thing; if I can fix it, I
should. It’s my duty. And if I end up spending hours and
hours on a job for someone else and can’t fix it, then I don’t
charge. That’s the moral way of doing business, even if it
is not a path to riches.
High-tech moggie feeding solutions
We have three cats, and they all eat different diets for various reasons. So we have different food bowls and feeding
patterns, and this routine involves some highfalutin (read:
expensive) microchip-based cat feeders for two of them.
I have written about these units before. I’ve also broken
one by trying to be clever; probably not the last time I’ll
do something like that! These devices run on four C-sized
cells, with no provision for external power. In this day and
age, that’s an odd thing, or at least I thought so. I did what
anyone else would do and tore it apart so I could power it
with an external supply.
I’ve done this with dozens of devices over the years,
including guitar stomp-boxes. I have also converted
primary-cell-powered torches into rechargeable devices by
switching to NiCads and adding charging sockets. It’s usually all pretty straightforward stuff. This time, however...
Getting these microchip feeders apart is easy; there are
no stupid security fasteners or single-use break-away clips;
just good, old-fashioned screws biting into solid plastic
turrets and good-quality plastic mouldings that fit together
seamlessly. A long-reach Phillips screwdriver is the only
special tool required, as some of the holes are deep, and
the screws are beyond the reach of a standard driver.
Inside, they are surprisingly complex, but there was
plenty of room for adding a socket in the rear corner,
and the wires to the battery bays were easy to access.
I dug through my boxes of power supplies, gleaned
from years of collecting them and never throwing any
away, and found a 6V DC supply that would do the
job. This supply would determine what type of power
socket I would install, because it is far easier to get a
new socket (if needed) than to change the output lead
of the supply (though I have done that many times in
the past).
I used to watch Dad changing a supply’s lead and/or
polarity by opening up the sealed plastic case. I’ve tried to
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replicate what he did but have never been successful. He
would sit the supply on one corner on the workshop floor
and, while holding it in position with his left hand, strike
the uppermost/opposite corner of the case with a hammer.
Every time I saw him do it, one quick rap with the hammer and the case would just pop apart down the seams
like magic. Whenever I’ve tried it, I end up with a smashed
case, typically parting everywhere but the seam and with
crushed corners. It can usually be glued back together, but
it is highly annoying that he made it look so easy, and I’ve
never been able to do it, even with him teaching me!
Since then, I haven’t even tried to do it, but I can do a
plug swap or add an inline switch in the wire near the supply’s output. When done properly, it looks OK and functions perfectly well.
Anyway, I found a suitable socket in one of my spares
boxes and installed it into a space in the back of the feeder. I
re-routed the battery leads to the socket, ensuring the polarity was right, and soldered it together. I used tape tabs to
hold the wiring out of the way of the door mechanism and
reassembled the whole thing.
I plugged the supply in, connected it and tried the feeder
using one of the RFID tags that came with it. Nothing; no
lights, no response to button presses or programming functions. Bupkis.
Well, that was disappointing. I checked the supply’s
polarity and output, and though the measured 6.5V
(unloaded) was a little high, I thought it was within limits. The polarity was correct, but it didn’t work. So, I took
the whole thing apart again and rewired it back to battery
power. This time, I got lights, but while the door tried to
open, it wouldn’t go all the way, even though the motor
tried to actuate it.
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Bother! (or words to that effect)
Try as I might, I could not get this thing to work correctly.
It was the first device in decades that wouldn’t operate after
a conversion. I was gutted, especially since this thing cost
300 Kiwibucks (about 280 Aussie dollarydoos) and it had
lasted less than a week. It appears that some things are not
meant to be mains-powered!
I was 100% sure that I’d gotten polarities and wiring correct, and I’d double-checked it half a dozen times before
applying power. I guess I was trying to be too clever by
half. Lesson learned! That feeder still sits in my workshop
today, dead and gathering dust.
While covered by a factory warranty, I’d have to ship
the unit to the USA for repair and pay all shipping costs
myself. That would have cost almost the same as a new
unit, and I think they’d ask questions about the hole I’d
bored in the back for the power socket!
So, an expensive lesson then. I still don’t know why it
wouldn’t power up with mains power. It was an old transformer-style supply, not a switch-mode one, so I can see
no reason that wouldn’t have worked. I wasn’t going to
try it again, that’s for sure! I did what any self-respecting
serviceman would do and went and bought another unit!
That one is still going strong today, and the four C cells
last almost a year, so it was a bit of a moot exercise anyway.
The pitfalls of parts swapping
However, the other feeder has now developed a problem. It sounds very rough when opening and closing and
sometimes stalls partway through the door-open cycle.
Either the motor was getting weak, or the gearbox driving
the door assembly was wearing out. Not good either way.
Now, I know what you’re thinking. Did he fire six shots
or only five? Sorry, wrong movie. I meant to say I have a
whole new spare, non-working device sitting in my workshop that I could burgle parts from. And you’d be right,
except for one tiny prob.
Between the time I got these and the new one, they’d
changed the model slightly, including the folding door actuator mechanism, so they look completely different on the
inside. Even the PCBs are different. You can rest assured
there was some blue language flying about the workshop
when I discovered that!
The first thing I tried was changing the batteries. Though
there is a low battery indicator on the feeder (a red flashing
status LED once every minute or so), I swapped them out
for some new, fresh alkaline cells. There was no difference,
as I suspected, so it was not caused by a lack of power.
I pressed on regardless and took the covers off the grumbling feeder. It’s been opening and closing half a dozen
times a day for years now, so I fully expected it to be worn
out, especially given the current gear noise.
The motor itself is the same in both the old and new versions, but the gearing and actuator assembly are slightly
different, which is to be expected as the door opens and
closes slightly differently in each version. This is a bit of
a curse because swapping one assembly to the other unit
would have been so easy. However, it’s rarely that easy!
The only real option was to disassemble the grumbly
gearbox and check it out internally for wear and tear. If
anything inside the unit had totally failed and needed
replacing, I’d be dead in the water, as the company does
not provide spare parts. Oh, for a 3D printer!
When I pulled it apart, I confirmed the motors looked
the same. I guess that changing it between models would
be pointless. The gearbox is a Nylon gear assembly that
converts the rotary motion of the electric motor into a linear action to actuate the bi-fold door.
If the door is closed, and the correct embedded microchip or RFID collar tag is detected, the motor runs in
one direction to open the door. If the door is open, and
the microchip or tag signal is no longer detected, after a
switch-selectable preset time, the motor runs in reverse
to close the door.
The limits appear to be set electronically, similar to an
electric window in a car, where the controller detects when
the window reaches its maximum and minimum operating range by detecting the increased current drawn by the
motor. This will also occur if someone gets their arm or
fingers stuck in the window, or in this case, a cat gets a foot
stuck in the closing feeder door.
I tested it when we first got these units, and that safety
feature works quite well.
Fixing the feeble feline feeder
In this feeder, sometimes the door won’t open more than
a few centimetres. It always seems to close OK, though; it
is just dodgy on opening, which likely takes more energy
due to working against gravity.
I guessed that something was fouling the gearing, or the
grease had dried out, and the gears were binding up. In
other words, I felt it was a mechanical fault rather than
an electrical one. At least if the motor was failing, I have
a spare one of those!
I took the five screws out of the gearbox housing and
carefully pulled the side clear. I’ve been caught with these
sorts of things before, where some gears and shafts come
out while others stay put, and half of it ends up falling onto
the bench. I really didn’t want to have to work out what
went where, having never seen it in place!
I managed to get the case off and saw that while the
gears had some noticeable wear, the light grease used was
dry and crumbly and lying in the bottom of the gearbox.
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I used a contact-cleaning spray to wash the box out and
mixed bearing grease and oil (all I had) to make a light
composite grease.
I applied it liberally over everything I could see and
added drops of oil on the shafts where they engaged with
the housing.
I reassembled everything and inserted the batteries. Without the bi-fold door fitted, I ran the actuator forward and
reverse manually several times to coat everything well. It
certainly sounded better! I then reassembled the whole
thing, and it has been running quietly and smoothly for a
few weeks with no stoppages. If it lasts another year, I’ll be
happy – who knows, maybe I’ll have a 3D printer by then!
Editor’s note: I’ve sometimes had luck spraying silicone
lubricant into holes in gearboxes on small pieces of equipment with similar problems. While it’s rarely a permanent
solution, it can save you from having to disassemble and
reassemble the lot, and sometimes you can even get away
with poking the straw through a hole in the case.
Repairing a retro Whirlpool washing machine
D. C., of Beachmere, Qld went on quite an adventure
delving into the innards of his trusty old washing machine.
It is a simple and robust design that has withstood the test
of time and just needed a bit of TLC...
We had an older model (non-electronic!) Whirlpool
6LSS5232 washing machine for well over 30 years. It is a
two-speed model with suds return, which my wife loves.
Washer technicians have told us that the machine is almost
indestructible and to keep it going as long as possible.
These machines are direct-drive via an ingenious gearbox
attached to one end of the motor, with the pump attached
permanently to the other end. This turns in one direction
for washing, then reverses for spinning and pump-out. The
design was so successful that many other manufacturers of
the time either copied the gearbox design or used Whirlpool parts in their own machines.
The drive motor is an open asynchronous AC motor with
high/low speed windings, plus a winding for the capacitor
start, which permits rotation in either direction. The usual
centrifugal switch controls the start winding disconnection.
However, the centrifugal switch does not operate reliably at low speeds, so the motor is always started with the
high-speed winding. After that, changeover contacts on
the centrifugal switch select the low-speed winding once
it is spinning.
Our machine was recently showing three faults as well
as quite a bit of cosmetic ageing and the usual rust from
corrosive detergents, so it was time for an overhaul. The
problems were timer unreliability, a leaking tub, and spinning a full tub of water while pumping out. The last one
was worrying, as spinning a weight like that puts a lot of
strain on the motor and clutch.
To make a less rushed job of reconditioning the machine,
I purchased a similar working machine, with a view to
later use good parts from that machine as spares. While the
spare machine was working, it had been sorely neglected
and was seriously rusted, so it was of little ultimate use
apart from spares.
The timer is the typical rotary mechanical device of that
era, with a “pull out to start” function and loads of cams
and contacts to control the various functions, driven by
a small timer motor. The fault turned out to be a broken
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detent spring inside the timer which holds the knob in the
start position. Of course, the spring is deep inside the timer
mechanism, so I had to dismantle it completely.
I was able to steal the spring out of the donor machine,
but there were many hours of fumbling and cursing, getting all the bits back together (six hands would have been
good) before I finally succeeded with repair phase one.
I then started the real overhaul of the washer mechanism, learning as I went by making lots of mistakes! I managed to get it all apart and cleaned out the caked-on detergent deposits from 30 years of hard work. The tub seal is
located deep inside the works and seals the agitator shaft
as it enters the bottom of the tub.
Amazingly, many parts for these machines are still available in the USA; some are even available in Australia, so
there was no problem getting a new seal and fitting it.
The spinning-while-pumping problem was a bit more
involved. The gearbox allows agitation when the motor
spins in one direction, and spinning and pumping out in
the reverse rotation. To enable the reverse rotation to do
two different jobs, spinning or pumping, the smart engineers at Westinghouse designed a device called a ‘neutral drain’.
One of the ubiquitous YouTube videos helped me to
understand how the neutral drain works. It is inside the
gearbox and consists of a large metal wheel with several
hard plastic cams and latches. The device counts up the
wash agitator movements until a latch is set, and the latch
prevents the drum drive dog from rotating when the motor
is reversed, so the neutral drain only works immediately
after a wash cycle. Thus, the water can be pumped out
without the drum spinning.
After a suitable time for pumping out, a short rest is
included in the cycle, which allows the neutral drain latch
to release, and regular spinning can resume. When the drum
spins normally, the drum’s brakes are released by a cam,
and the clutch allows slippage until full speed is reached.
However, when the neutral drain is in, the drum is held
firmly at rest by its brakes.
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February 2024 97
The Whirlpool washing machine shown with its AC
motor and gearbox assembly on top.
The hard plastic neutral drain components wear out with
time, and a “neutral drain kit” is readily available, which
completely solves the problem. I sent the required dollars,
received and fitted the components, renewed the gearbox
oil, then bench-tested the motor/gearbox assembly, which
worked perfectly.
To make bench testing easier, I built a small motor test
unit that allows forward/off/reverse rotation and high/
low-speed selection. It was just a matter of mounting and
wiring two switches and a start capacitor in a metal box
and wiring it from the mains supply out to a motor plug.
All that remained was to fit everything back into the
newly de-rusted and spray-painted cabinet and do a test run
with some real washing. All went well; my wife approved,
and with any luck, we will get many more years out of the
old machine.
I learned a lot about the operation of our machine and
now feel confident to solve any new problems.
Finally, I dismantled the poor old donor machine, consigned useful spares to the workshop shelves and gave the
remainder a decent burial at the local recycling centre.
It started gaining time; after 20-odd years, you can expect
some problems. Usually, when daylight saving changes, I
don’t have to adjust the minutes, just the hours. However,
last time, it had gained some time, then after setting it, I
found it had gained again the next day.
Rather than have the incorrect time showing, I switched
it off, and when I got sick of walking into the bed in the
dark, I decided to have a look at it.
Clock radios of this era generally used the AC mains frequency as their time source, and this clock was no different.
It uses an LM8560 IC as its clock driver. Plenty of data on
that chip is available online, albeit as poor-quality scans.
My Teac was very similar to the data sheet circuit as far
as the mains cycle clock circuit goes, and the CRO showed
signals that looked pretty much what you’d expect. The
PSU main electro looked OK, so I rapidly came to the conclusion that the IC had probably developed a fault after 20+
years of service. I don’t blame it.
I found a replacement on eBay from China for less than
$2, including postage. I often wonder how they manage
this – I would spend more than that on postage alone for
the smallest domestic parcel, without even considering my
time, packaging materials and international freight. Perhaps
the Chinese Government subsidises it, or maybe its one of
the reasons Australia Post is losing money. Maybe both.
A month or so later, it arrived, and after walking into the
bed again one night, I was inspired to fit it. It didn’t take too
long, but I was both unsurprised and disappointed that the
display showed gibberish with the new part. It wouldn’t
respond to the time set buttons either.
I checked the orientation and soldering and neither
looked like the source of any problems. After muttering
some profanities and vowing never to buy cheap electronic
bits on eBay again, I picked it all up and unceremoniously
shoved it onto the e-waste pile.
A few weeks later, I saw that my son had left his Panasonic clock radio in his room when he moved out, and
later that evening, it was in place next to the bed with the
correct time. It wasn’t until the next day that I noticed the
display was dim – so dim that I first thought it was turned
off and had to shade it with my hand to read it.
Ahead of its time
D. T., of Sylvania Southgate, NSW has experienced that
strange feeling when you manage to fix a faulty piece of
electronic equipment, only to be baffled how it ever worked
in the first place...
I bought my Teac clock radio over 20 years ago. At the
time, I wanted a combined phone-plus-clock-radio to minimise space used on the bedside table, and this Teac was
the only one around.
While the display was a bit bright at night when it was
new, it wasn’t long before the brightness ‘wore off’, and it
has been a good product overall.
At night, the LED clock is easy to read; much easier than
finding my smartphone and figuring out where the on button is. It is also good to navigate by – late at night, I can
walk toward the display in the dark to find my side of the
bed without disturbing my wife.
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This early-2000s era clock radio uses a couple of singlesided PCBs and mostly standard through-hole parts.
Australia's electronics magazine
siliconchip.com.au
I tried it like that for a while, thinking I didn’t need
to see it during the day, but I found it annoying looking
over and not being able to read it. Obviously, I look at it
more during the day than I thought. At least it was keeping good time.
I thought this might be a case of bad electros causing
the high-voltage feed to a vacuum fluorescent display to
fail, but I quickly ruled that out when I opened it up and
found the display used LEDs. Interestingly, I noticed it
used the same LM8560 IC, with the same package and
everything.
I rescued the Teac from where I left it, then desoldered
both ICs, and soldered the one from the Panasonic into
the Teac. I gingerly switched and was greeted with a nice,
clean, non-gibberish “12:00” flashing in bright green digits. I set the time and let it run.
It would be great if that were the end of the story; however,
I’m slightly embarrassed to say that my diagnosis of a faulty
LM8560 was clearly incorrect because, by the next morning, the time was out again. So, back to the drawing board.
I dug out the data sheet again. For an LM8560 to gain
time, you’d think it would need to receive extra pulses,
causing extra counts. Given the rate of time gain, I calculated it was receiving probably one or two additional
pulses per second.
I measured the main supply electro again – it was
marked 470μF but measured around 350μF. It looked OK
and the rail looked OK on the CRO too, but I replaced it
anyway.
I also checked the clock line. It was a half-wave rectified
line from the transformer via a 100kW resistor and looked
good. However, I noticed that while the data sheet showed
a 1nF cap across the input pins of the IC, the Teac didn’t
have one, nor did it have pads for one. This cap and the
100kW source impedance would have formed a simple lowpass filter with a time constant of 100μs.
I thought about adding that capacitor. I don’t like second-
guessing design engineers; I worked as one for many years,
and usually, the design you choose is what’s ‘needed’.
Clearly, this design hadn’t needed that capacitor for 20
years. But I was getting tired of this repair dragging on for
so many months, so I soldered in a poly I had handy.
It was then a matter of putting it all back together and
trying it out. The initial results were promising, and I was
relieved to find it still showing good time the next day, and
it continues to do so.
So what was it? I’d guess the main supply electro. It was
definitely low in value, and perhaps something was intermittent about it, or its ESR had crept up over time. It reinforces my distrust of old electros.
There could also be a latent fault somewhere else, like a
shorted turn in the transformer reducing the clock voltage
margin. I’m not sure. Interestingly, I note the Panasonic,
like the Teac, had no capacitor on the clock input pin, so
it’s probably optional. I don’t think having the poly cap
there will cause any harm. I’m just glad I can find my way
to bed now without injuring myself!
Editor’s note: increased ESR in the power supply filter
capacitor might not be obvious (unless you use an ESR
meter) and could lead to reduced noise margin on the timing input. The manufacturer no doubt figured they could get
away without the extra filter capacitor, and they were right,
but sacrificed some reliability in saving that cent.
SC
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