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SERVICEMAN’S LOG
Computer abuse
Dave Thompson
As most of you probably know, I don’t
write much about my day job, ‘fixing’
computers. Not because you wouldn’t
be able to handle the dramatic highs
and lows of such a high-octane job;
it is completely the opposite. You’d
be bored to tears for the vast
majority of it. Still, now and
then, something comes through
the workshop that leaves me
speechless!
N
owadays, most 10-year-old kids can fix the things that
usually go wrong with computers. Modern software
and children now handle what was once a very specialised field. Most of the time, it is mundane, with the odd
curly problem thrown in to make things a tiny bit more
interesting. Of course, those rare wins can be very satisfying, even though they are few and far between.
More often than not, they are tempered by having to break
the bad news to someone who has lost their data, or simply
their machine, because it has reached the end of its useful
life. It doesn’t help that most computers are now designed
to last for a couple of years, then die, with all their memories lost, like tears in rain (cue the heart-rending speech
from Blade Runner).
Most tablets and laptops these days work fine for a
while, then suddenly quit, or in the case of laptops (pun
intended!), they physically break because the chassis and
frames are made so thin in an effort to ‘add lightness’. With
many machines, simply opening and closing them a few
times a day – what I’d call ‘normal use’ for a laptop – will
soon break them.
The other issue with many portable computers is the
power socket. On tablets, this is typically a micro-USB
or a USB-C connector. On laptops, it will often be something proprietary, especially in the case of Dell machines,
or something more familiar like that used in most Acers.
Over the years, I have repaired hundreds of power sockets
because they are so easily broken. We’ve likely all picked up
a device by mistake that is still plugged in and put strain on
the cable, or tripped over the cable laying across the floor
to the nearest power point and sent the machine flying!
The resulting leverage on some of the connections is
considerable due to the size of the plugs and leads, and it
is no wonder that sometimes the sockets get torn from the
motherboard.
However, that was not the real problem with a machine
that came into my workshop recently. I repaired the power
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socket on this one a year ago, but it came adrift again. The
client swears it hadn’t been dropped or mistreated, but
as their dad literally had to bolt the screen back on, I had
some questions. I don’t think I have seen a laptop in such
a poor state, and I’ve seen a few!
Young people these days...
An adolescent owned this machine, and in my experience, they don’t tend to look after their tech (or other possessions) very well. The number of units that come through
the workshop that are scarred from schoolyard use has
increased over the years. Many schools now demand that
students have tablets or laptops, often dictating which make
and model they should bring to school.
Usually, this is an iPad or iMac, among the most expensive tech you can buy. One wonders if the schools get a
kickback on these sales, as they used to do when Apples
were first introduced into schools in the 1980s.
When I was at school, not quite the chalkboard days, we
had to have a certain number and style of books. I remember standing in line waiting with a list of requirements as
we all filed past stacks of exercise books of all descriptions.
This, of course, carried on into universities, where students must buy reference books, usually written by professors there, to pass their classes. That’s a rort in itself, but
a subject for another forum!
So now most schools tell students they must have this
Australia's electronics magazine
siliconchip.com.au
Items Covered This Month
• Stress testing your electronics
• Using a chlorinator for rust removal
• Repairing a 27A switch-mode battery charger
• Fixing an LG42LD460 TV power supply unit
• Repairing WiFi-controlled LEDs
Dave Thompson runs PC Anytime in Christchurch, NZ.
Website: www.pcanytime.co.nz
Email: dave<at>pcanytime.co.nz
Cartoonist – Louis Decrevel
Website: loueee.com
or that tablet or laptop. While Chromebooks are popular in
some schools (and are at least reasonably cheap to replace
when they are inevitably broken), most of the more prestigious schools require expensive makes and models.
That is all well and good, but give a 13-year-old kid a
tablet or laptop, and we know they are going to chuck that
thing around, no matter how much it costs. I’ve seen many
almost-new devices with broken screens, dented corners,
drinks spilled down the keyboards, the usual stuff. This
one was slightly different because I had already repaired
the power socket once.
If we do walk away with it plugged in when the lead
runs out, the strain on the socket can wreck it. Whether
it’s a micro-USB or USB-C charging port, as used in many
phones and tablets, or one of the bigger sockets used on
laptops, the result is often the same: breaking the socket,
or some of it, or tearing it off the PCB inside the machine.
These sockets are often held onto the board only by the
soldered joints and perhaps a few Earthing tags. As those
in phones and tablets are usually surface-mounted, there
really isn’t much holding them to the board. Solder is not
glue; it is inherently weak.
If we’re lucky, four tiny fingers of metal extending from
the socket case go through four corresponding holes in
the ground plane on the PCB. Still, many of these sockets
are just spot-glued with some type of component cement
before being soldered in a bath or reflow oven.
There is virtually no strength in that glue or connections,
and in the scenario of walking off with it plugged in, often
the socket is torn from the PCB. In many cases, a few of the
PCB tracks go along with it.
Getting inside the device
Over the years, I have replaced hundreds of these sockets in phones, tablets and laptops. The main difficulty is
that modern devices no longer have a back that can
be popped off to reveal the screws that must be
removed to access the ‘logic’ board.
Almost all phones and tablets now require
going in through the screen, which automatically
makes them infeasible to repair, even if you have a
hotplate for loosening the glue on the screen. Most
screens are now so thin that even a slight twist will
crack them, and new screens are often prohibitively
expensive, if you can even get one!
At least most modern laptops are easy enough to get
apart, held together by about a dozen same-sized screws
and some easily ‘poppable’ plastic clips. The whole bottom
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(or top) typically comes away with just a few ribbon cables
connecting the keyboard or touchpad to free up.
It is nothing like olden-day devices that had tons of
hidden screws of all weird sizes, which were often buried
under the keyboard and even under the rubber bumper
‘feet’ on the bottom, which had to be pried loose to access
the screws. Of course, they had to be stuck back down with
new tape when it was all reassembled.
The worst of those I can recall had a long, thin strip of
rubber running the length of the machine, acting as a single
long ‘foot’, which invariably tore when trying to remove it.
Fun and games for computer techs back then!
Returning to the laptop in question
So, back to this one on the bench. As mentioned, I have
repaired its power socket before. While not old, the computer has had a very tough life. Usually, when I repair one
of these sockets, the repair lasts for the life of the machine
because I use epoxy resin to bolster the strength of the socket
once I’m sure it is all reconnected and working correctly.
One has to be careful doing this because there is not a
lot of room in these things, and it pays to make sure the
top (or bottom) cover will fit on once a fillet of rock-hard
glue is added around the socket!
I don’t know how this current damage was done – the
kid assured the parents that she’d not been rough with it,
but the fact remained that the socket and motherboard were
once again rendered asunder. I could feel it floating around
in there when I probed it with one of my dental picks.
Opening it up was interesting, because most of the plastic
that made up two of the corners, where the hinges for the
screen usually live, was simply not there. The screen itself
had a diagonal crack in the top-left corner. I don’t think I
could damage a machine that badly if I tried!
The screen frame had popped open, and the clips that
are usually there were missing in action, possibly floating
around the back of the panel somewhere. The most obvious
hint that something was amiss is that the husband had broken out his DIY skills:
he had drilled out
and held the righthand hinge and
screen together
with two nuts and
bolts, which he likely
got from the local hardware
store.
I thought I had pretty much seen
everything over the past 25 years of
doing this job, but I haven’t seen a
post-industrial repair like this
before!
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July 2024 87
That said, the repair he had made was quite sound. I
have no idea how he missed the LCD panel while drilling
the two holes; it was likely pure luck. If he’d touched even
the frame of it with the drill bit, it likely would have put
yet another crack in the screen, and if he had gone through
one of the ribbon cables or connectors, it would have been
game over, man, game over!
In the above photo, you can also see the black-and-white
WiFi antenna wires, which are ultra-fine shielded cables
that usually wrap around the edges of the panel, ending
up at the top, on either side of the camera. In this case, the
black one should be wrapped around the left-hand side of
the panel, instead it is hanging in the breeze through the
broken hinge section on the right side.
Both of these wires start on a removable/replaceable module on the motherboard and are routed through channels
designed for them, then pass through the lid hinge’s normally enclosed cavities into the frame around the screen.
Not any more; on this side, the black lead has been bundled
with the white lead, and the white wire has been severed
almost at the hinge area; it simply pokes out into space.
I imagine this would compromise the WiFi performance,
but I have seen machines perform quite well before with
those wires wholly disconnected from the module. That can
happen when a tech has neglected to replace the tiny coax
plugs at the ends of these cables onto their tiny sockets.
On older machines, to get the motherboard out, I often
had to take the WiFi module out, as it was fouling on the
chassis, and in some cases formed part of the motherboard
support structure due to it being screwed into place. Those
antenna leads must be routed into their channels and reconnected during reassembly. If the user is close enough to the
router, it would still work, but the operating range would
be much shorter. It certainly isn’t ideal to have one poking
out the side of the machine!
So, the hinges are compromised on both sides, although
only the right side has been fixed with bolts from the shed.
The left hinge floats in the broken panel frame; the little
metal inserts in the plastic turrets that usually support the
hinge screws have all broken away and are sitting on the
screws still attached to the hinge.
This was looking increasingly pointless to repair, and I
hadn’t even gotten to the motherboard yet.
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Disassembling the case wasn’t as difficult as I thought
it might be because most of the screws weren’t holding
onto anything anyway! Most of the clips that usually kept
things nicely flush had sheared off, so it was simply a matter of getting a spudger (in this case, a guitar pick I use to
open cases) and going around the edges to see what would
come apart.
A few of the screws still bit into their threads and held the
case together, so I removed those. The bottom came away
cleanly and I could clearly see the power socket floating
loose in the recess that usually helped locate it.
The plastic surround that helped support it had broken
away last time, and I could see that some of the epoxy resin
was still where I’d put it, except that the socket had broken
out of it. There must have been a lot of force because that
stuff is pretty tough, especially when it has lots of nooks,
crannies and surface area to grab hold of.
Given that the plug on the power supply was bent at a
crazy angle, someone had really yanked on it to cause this
much damage!
I fished the socket out and could see it had torn the
connections from the back of the socket. It had also taken
some of the corresponding PCB tracks off the motherboard;
there was nothing left there to solder anything to. With the
previous repair, I could at least resolder the socket before
testing and gluing it in place, but now, a new motherboard
was the only real option.
The glue I had added previously had also torn some
tracks as part of it broke away, making even more of a mess.
Maybe it wasn’t such a good idea after all, gluing it on, but
I have done dozens of repairs like this over the years, and
to the best of my knowledge, all those repairs lasted for the
laptops’ natural lives.
This one is an anomaly; the sort of damage I’m looking at
can only be caused by gross mishandling or perhaps being
thrown in a tantrum or similar. I didn’t ask; all I was told
was that the daughter assured her dad she hadn’t dropped
it. Maybe she was using it as a cricket bat! I don’t know,
but I’ve seen less damage from machines that have fallen
down the stairs or have been run over.
I went through the motions of trying to source a ‘new’
motherboard, but the best I could do was a ‘refurbished’
one out of China. The last one I bought from sources there
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didn’t work on arrival, and I took a big hit on that, so I
wasn’t keen.
Given that the rest of it was in such dire shape, I made
the call to the dad and told him the bad news. He was philosophical about it, likely envisaging having to buy a new
device for his daughter so that the same thing could happen to it. Parenting is tough, I guess!
I put it back together as best I could, and they duly
came and picked it up, the daughter looking suitably sad
and sorry. I gave them the good news that her data was
all there, so I could easily transfer it when they got a new
one. I didn’t have the heart to charge them after returning
the wreckage.
Repurposing a pool chlorinator
I spotted a couple of pool chlorinators on a recent visit
to the local tip shop. One was pretty beaten up, but the
other was in good condition, apart from having the power
cable cut off.
I decided to grab the better one of the two, as I’ve been
using one of these units for my electrolytic rust removal
bin for several years, and it would be handy to have a
spare. When we got home, I put it away and didn’t think
any more about it.
About a week later, my pool chlorinator stopped working. On disconnecting it, I noticed that one of the front
panel LEDs flashed. Investigating further, I found that the
35A bridge rectifier had failed. I have spare rectifiers, but
I decided to check out the “new” one to see if it worked.
If it did, I’d put it into service instead of repairing the one
I had been using.
I could see why the power cable had been cut off; the
outlet socket on the bottom of the unit was broken, exposing live terminals. The first thing I did was to remove the
outlet socket and rewire the unit to bypass it and the timer,
which I didn’t need anyway. I then fitted a new power
cable and plugged it in. The ‘No Water Flow’ LED lit up,
indicating that the unit most likely worked.
The unit has two heavy output leads, one for positive
and one for negative, plus a thin wire for water flow monitoring. I connected the thin wire to the negative terminal,
and the unit then started pulsating. That was unusual, but
it was likely because it didn’t have a load.
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I connected it to the rust removal bin, the pulsating
stopped and the Chlorine Output meter showed that the
unit was working. It could be adjusted by turning the output control. The old chlorinator has a 9V 20A transformer,
which I could always use for something else. The replacement unit has a 9V 27.8A transformer and two bridge rectifiers instead of the one in the old unit. So this unit is more
powerful than the old one.
I made two plates, then pop riveted one over the hole
where the timer had been and the other over the hole where
the outlet socket had been. That made it ready for use.
I have been using electrolytic rust removal for several
years. It is very handy for cleaning up rusty tools and other
items but only works on ferrous metals. Once, I picked up
a 6-inch vise at the tip shop that was totally seized. After
three days of treatment, I got it apart, and another three
days later, it was cleaned up and I could paint it and use it.
B. P., Dundathu, Qld
Editor’s note: for information on the process, see our article in October 2014 (siliconchip.au/Article/8041).
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July 2024 89
Switch-mode battery charger repair
This Innovative Energies SR750-24 charger converts
its 230V AC input to 27.5V DC at up to 27A. The charger
had not been used for some years, so its failure was not a
great surprise. I agreed to see if it could be repaired, but
an online search showed that it was a legacy item and
quite a few years old, so spare parts supply could be difficult to obtain.
With some degree of trepidation, I took possession of the
charger, which was not easy to carry as it weighed 5kg and
measured 350 × 200 × 75mm. Removing six small screws
allowed the cover to be lifted off and the reason for the
weight became apparent – it was fitted with two massive
internal aluminium heatsinks and four large coils (chokes
and/or transformers).
The probable main reason for the failure was also immediately obvious: two 0.68µF 275V AC WIMA capacitors
had ‘spilt their guts’ of the insulating oil contained within,
which was spread all over the main PCB in their immediate area. I considered that the oil could contain nasties, so
I kept my bare hands away from it.
This PCB area included several small common components and ICs. Later investigation revealed this circuitry
was in the charger voltage and/or current control.
The first problem was removing the main PCB from its
case to access these capacitors’ solder side. That turned
out to be quite simple, as the mains input wired connections and the output DC connections are easily pulled off
PCB-mounted spade connectors. Then, after undoing eight
small screws, the PCB lifts straight out.
This revealed that each of these capacitors was wired
in series with the incoming mains Line and Neutral conductors, coming before several mains filter/noise suppression components. This also indicated that these capacitors
were being used as simple AC voltage-dropping devices, so
their capacitance values would not be particularly critical.
As the series mains input 10A fuse was not blown, other
major components had probably not failed. The high-
voltage stress placed on these aged capacitors when the
unit was switched on could explain their failure.
The next step was to procure and fit replacement capacitors of similar size and specification to the original failed
capacitors. The closest available value stocked by Jaycar
was 1µF, so I fitted them temporarily (they have a 50Hz
reactance value of 3.2kW versus 4.7kW for 680nF). I thought
that was close enough for a go/no-go test.
I cleaned the spilt oil off the PCB as much as possible
before soldering in the new capacitors and reconnecting
everything. While standing well clear, I switched the mains
power on. This smoke test was successful as there was no
smoke, no component appeared to overheating, the Charger Load display came on and the DC output measured
about 27V.
I subsequently connected the charger to a suitable 24V
lead-acid battery and it charged the battery in the expected
manner. After a further soak-test period, it was still operating. So, another electronic unit that would have cost a
considerable sum to purchase in its day was saved from
the scrap heap by about $5 of replacement parts.
G. C., Wellington, NZ
LG 42-inch LCD TV repair
After a successful service of 15 years, my LG 42LD460
LCD TV failed. During the last cricket World Cup, hosted
by India, the TV served flawlessly! However, I have been
unable to switch it on for the last three weeks. The LG TV
expert came and opened the back cover deftly. After a few
tests, plugging in and out a few cables here and there, he
Left: the
failed
SR750-24
battery
charger.
Right: the
42-inch LG
LCD TV
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joyfully declared that the power supply unit was beyond
repair.
When I asked for a replacement, he chuckled and, after
a few calculations, revealed that it would cost me about
INR 11000 ($200) for a replacement board and would take
about a month to get. He said spending so much on repairing a 15-year-old TV was not a good idea when a new and
better TV only cost about twice as much.
After he left, I brought down the TV from the wall,
opened the back cover and checked the power supply.
I had to remove 16 screws to remove the back cover and
found two boards, the TV motherboard on the left and the
power supply on the right.
The power supply has four connectors: the mains input,
a ribbon cable to the motherboard and red and black wires
supplying the backlight. While all the other cables came
out easily, the ribbon cable gave me some trouble. I spread
the locking fangs with a small screwdriver and it came out.
The power supply board has a surface-mount fuse, which
I knew the LG expert checked. I checked the first bridge
rectifier of four diodes and it was OK. All the electrolytic
capacitors seemed fine, with no bulging, and I didn’t see
any blackened resistors. The rectified DC finally comes to
a six-lead STR-W6053N IC, which converts it to lower DC
voltages for the motherboard.
The IC’s data sheet reveals that there is a feedback signal that comes from the TV motherboard through lots of
circuits. If the motherboard does not produce the requisite
feedback signal, the PSU will not work. Since the repairman said the power supply was dead, I removed it and
took it to a local TV repairman.
He told me that the TV is required; he can’t do anything without it. I asked him if he could visit my house to
check the TV in situ as shifting a large TV is difficult! His
answer was no.
I searched the internet for TV replacement parts and
found many shops that deal in TV spares, but couldn’t
find my model listed. Frustrated, I rang one shop, and they
quoted me around INR 4500 ($82) for a new power supply. I immediately placed an order and crossed my fingers!
The power supply arrived four days later, neatly packed
in a box. I opened the box and fitted the module into the TV.
Nothing happened! It was still dead. Frustrated, I called the
shop again and told them that the module seemed defective
as the power supply was still not coming up.
The man on the other end of the phone had a good knowledge of TVs. He asked me all the details of the fault: how it
started, what the branded TV expert opined and my amateur repair process. He then told me that, in all probability,
the TV motherboard was defective, not the power supply.
He also informed me that he had seen many similar cases
of incorrect diagnoses by the branded experts.
He told me that I could return the power supply module
and get a refund or buy a TV motherboard. If the power
supply turned out to be OK, I could return it for a refund.
Therefore, I end up coughing out another INR 5000 ($91)
for a motherboard card. The card arrived in three days
from Hyderabad.
The motherboard card replacement is a little more delicate as it involves the removal of two flat ribbon cables,
but they came out pretty easily (just open the lock...), and
the new card was in place quickly. And the TV woke up
after a slumber of 29 days! Before boxing up the TV, I tried
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July 2024 91
the old power supply, and it also turned out to be working! So the TV motherboard card was the culprit all along.
The power supply card has been returned for refund and
the TV is still working well. At one point, I almost made
up my mind to get a new TV as my wife was missing her
daily serial shows. Only my persistent mind kept the hope
of a successful repair alive.
TV companies will always lure you into making new
purchases by telling you that parts for older models are
unavailable etc. But don’t get fooled. The old parts are
available all over the internet. Search for them or even call
them. They will certainly help you out because they also
want to sell their goods!
B. S., Kolkata, India
Repairing a WiFi-controlled mains LED light
I purchased several WiFi-enabled ‘smart’ ceiling lights
from Bunnings a while ago. A nifty app allowed me to change
the brightness and colour temperature using a smartphone.
While that was great in theory, we found that we typically set the colour and brightness once and then, around
99% of the time, simply used the light switch to turn them
on or off when needed, as these lights were in our dining
room and TV area, not in a bedroom.
However, these clever lights proved highly unreliable.
Two out of four failed and, as is the norm these days, it happened just after the warranty expired. Initially, they only
partially failed, refusing to respond to WiFi commands but
still turning on via the light switch at a usable brightness.
So, we tolerated this unfortunate failure and continued
using them as ‘dumb’ lights.
Regrettably, after several months, both lights failed
entirely within a few weeks of each other. Not wanting to
spend a significant amount on a new light that would likely
be just as unreliable, I decided to investigate whether they
could be fixed.
Removing the first light, I found that all the electronics
were on a large PCB, which appeared to be made of ceramic
or a similar material. Whatever it was made of, it was clearly
designed to dissipate the heat produced by LEDs, and it did
so very effectively. Due to its excellent heat conductivity,
I had to use a much larger soldering iron tip than usual.
I also noticed that the light’s white metal outer case acted
as a heatsink, a necessary feature since excess heat is the
leading cause of premature LED failure.
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Tracing the circuit proved extremely difficult due to
the opaque ceramic substrate. However, the basic design
quickly became apparent. The mains was converted to
a current-limited 24V DC using a WS-LV24-G24L-L LED
driver module. Next was a tiny SMD 5V switching regulator powering a TYWE3S 16-pin ESP8266 WiFi controller
module, along with an unmarked microcontroller.
Finally, a couple of Mosfets were used to drive the two
banks of LEDs (daylight [5000K] and warm white [3000K]),
with each Mosfet controlling a single bank. These two banks
allowed the app to set the light’s colour temperature by
adjusting the power ratio of the two LED banks.
A multimeter confirmed that the 5V power rail was OK,
measuring correctly at both the MPU and WiFi modules.
Next, I measured each SMD resistor, and they were all
within spec. I then unsoldered and tested each Mosfet,
and they were also both OK. The fault must be in either
the PCB tracks, the MPU or the WiFi module.
However, it was virtually impossible to check the PCB
without a circuit diagram due to its optically opaque substrate.
It appeared impossible to replace the unmarked microcontroller without a part number or, more importantly,
a way to obtain the firmware. The last suspect was the
ESP8266 WiFi module, but a Google search showed only
one hit for it worldwide, and it was nearly as expensive
as a new ceiling light.
So, it appeared that replacing any of these parts wasn’t
a viable option. After some thought, I wondered if it was
necessary for the WiFi feature to work. I could convert the
lights to ‘dumb’ lights with just one or two resistors!
As I prefer daylight white LED lighting, I only needed
to solder one 5W, 10W resistor between the +24V supply
and the daylight white LED bank, bypassing the Mosfet. If I
preferred a more ‘warm’ light, I could have used two resistors, one for each LED bank, although the resistances might
have needed to be increased to get the right final brightness.
While not the most elegant solution, it converted the
non-functional ‘smart’ lamps into functional ‘dumb’ lights
controlled by a light switch. While it would have been more
elegant to repair the WiFi functionality, this makeshift solution got both lights working for less than $2, which was
much better than spending $150 to replace both with new
smart LED light fixtures.
SC
G. C., Cameron Park, NSW
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