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SERVICEMAN’S LOG
The dishwasher that wouldn’t
Dave Thompson
It’s that time of year again when everyone seems to go a little mad. I
know I do! Unfortunately, our dishwasher decided to go a little mad as
well, leading to me calling in the big guns.
It has been playing up for a while and we’ve been doing
the usual things, running commercial cleaners through it
and putting in bowls of vinegar, the sort of fixes suggested
by the internet. The filters are always a good place to start;
this stainless-steel German-branded model we have now
has quite a good system for ease of access and cleaning
the filters.
They were all clean, but I could hear a faint grumbling
sometimes while the machine was doing its thing. Suggestions were made that something had gotten through to the
pump and it was causing problems, but I just couldn’t see
how that was possible given the filter system.
It is, of course, possible we lost an impellor blade or
something else had come loose beyond the filters and was
fouling the pump. Still, I couldn’t see anything in it, and
surely it would be making a much more noticeable noise
if that were the case.
We put up with still having dirty dishes in the morning on the odd wash cycle, but it got progressively worse
over time. This unit is around five years old, and it isn’t
the original dishwasher we put in when we renovated
this house.
That was a Samsung model, using a different type of
technology to the rest of the pack (I’m a sucker for trying
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new things!), yet it really never worked properly. It would
fault often, and I wrote about it at the time, because at
under two years old, it should have performed way better than it did.
I sold that appliance cheaply to a local repair guy who
said he knew what was likely wrong with it and waved
goodbye as he drove away with it on his trailer.
Of course, we took quite a financial hit, but we simply
wanted a machine that worked and cleaned the dishes
without faulting or stopping half-way through a cycle.
This new fancy German one was far better in every respect,
from the clever folding dish-retaining system to the almost
silent operation.
Stealthy silverware scouring
The latter isn’t a huge selling point for me, as we put it
on downstairs overnight, but it is amazing how quiet it is.
The only noise from it usually is the odd water-draining
gurgle – which is, of course, not the dishwasher per se,
but our drainage system, and the beeping when it finishes
a cycle. We’ve been very happy with it, and it does a fantastic job of washing dishes. Until recently.
As I mentioned, I’d heard the odd grumble from it, which
was all the more obvious as it is usually so quiet. It didn’t
seem to make much difference to the operation, though,
and there were no error codes thrown up or any other sign
that something was amiss. The dishes still washed OK, and
everything seemed tickety-boo. But then it wasn’t.
We started noticing that the cutlery, which sits in a sliding tray at the top of the machine, was often not washed
properly. There is no dedicated rotating arm for this tray;
instead, the one under the middle glasses tray must spray
this cutlery tray as well, and it just wasn’t doing it.
We would often also find the pellet undissolved sitting in
the middle tray. It is designed to pop out of the dispenser
and sit in a soap-dish-type tray that doubles as the handle
for pulling the basket out of the machine.
Those rotating arms come off relatively easily, so I
disassembled them and washed them in the sink with
detergent, ensuring all the water holes were clear, and
they were. They seemed very clean and unimpeded, so
if it isn’t them, it must be the pump not delivering the
water properly.
I checked the input water line to make sure it was clear
and flowing properly, which it was. And that’s about the
extent of what I could do. I visited the product’s web page
and downloaded the usual manuals and documentation.
The suggestions for this sort of concern were mostly what
I’d already done.
Australia's electronics magazine
siliconchip.com.au
Items Covered This Month
• Dishwasher repair
• Closing the case on a roller shutter
• Repairing an off-grid water heater
• A faulty leaf blower charger
Dave Thompson runs PC Anytime in Christchurch, NZ.
Website: www.pcanytime.co.nz
Email: dave<at>pcanytime.co.nz
Cartoonist – Louis Decrevel
Website: loueee.com
I wasn’t about to drag it out and take the sides off – that
is beyond my pay grade. I’ve done it before on an older
model dishwasher, but this one is much more intimidating. There was nothing for it but to book one of their techs
to come out and have a look, something we could do easily through the web page.
This is a great feature as it would be a serviceman very
familiar with the brand. I gave a detailed description of the
problem in the web form and all our other details and hit
the ‘send message’ button.
Time to call in the experts
Within a day, a guy called, and we made an appointment
for him to visit just a few days later. I initially thought I
might have to wait for several weeks, so this was a pleasant surprise. He said he knew what the problem likely
was and would bring some parts. Excellent service so far!
As is usual for this type of serviceman, he could only
give us an approximate time between 1pm and 5pm. This
is fine for us because we work from home, but it would be
pretty annoying if I had to take half a day off work just to
wait around for him. I guess that’s just the way it works;
many of the jobs they do, they don’t really know how long
it will take.
This reminds me of that Soviet man who decided he
wanted to buy a Lada. He was told that the waiting list for
the car was long and he would get it exactly three years
from today. He asks, “will it be ready in the morning or the
afternoon?” The salesman is shocked and responds, “It’s in
three years. What difference will it make?” He responds,
“well, the plumber is coming that morning”.
Anyway, to be fair, I get asked this all the time when
someone drops a machine in to me to troubleshoot: how
long will it take? I always ask them, how long is a piece of
string? Unless I know exactly what the problem is (often
I do), I can’t give an accurate time-frame until I get well
into it.
If I don’t know what I’m dealing with, I don’t know how
long it will take. All I can do is call the customer and tell
them once I find the problem, which I usually do anyway,
especially if it is going to cost more. I’ve always operated
with a ‘no surprises’ policy. I don’t just spend hundreds,
then present them with a bill, giving them the option of
what to do and which way to go.
That is, unless I can fix it quickly and inexpensively, in
which case I call them and tell them it is ready. I suppose
people are worried about mounting costs if it is going to
take a while.
As it turned out, he arrived at around 1:30pm after calling
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ahead 30 minutes before to let us know he’d be there then.
Again, good service.
Operating on the patient
When he arrived, he put down some protective blankets on the floor and tried a few cycles on the washer,
which he could cancel at any time, and he confirmed
the pump was the likely culprit. Of course, he did what
I’d done, checking the inflow and outflow and filters. He
then pulled the washer out from under the bench and
onto the groundsheet, and whipped the covers off with
well-practised ease.
It was obvious he knew exactly what he was doing, and
all the while, he kept up informational patter as he went
through it. Just looking at the insides, I was glad I didn’t
try this. It looked hugely complex compared to the one I
pulled apart years ago, with tubes and wires and valves
everywhere.
It was also stuffed with sound-deadening material, with
wires and tubes buried in it, so I really wouldn’t be comfortable tackling a job like that. I guess now we know why
it’s so quiet!
He sat on the floor on the side away from where I was
standing so I couldn’t really see what he was doing, but
he passed me the pump assembly he’d just removed like a
surgeon handing a nurse a freshly removed organ.
The manufacturing quality of this component was
unlike anything I’ve seen in a long time. It looked like a
turbocharger from a car and boasted a hard plastic body
and water connections, but the quality of the plastic and
the moulding was amazing, and I marvelled at the compactness of it.
The guy said it was quite rare for a pump on this particular model to fail after such a relatively short time, so the
company would be replacing all the parts he used on this
repair under warranty, even though technically it was out
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March 2025 95
access some such fasteners, so I completely understood
this guy making his own custom tools.
Anyway, he finally finished installing the bits and bobs
he’d brought with him and plugged the washer back into
the power socket. Everything else was still connected, so
he ran a quick cycle through it and seemed satisfied it was
all working properly. It certainly was much quieter, even
with the sides off; we must have gotten gradually used to
the noisy pump.
He soon had the sides back on and, after a quick clean over
with a rag, had it all looking perfect. He slid it back into the
gap under the sink, ensuring all the hoses and cables were
in the right place and not crimped or kinked. We had some
dishes in the sink, so I loaded it up and put a pellet in it and
set it to do a 60-minute cycle, the usual setting we use it on.
It worked perfectly and I couldn’t hear it at all now! I
guess when something starts grumbling we don’t hear it after
a while and until the problem is resolved, we just consider
it ‘normal’. But of course, it isn’t normal. It’s like a loudly
ticking clock – after a while, we don’t hear it because our
brains just negate the sensory input.
Manufacturer support is worth paying for
the other side of our warranty period. We would only be
liable for this guy’s fee. He also replaced a couple of sensors and valves while he had it apart.
The pump assembly retails for about $500, so I’m glad
they were covering it! I’m not sure what the sensors and
valves would cost, but he said it would be a good idea to
replace them while he had it apart, and they were paying
anyway! Another big tick in the good service box.
It seemed like a relatively tricky job putting it all back
together, if the time taken was anything to go by. As I wrote,
I couldn’t see what he was doing, but he was elbow-deep
in the guts of this machine for quite a while.
Our galley-style kitchen is quite narrow and, with the
machine in the middle of the floor, there was no getting
past it. I could have gone around and come up from the
other way, but I really don’t like people hovering over
me while I work, so I extend the same courtesy to other
servicemen.
I was interested in his tools, though, and had a discussion with him about that while he worked. He was quite
happy to chat. He had what looked like a pretty comprehensive toolkit, and I could see a few special tools he’d accumulated over the years, likely for all the different models
he’d encountered.
While some were supplied by the various manufacturers, others he’d made himself from existing tools. Dad and
I did this for various cars I’ve owned and ended up doing
my own repairs on.
British cars especially had some bolts and nuts in crazy
places, as if they suddenly thought, where is this Fitzer
valve going to fit? I know, we’ll put it behind and under
the engine next to the firewall and make the nuts and bolts
impossible to get to!
We fabricated many special spanners and wrenches to
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We are lucky in that we bought a known, branded appliance, and we did so because the last one had let us down so
thoroughly. The old adage that you get what you pay for is
especially true these days. That said, some of the cheaper
appliances work just as well, but it is always a risk to buy
them given they often have no official after-sales technical support. Instead, you have to rely on some random
service guy who might be able to fix it when it breaks. Or
perhaps not.
I imagine some of the parts for those cheap, big-box store
models would be nigh on impossible to get, unless of course
they use the same parts as some other brand, like some TVs
sold here under other names. Many use the same PCBs as
big-name overseas brands, but finding out which parts are
compatible can take a lot of time and research.
I’ve found online forums very handy for this, as many
service people post in them and I’ve had many questions
answered by the people who frequent those forums. They
tend to share their knowledge freely.
At the end of the day, buying the best we can afford is
usually a good practice, and this appliance illustrates that,
with the company standing behind their gear and supplying parts for them because they know they will wear out
one day. The pump went pretty early, I suppose, but we
run it every night and it has done a lot of work in the time
we’ve had it.
Servicing Stories Wanted
Do you have any good servicing stories that you would like
to share in The Serviceman column in SILICON CHIP? If so,
why not send those stories in to us? It doesn’t matter what
the story is about as long as it’s in some way related to the
electronics or electrical industries, to computers or even to
cars and similar.
We pay for all contributions published but please note that
your material must be original. Send your contribution by
email to: editor<at>siliconchip.com.au
Please be sure to include your full name and address details.
Australia's electronics magazine
siliconchip.com.au
Nothing lasts forever, and with built-in obsolescence
increasing, it is only going to get worse for consumers.
That’s even before you factor in totally unexpected events
like the pandemic, which shut factories down all over the
world and created a huge parts vacuum that has still not
been filled.
It is increasingly difficult for me to get computer parts,
for example, with my traditional suppliers only stocking a
fraction of what I could get from them pre-pandemic. This
has a knock-on effect on customers who might be looking
for a new machine.
While it appears that some stores seem to have an abundance of parts, they could have either bought a container-
load before the pandemic, or have some pretty good contacts in Taiwan and China where they can snap them up
before any of the more traditional suppliers can get their
hands on them. Either way, it makes my business difficult.
Thank goodness for the guy who fixed our dishwasher,
though. He was prompt, professional and claimed that all
parts were available for it. For a 5-year-old appliance, that’s
not bad these days.
It has been going flawlessly since he swapped the pump
out, so that was obviously the problem. He took the old one
away, but I wished I’d taken a photo; it really is a beautifully made item – classic German engineering!
I guess it could be a different story if something goes
wrong with the electronics or the touch-activated control
panel, but I guess we’ll cross that bridge if we come to it.
dropped on the bench top with a noticeable ‘clunk’ noise.
Looking at the top of the PCB, the remote had obviously
been dropped from a fair height, producing enough force
to separate the inductor body from its mounting pins.
This is another example of poor design, with the inductor’s ferrite body being much too heavy for the support provided around its mounting pins, which just disintegrated
when it was dropped.
Could I fix the inductor, would I need to rewind it, or
bite the bullet and source a replacement? Luckily, it was
at least labelled, so at least I knew its value was 470µH.
After a careful (magnified) look, I saw that, luckily, there
were two enamelled copper wire pigtails sticking slightly
out of the bottom of the inductor. So it looked like repairing it was at least theoretically possible.
The repair turned out to be relatively easy. I tinned both
pigtail ends, then carefully positioned the longest pigtail
over its PCB pin and soldered it in place. To minimise the
chance of future separation, I used superglue to hold the
inductor body in place.
I considered using silicone sealant, but it takes a several
hours to provide sufficient mechanical support, whereas
superglue (aided by Zip Kicker for instantaneous hardening) dries immediately, with high mechanical strength. I
then soldered the other pigtail in place and added enough
superglue to provide a really strong mount.
Thinking about what else I could do to stop the inductor
separating from the PCB again, I temporarily reassembled
the case and realised there was no mechanical support on
top of this heavy inductor, so I also glued some high density sponge rubber to the case, which provides the necessary extra mechanical support.
Apart from the unfortunate synergy of poor inductor
design combined with the lack of any support above the
inductor, this remote appears well made. However, these
two design flaws would have been sufficient to have consigned this expensive remote control to being ewaste; just
another example of an expensive item ($140) ruined by the
manufacturer saving 50¢.
I was also surprised at the large capacity of the batteries in
this remote control. They are much larger than usual, with
a four-cell pack of 14500 AA-size lithium-ion rechargeable
cells. That’s quite a massive increase over the single tiny
Repairing a roller shutter remote control
My daughter runs a local primary school canteen. Yesterday, she dropped a largish remote control in my hot little
hand and said that the battery won’t charge and it doesn’t
work. I decided, as I usually do, to remove the four Pozi
driv self-tappers and have a look inside.
Fault diagnosis turned out to be super easy because, as I
prised the two plastic covers apart, a small ferrite inductor
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The opened-up remote control for the school canteen roller
shutter door.
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March 2025 97
coin cell used in car and garage door RF remote controls,
or the two AAA cells in IR remotes.
Happily, my daughter reported the next day that, after
charging the battery, everything was working again, with
no problems feeding her ravenous horde of school kids.
G. C., Cameron Park, NSW.
Joolca HOTTAP V2 repair
My daughter rang and asked if I would help her partner
fix their portable off-grid water heater, which had stopped
working. It connects to a water source and an LPG gas
bottle. There was a digital temperature gauge and controls to set the water and gas flow to adjust the temperature of the hot water outlet. It is powered by two D cells
in a battery box.
We decided to check the batteries and battery box to make
sure the heater had power. The battery box simply unscrews
from the unit, providing access to two terminals that feed
the heater. I measured the voltage at 3.2V, which is fine.
Next, we took off the cover to check for any obvious damage. The heater has an ignition coil, a solenoid to control
the gas flow, a Klixon thermal switch connected to the outlet pipe, a microswitch that looked like it operated when
water flowed through the system and various other components. Nothing seemed to be damaged or loose.
We decided to connect the heater to the garden tap and
see if anything happened. The display did not show any
indication, and nothing else seemed to be working.
Overnight, I visited the Joolca website and found that the
most common fault was flat batteries. I also discovered that
if the Joolca logo on the temperature gauge was pressed, a
fault indication should be displayed.
The next morning, I had another look at the battery box.
I pressed the Joolca logo and there was no indication on
the display, so maybe no power was reaching it. I then
removed the battery holder and measured the voltage as I
had on the previous evening; I got a reading of 1.6V. Obviously, something was wrong with the power. I checked
both batteries, which were about 1.5V each.
The batteries are connected in series by a metal strip
in the battery box lid. When I examined the holder under
my magnifying light, the spring on which the negative of
one cell sat seemed to be loose. I found that if I wriggled
the battery, I could get a voltage reading. So it looked like
the fault was a high resistance in the battery caused by the
loose spring.
I had to cut two plastic tabs to remove the metal strip
from the plastic lid, then clean and re-attach the spring.
When I put it all back together, with the metal strip glued
in place, I measured 3.2V at the terminals and get the display to show a fault code, indicating no flame. So my initial
measurement of the voltage the night before was obviously
a fluke, with momentary good spring contact.
I reinstalled the cover and connected the system to the
garden tap and my LPG bottle. When I allowed water to
flow, I heard the ignition sparking and the gas solenoid operating. The temperature gauge showed water temperature
The top three photos show the Joolca HOTTAP V2 unit and
its faulty battery connector.
►
The bottom-most photo shows the charger used in the leaf
blower, which had the wires shorting each other due to
damaged insulation.
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Australia's electronics magazine
siliconchip.com.au
increasing, so the heater was working. My daughter was
happy to have hot water when next they go camping.
J. W., Hillarys, WA.
Leaf blower charger repair
I bought a Black Eagle leaf blower many years ago on eBay.
Over time, I have repacked both batteries with new 18650
cells, as documented in the Serviceman column of the June
2024 issue (p92; siliconchip.com.au/Article/16294). I also
repaired the charger after the wire broke at the plug end.
I later had to re-solder a wire on the leaf blower’s power
switch, as one of the wires had come off.
The leaf blower is still working well but this morning,
my wife told me that the original charger was not working and the LED was not lighting. First, I plugged it in to
a different outlet to verify that it didn’t work, which was
confirmed by the fact that the LED did not light up.
On closer inspection, I found that the insulation on the
wires next to the cable strain relief was broken and the bare
wires were touching each other. I wondered if the charger
would still work after the output had been short-circuited.
I removed the charging cable, separated the remaining bits
of wire and plugged it in again. The LED lit up green, indicating that it probably still worked.
The next problem was to separate the two case halves;
they were glued together, rather than being screwed. This
is very annoying and makes repair difficult.
I took the charger out to my workshop and got a wood
chisel and hammer. I carefully went along the seam with
light blows, working my way around the entire charger.
This worked without breaking the charger case, and the
two halves separated.
Next, I pulled the remaining cable out of the cable strain
relief and fortunately, it came out without too much trouble. I turned my attention to the circuit board, which had
something that looked like contact adhesive over the wires
where they entered it. Scraping this off with the point of
a knife was successful, so I could desolder the wires from
the board.
I shortened the cable and tried to get it back through the
strain relief, but this proved to be quite difficult. In the end,
I bared around 30mm of the cable end and tinned it. I was
still having problems getting the cable through, but found
that I could do it by separating the wires and feeding them
through one at a time.
I have used superglue to secure the cable to the strain
relief in the past, but I decided not to use it for this repair
in case I needed to fix it again later. So I tied a knot in the
cable to prevent it from pulling out. This might not be ideal,
but I have found quite a few devices with this done from
new, so I did the same.
The circuit board had terminals labelled B+ and B−,
which made it easy to know which was positive and which
was negative. I knew that the plug was wired centre positive, but I double-checked the output of the new charger
just to verify this. Then I used my multimeter on the ohms
range to verify that both wires of the cable were intact and
to identify which was which.
I soldered the wires to the PCB and tested the charger
before gluing the case back together with superglue and
clamping it in the vise until the glue dried. Another successful repair and another item saved from the scrap pile.
B. P., Dundathu, Qld.
SC
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