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SERVICEMAN’S LOG
This time, it's personal!
Dave Thompson
If I were living up to my increasingly curmudgeonly ‘old man’ persona,
I would complain about the fact that nothing is made to last these days. I
know that I’m just a grumpy old sod, but in my defence, things just really
aren’t made the way they used to be.
We’ve all read the servicing stories here detailing how
people needed to swap the motor out on a 40-year-old washing machine or kitchen stand mixer because they finally
wore out after all those years of faithful service. However,
nowadays, we all too often hear tales of a 'smart' TV that
lasts less than two years or an expensive kitchen appliance
that fails after just over a year (sometimes sooner!).
Most of us have experienced this. My wife has had several of those trendy fitness watches that are all the rage
now. She has had two in the past few years, and both failed
either physically (the flimsy straps or case breaking) or electronically (the screen failing). Those things are not cheap
to buy, yet they are cheaply manufactured.
There are no spares for them other than third-party products from sites like AliExpress, so essentially, they are
throwaway items. Being old-school, I’ve been wearing my
Tag Heuer Professional watch every day for 30 years now,
and it still looks like the day I bought it.
It is definitely not a throwaway item, and while it has
been regularly serviced, spare parts are still available from
the maker if need be (the bezel detent spring has been
replaced twice). My wife now has a Garmin smartwatch,
which seems to do what it says on the tin. It also appears
very well-made and is as robust as those devices need to be.
So, companies can do it if they want to. I feel that because
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so much of technology is here today, gone tomorrow, the
manufacturers just don’t expect anything they produce to
last long enough before it is essentially redundant, so they
don’t care that much about repairability or even providing spare parts.
In my bread-and-butter trade, computer service and
repair, a particular computer brand (that always reminds
me of brown sauce) became a joke for its high failure rates.
So much so that my customers commented, on many occasions, that the company must have built a timer into the
machines because they always seemed to fail just outside
their warranty period.
I’m not claiming that this company was the only one
whose computers failed – that happened across the board.
Honestly, their failure rates were more likely tied to
mechanical hard drive reliability (or lack thereof) than a
secret motherboard timer, but I’m not entirely discounting
that conspiracy theory!
Of course, we all know nothing is made to last these days.
Everything has become consumable because technology
marches on at an alarming rate. Last year’s $10,000 OLED
TV is today’s $1500 bargain bin special, replaced by some
new QDLED, 4XLED or ZZYZXLED models (I might have
made some of those up).
Moore’s Law (the idea that the number of transistors
on a chip doubles roughly every 18 months) might seem
naïve now, but as a product of his time, it is still valid.
The increasing complexity and reduced cost of integrated
circuits have greatly impacted how and what we buy and
what is being created in those massive factories overseas.
Despite the bad things that come from it, the beauty of
all this technology and manufacturing is that relatively
inexpensive consumer electronics are widely available for
anyone in all but the farthest-flung reaches of the planet,
even New Zealand!
One of the first truly ‘consumable’ items many of us experienced was the venerable computer printer. Early printers
were made like old English cars. Solid, heavy, noisy and
mostly reliable. Later printers were flimsy, but at least they
produced good-quality prints when they worked.
However, the printer companies eventually realised they
could sell the printers for less, often below cost, and make
up for it by charging a King’s ransom for the ink (and sometimes other consumables).
I once worked out that for a typical $100 printer, an average customer would shell out $2000 for ink over its lifetime. No wonder all those ‘refill your own ink’ businesses
Australia's electronics magazine
siliconchip.com.au
Items Covered This Month
•
•
•
•
•
•
A device with one foot in the grave
A quick fix for a failed start capacitor
Cleaning a dirty preamplifier
Fixing a muffled woofer
The old days of TV antennas
Simple troubleshooting
Dave Thompson runs PC Anytime in Christchurch, NZ.
Website: www.pcanytime.co.nz
Email: dave<at>pcanytime.co.nz
Cartoonist – Louis Decrevel
Website: loueee.com
flourished under that business model. At one point, printer
ink was the most valuable product on earth by weight!
Many people would buy a new printer rather than shell
out for expensive cartridges.
Because consumers who wanted decent colour printers
had few options at the time other than ink-jet or bubble-jet
printers, we all printed millions of pages with them and
fed several booming industries.
The problem with them is that when a 50¢ plastic piece
of hardware fails, we can’t buy spare parts to repair it.
Manufacturers soon decided they didn’t want capital tied
up with spare parts sitting on shelves, and they’d rather
us buy a whole new printer. That’s what the consumable
business model became. The printer itself became the consumable and that is still the case today.
It was a boon for the manufacturers, but making printers
a throwaway item sure created a lot of waste!
Now it is also the same with mobile phones, tablets, laptops, fridges; anything with a shelf life of less than a couple of years. Even if made available, parts are expensive
and often impractical to source. It is great that the Right To
Repair movement exists, but they have only made a small
dent in the problem so far. If the parts aren’t readily available, we still have to take the hit and chuck the item away.
There is certainly a wealth of gadgets and tools out there
designed to keep us buying more.
One such device is a foot sander. I don’t know the actual
name of it, but you’ve likely seen these things for sale at
pharmacies and big box stores. They are designed to remove
dead skin from feet and prevent corns and other maladies.
A motor and gearbox assembly spin the replaceable abrasive roller, and it’s used very much like a palm sander,
except for feet.
They are usually battery-powered and come with a charger and rechargeable batteries hard-wired inside. Some are
marketed under brand names, but many are just generic
and sold cheaply. Again, they have consumables to keep
the cash rolling in, in the form of abrasive sanding rollers
that wear out all too quickly.
A cynic might think these could be made of sterner stuff
and last a lifetime, but where’s the profit in that? My wife
has one, of course, and it has done some work. We found a
Chinese source for the rollers, so we didn’t have to pay the
exorbitant prices at the local outlets. These replacements
might not be quite as high quality, but considering their
low cost, they work well.
She went to use it the other day and had it charging as
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usual. When she picked it up, it was smoking hot! She
called me in, and she was right; the thing was almost too
hot to hold. Not only that, it also wouldn’t turn on. Flick
the switch, nada. Something was evidently wrong inside
there, which meant I was duty-bound as a Serviceman to
open it up and have a look as soon as possible.
This is a simple device, but was it simple to open? No, it
was not! Only three small PK screws held it together, but it
seemed to be like one of those puzzles where nothing will
come apart until some magic happens. I could separate the
case slightly and see the batteries inside, but pulling the
abrasive wheel end apart seemed impossible.
The roller itself just popped out, but the rest of it seemed
to be either glued or clipped together in a way I couldn’t
figure out. A central piece needed to be removed, but it
appeared to be nailed in there; I couldn’t move it at all.
There were no hidden screws under a sticker or anything
like that.
In situations like this, the urge is to use more salt and
pepper and make something move, but I thought I would
break something if I did that. It seemed impossible, so I
did what anyone would do and walked away to ponder the
problem. A fresh set of eyes might be the answer.
I returned the next day, and fresh eyes didn’t help; I was
just as perplexed. I poked and prodded to no avail and, in
the end, just decided to use brute force where I thought it
should come apart. I figured that if it broke, I’d repair it or
just get a new one; this ‘simple little job’ had turned into
a real mission.
Thankfully, it did come apart in the way I thought it
would, and it appeared to have been made purposely that
way due to the clips inside it. I was fortunate not to break
any off, and I got it apart without damage. It took a lot of
blue language and struggling, though; this is the curse of
The Serviceman!
I wonder why someone would design something like
that – after all, it isn’t like they were trying to prevent me
from repairing it. Or were they?
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March 2024 99
Either way, I could see the problem right away. One of
the internal AA cells had vented and dumped a gloopy
mess all over the PCB. I could deal with that. I had a couple of commercial, high-quality NiCad cells that I could
use to replace both.
The heat appeared to have been generated by a half-watt
resistor in the charging circuit. It had been mounted standing clear of the board, so this was obviously by design. The
board was a little scorched underneath, but I desoldered
and pulled one leg and used my LCR meter to measure it,
and it was still within 5% of its marked value, so I just
resoldered it back in and left it.
The batteries were a different story. The blown one
measured about 0.1V, while the other was 1.1V. That was
understandable as it hadn’t been charged, but I was going
to replace them both anyway.
They were connected to the PCB by the usual nickel
straps many batteries come with these days. These are typically spot-welded on and are rolled to form a solderable
connector. Desoldering them from the board is easy; getting them off the board was a different story!
I don’t know what the military-spec construction adhesive they’d glued these cells to the board with was, but it
was as hard as nails, and I feared I would have to cut the
batteries off with a Dremel or similar rotary cutting tool.
The board itself was single-sided, so nothing special, but
it was only half a millimetre thick and very flimsy. That
seems to be the modern way.
This meant that if I went Arnold Schwarzenegger on the
batteries with a pry bar (screwdriver), the board would
break beneath it.
I loaded a new blade into one of my hobby knives and set
about trying to cut the dead batteries off the board. This is
the sort of job horror stories are made of; super-tough glue,
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poor access and a hyper-sharp blade are a recipe for disaster. As a long-time aeromodeller, I have been using these
knives since I was a boy and have many of the distinctive
straight-line scars on my fingers and hands to prove it!
Luckily, this time, with decades of cautionary experience, I was OK. Still, one has to be constantly careful with
tools like this. A moment’s lapse in concentration can really
ruin someone’s day!
The batteries did have a shrink-wrapped coating on them,
so I was able to cut the cells free from that and at least get
the bulk of them out of the way. But that left the cement
and the jackets still stuck on the board. I trimmed what I
could of the leftovers and tried sitting the new cells in the
same position.
That worked, but it wasn’t ideal. There was no way I
could remove that glue from the board without damaging
anything, so I just mounted the new cells on the remains
of the old glue and used a spot of gel cyanoacrylate adhesive to hold them in place. I have a small spot-welder for
this type of battery work and used that and nickel strips
to connect the new NiCads together.
These batteries have a much higher capacity than the
old, dead ones. While the charging circuit might not be
optimal for them, they would trickle charge without too
much bother. Also, the runtime of the repaired unit would
be about twice as long as before.
Now all I had to do was reassemble it and I’d be finished.
Well, that was easier said than done. Trying to manipulate the three main parts back together was like trying to
herd cats into a bath. I know how it came apart, but using
brute force doesn’t work as well when trying to get it back
together as it did when getting it apart.
It felt as if doing the same thing in reverse was definitely
going to break something. The designer of this thing must
have worked for Reginald Perrin’s company, Bastards Inc!
I spent a good while sweating and coercing it back
together. I can’t imagine how those poor sweat-shop workers making these things cope with it. I suppose they have
their tricks and methods (perhaps even a jig), but this was
such a frustrating gadget to work on. Given its relatively
low price and throwaway vibe, it seemed increasingly
ridiculous for me to even bother with it in the first place.
Still, that’s what a good Serviceman does. If it can be
fixed, it should be fixed. I wonder if, in the future, there will
be any servicemen (or women) left who will even attempt
to make things right when they see something broken. I’d
like to think there will be, but time will tell.
I managed to coerce the parts back together and screwed
the PKs back in. After inserting the replaceable abrasive
wheel, I switched it on and was rewarded with a fast-
spinning roller. I would be very careful about getting this
thing anywhere near my skin, but I guess that’s the beauty
industry for you!
My wife was grateful to have it back, and after a few
months, it is performing well and charging correctly. While
this was a ‘throwaway’ item, I feel that we should be repairing as many of these types of gadgets as possible because
the e-waste we humankind are generating is appalling.
I would be all in favour of making things to last again,
or at least making them repairable, with traditional spare
parts business models returning. I don’t think much good
can come of just making things to throw away, especially
with toxic electronics and batteries onboard.
Australia's electronics magazine
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A quick dryer repair
G. D., of Mill Park, Vic fixed a machine with a common
fault, but the exact way it failed was a bit surprising...
A few weeks ago, my daughter called to say her clothes
dryer would not start. She had just finished one load,
and the machine just made a humming noise when she
tried to start the second. I called in the next day and sure
enough, a humming noise was all it would do, so off came
the back cover.
The problem was immediately very obvious. It was a
failed start capacitor, but the failure mode was something
that I had not seen before (photo below) – it looked like it
had grown a tumour! A trip to a local supplier provided
a replacement, although not in the same package format.
Once installed, the machine worked as it should.
rest of the PCB looked acceptable, evidently having been
made on a different assembly line. Not being able to identify the unit meant I didn’t have a circuit diagram. Still, it
appeared to be a straightforward audio preamp with RIAA
correction circuitry switched in or out.
I cleaned and tinned the switch terminals, checked the
switch, replaced the missing tracks with wires and reassembled it all to give it a try. Success! Everything was working
as expected. In the end, an easy fix for a bad job.
Fixing the muffled woofer
T. T., of Bribie Island, Qld, had a friend ask him to look
at his audio preamplifier, which he said was crackling and
sometimes wouldn’t work at all...
I agreed, and when I received the preamp, I found that
it was housed in a small plastic enclosure with RCA sockets marked “Aux”, “Phono” and “Output” on the back.
On the front was a switch for selecting “Aux” or “Phono”.
There was no brand name or model number visible anywhere, which made me suspicious, but he assured me that
although he had bought it many years ago, it had been from
a reputable shop in Sydney, and it had worked fine when
he bought it.
Opening the case revealed a PCB supported only by being
soldered to the switch terminals. When I say soldered, that
was a stretch of the imagination! It looked as if coffee or
some sticky, brown cold drink had been spilled onto the
PCB while the factory worker attempted to do the soldering (see the photo at lower right).
Three of the six switch terminals had only vestiges of
solder on them, and the copper of the corresponding PCB
tracks and pads was badly corroded and lifting from the
board. The copper pads were just touching the switch terminals here and there. Quality control in that factory must
have been on holiday that day!
I had to scrub the dried residue from the board, which
did away with the lifted and corroded copper tracks. The
P. M., of Christchurch, New Zealand recently came across
some bouncing speakers. That is, after he fixed them and
they were put back into service, they came back again...
A local music venue has two powered speakers for its
main PA system. One failed and was delivered to my door.
The problem was that the woofer was no longer woofing.
I am familiar with these units, so I dismantled the amplifier module after confirming that the problem was with the
amplifier and not the speaker driver.
This module is not dissimilar to the one used in the
500W Class-D Mono Amplifier (April 2023; siliconchip.
au/Article/15730). It uses two IRF4227 Mosfets driven by
an IRS20957 driver IC to deliver approximately 500W.
A common problem with these units is the output inductor that filters the switching frequency from the output.
This component works hard, as all the output current flows
through it. The manufacturer has supplied an uprated coil
to be used as a replacement.
I fitted a new inductor and tested the amplifier, and all
was well. After reassembly, the speaker was returned to
the customer. A few weeks later, the other speaker from
the venue turned up at my door.
This time, the woofer was cutting out intermittently. After
a few checks, I replaced the output inductor and could not
get the fault to occur again. The speaker was returned, but
a few days later, it boomeranged.
Once again, I could not get it to fault, but I had an idea. I
had a dead module from a previous repair of another unit.
At that time, I could get a replacement module from the
supplier, but this time, when I checked, they didn’t have
any more. So I would repair my dead module and swap it
for the troublesome one.
The very obviously failed start capacitor from a clothes
dryer.
This PCB from a preamplifier had little to no solder left on
the terminals of one of its switches.
The case of the sticky preamp
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Australia's electronics magazine
March 2024 101
I figured the older one had died because of the output
inductor, so I first replaced that and then the shorted Mosfets, and to be sure, the driver IC as well.
But when I fitted it to the speaker, it refused to work.
I was running out of ideas, so I asked the supplier if I
could send my module to him to see if he could repair
it. He agreed but reported that it worked perfectly when
it got to him.
Like the speaker, I was baffled, and asked if he had any
suggestions. He asked if I had checked the low-side bias
supply that comes from the separate power supply board.
This supply is roughly 12V, sitting on top of the main negative rail, and is used to switch the low-side Mosfet. It comes
from a separate winding on the switch-mode transformer
and is regulated by a 7812.
Apparently, it is not uncommon for the legs of the regulator to fracture due to vibration from the speaker. I checked
the regulator and found it was solid, but the pins on the
transformer had fractured solder joints. A quick touch-up
and the speaker was back in business.
A couple of months later, one of the speakers was back,
this time with a different fault. After running for a while, it
would start to make a fizzing noise from the high-frequency
horn. These speakers are bi-amped, so they have a separate
amplifier driving the horn. I only heard the fault a couple
of times, but it disappeared each time I got near it.
I decided that the only way to narrow down the problem
was to get the other speaker and swap modules between
them. The electronics in these include a preamp board
and a DSP board, which handles the crossover and equalisation. I swapped both from one speaker to the other, but
the fault remained with the original.
I swapped the amplifier boards and let both run on test.
Of course, neither of them faulted.
I accidentally left them running all night; the next morning, one was not working at all. It was not the one that had
the fault originally, so the failure was with the amplifier
board. I swapped the board for my repaired one to save
time, and all was well again.
The HF amplifier on the board consists of a high-power
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The repaired amplifier module from the powered speakers.
Class-D IC (TDA8954TH) mounted under the board in contact with the heatsink, plus a few other components. I suspect that IC was the cause of the noise, and it eventually
failed completely. As it is an SMD device with 24 pins, I
was in no hurry to replace it. Maybe next time.
The old days of TV antennas
S. G., of Bracknell, Tasmania was a bit shocked when he
had to deal with a very messy TV installation...
This happened many years ago, well before digital television; I guess it was around 1985. I was working as a contractor installing television antennas when SBS Melbourne
was transferring from channel 0 to UHF channel 28. Work
was coming in fast, and it was all techs ‘to the pump’ for
the upgrade as many people still wanted to watch SBS.
Many installations needed a total rewire, replacing the
old 300W cable with newer 75W cable to all outlets due to
300W cable being very lossy at UHF (477MHz for channel
28). Some jobs were easy (one antenna to one television),
while others needed much more work. Depending on the
job, we would be there from an hour to maybe a whole day
for bigger sites.
This job was one where I thought I would be in and out
real quick. How wrong I was!
The customer was one of Melbourne’s big hotels/motels,
with a basic MATV system that serviced the main bar,
sports bar and ladies’ lounge, with another feed over to the
motel part of their complex. Thankfully, the whole system
was wired in what looked like good-quality coaxial cable.
The problem was that none of the televisions around
the hotel or the motel had much reception; what could be
received was very poor quality, varying from channel to
channel and television to television. It was a real mess.
Where to start? First, I measured the signal at the main
distribution amplifier (a KingRay DW40). This turned up
trumps; I found very little signal. So, up on the roof (flat,
thank goodness) to find the big VHF antenna. Looking
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closely at it, I found the balun’s plastic cover was not
installed properly and had become dislodged, sliding down
the coaxial cable, allowing water into it.
After a quick talk with the manager, it was decided to
replace the antenna with a combination UHF/VHF antenna
and replace the water-damaged coaxial cable as required.
The antenna was mounted above the main office, with
the coaxial cable running through the roof and down an
internal wall.
Having done that, I finally had a solid signal to feed into
the distribution amplifier. Readjusting the gain and slope
controls at the test point on the amplifier brought all of
the televisions into working condition, with no crosstalk
or inter-channel interference.
I went around the hotel, checking the televisions as I
went; the main bar still had reception problems. The Teletext wasn’t working very well; it was important as the public in the bar would want to see the sports results.
The bar had sixteen 26-inch televisions, all tuned to
different Teletext pages. They were all sitting on a heavyduty shelf behind the main bar. After a bit of cable tracing
(wires were going everywhere, including PA and phone/
intercom cables), I found that all these TV sets were fed
from one coax cable via a series of splitters.
It looked like the system had grown over the years, but
the splitters were all of the wrong types, and someone had
used a couple of 300W four-way splitters and had made
a real mess of the job. I had to rewire the lot with the
correct 75W splitters. Some sets had the old-style tomb
balun, with the coaxial cable direct to the screw terminals of the balun.
All the televisions were fed from a single coaxial
cable, which I traced back to the wall, expecting to find
a wall outlet, but no! All I found was a 75W Belling-Lee
line plug and socket. I needed to pull it apart to measure the signal coming from the amplifier and adjust for
the signal level.
The next thing I remember was getting a strong electric
shock through one arm, across my chest and through my
other arm. It nearly knocked me off my ladder! Sitting down,
I had a short break to think about what had happened, and
that’s when the penny dropped.
All 16 sets were of the same manufacturer and model
and likely would have been powered from a switch-mode
supply. The antenna input socket would have a couple
of capacitors to isolate the input antenna socket from
the chassis, which usually sat at around half the mains
supply voltage. I had 16 in parallel, each putting a small
current into the antenna cable. In total, it was enough to
pack a wallop!
After fixing and replacing the coaxial cable, installing
proper splitters, an isolated wall outlet, and tidying up
the cabling, I was greeted with a first-class signal, no more
Teletext dropouts, and a happy manager. I also installed an
AC/DC isolator at the head end, and to the main feed that
went to the motel wing.
I ran into a similar situation later, when I was working
in Mildura for a local television repair centre around 15
years ago.
A customer from one of the outlying cattle stations on
the other side of Wentworth called me to say her television reception had failed. The next day, I loaded up the
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104
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work van with what I thought I would need: new antennas,
masthead amplifiers, cable, masts, guy wires and sundries.
It took me just over an hour to get to the farm gate and a
further 15 minutes to the farmhouse.
The television reception was woeful. The customer had
several televisions around the house (four in all). The main
one was a little 20in Sanyo set that had stood the test of
time. Turning the set on, I was greeted with a screen full
of snow.
I was about to check the aerial connection when I realised that the socket on the set had failed at some point, and
the customer had removed it and spliced the cable from
the antenna directly to the cable from the tuner.
This set (like many others) has capacitors built into the
antenna socket to isolate the chassis from the antenna
system. Most televisions of the era had the chassis at half
mains potential. I told the customer to wait to use the television until it was repaired; it was taken back to the workshop and fixed later.
The rest of the antenna system checked out OK, and the
reception was restored once the masthead amplifier had
been replaced.
Don’t overamplify troubleshooting
J. N., of Mt Manganui, New Zealand reminds us that
sometimes looking for faults in the most obvious places
first is the best strategy...
As I am known to take a challenge with regard to repairs,
a friend asked me if I could look at his Fender AmpCan
15W guitar amplifier that kept cutting out intermittently.
I said yes, but no guarantees. After he delivered it, I put it
through its paces with my own guitar and, sure enough,
it was annoyingly intermittent (the worst faults are when
they are intermittently intermittent)!
Firstly, I dismantled the unit and discovered that it
had an internal 12V SLA battery and could also be powered from a suitable charger. The owner lost the charger
and had been trying to run the amplifier from a 15V DC
power supply.
I found and downloaded a copy of its circuit, wiring
diagram and user’s manual. They allowed me to discover
that the charger could charge the battery and power the
unit separately, but not both. The external power passed
through an L7815CV 15V regulator and a diode to the battery, then onto an isolating main switch.
I established that the battery positive terminal was the
point where the power was being lost. I immediately suspected the L7815CV voltage regulator; however, on removing it and bench testing it, it proved good! So the following
diode must be faulty. After isolating the diode, I found it
was not so. Where to now? Re-soldering, of course!
To identify any faulty solder joint, I resoldered each point
separately. And there it was, the last spot after the diode
output from the voltage regulator. It just goes to show that
I could have saved a lot of time by applying the simplest
remedy first!
Luckily, the battery was still usable. I had a used 15V
2.1A battery charger that allowed battery operation. To
ensure safety for the L7815CV, I relocated it onto the large
heatsink for the amplifier, as the original charger rating
was only 400mA.
The owner is very happy with the repair, especially as
he can now use the unit cordless.
SC
siliconchip.com.au
Australia's electronics magazine
March 2024 105
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