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SERVICEMAN'S LOG
Variety – the spice of life?
It has been an assorted month with lots of
minor faults. They ranged from a dead garage
door controller to a whistling TV set, a crook
notebook computer and a couple of trouble
some VCRs – including one that bounced.
My first story concerns a Blaupunkt
stereo TV set with a dead remote
control. The main drama with most
remote controls is opening them
without breaking or damaging them.
Most are clipped together but which
way? Is the lower half of the case on
the inside or vice versa? And are the
clips on the outside or the inside?
Having opened this one, I confirmed
a flat battery and cleaned away the
obvious corrosion due to the coffee
(or was it lemonade?) which had been
spilt over the unit and which had
leaked onto the PC board. After that,
I quickly tracked the problem down
to a fracture on the crystal leg.
While I was on a winning streak,
I tackled a Sharp remote control
which wouldn’t select programs 1-14,
although the rest were OK. I suspected that part of the multilayered PC
board had corroded but when I finally
opened it, I found it was remarkably
clean. It was only by chance that,
under a strong light, I caught sight of
a fine 50mm-long crack!
This surprised me, as I was sure that
no-one else had been inside this unit
since it was first manufactured some
eight years ago. What’s more, there
was no indication of any damage to
the outside, yet there it was; a 50mm
crack cutting off the return path to the
IC from these buttons.
Not only that, but the fracture was
not from one edge to the other but in
the middle of the board. I can only
surmise some stress had been applied
to it during manufacture and it had
maintained continuity until just recently. Anyway, the repair was simple
– a little solder over the cracked track
soon had the unit going again.
Garage door controller
My next job was a garage door
opener. The unit in question was a
B&D Controll-A-Door, and the LED on
the remote control transmitter wasn’t
even lighting. Access to the inside
was via just one screw but unlike the
last remote, it was very dirty inside. I
brushed out the dust and cleaned the
board with metho and a toothbrush.
When I tried it again, the LED was
just beginning to glow intermittently.
28 Silicon Chip
I first suspected poor contacts on a
plug that’s fitted to set the frequency
but they proved to be OK.
The problem with small assemblies
like these is holding them steady
while you attach two meter probes and
push a button simultaneously. First, I
determined there was continuity from
the 9V battery to the circuit board, via
the switch. I then checked the board
and crystal for dry joints and fractures.
I tried freezing the parts and noticed
that the intensity of the LED varied
but without pinpointing the cause.
There was an old style .0068pF
styroseal capacitor (a type which has
problems with internal connections)
so I replaced that but to no avail.
Similarly, I made sure that there was
no dirt or shorts between the vanes of
the preset tuning capacitor.
When in doubt, it always a good
idea to check the supply rail to various parts of the circuit. To do this, I
soldered a pigtail to the negative side
of the PC board 9V battery connection
and followed the trail with the positive probe. It didn’t take long to find
the culprit, there being a substantial
voltage drop across the microswitch.
A few squirts of contact cleaner between the cracks of the switch shell
restored its function completely but I
would be a lot happier if I could find
a replacement.
I checked that it was actually
transmitting by listening for noise in
a shortwave radio and it seemed OK.
Most similar remote controllers can
be checked like this but it is better to
use one of the remote checkers available on the market. However, many
of these won’t prove that the correct
waveform or frequency is being produced. They only prove that the unit
is transmitting.
Sanyo colour TV set
My next customer brought in a
Sanyo SS Plus CPP6012-00 TV set (A3A20 chassis series). He described the
fault as what amounted to intermittent
line tearing and rolling but only on
some channels and when the set was
cold. I began to worry when he told
me that another company had tried to
fix it but had given up and suggested
he bring it to me.
I asked him straight out who this
obliging company was and made a
mental note to return the favour. However, they did tell him what a “good
chap” I was and so, with my ego suitably stroked, I took on the challenge.
I began the job by phoning the
other service company to find out
what they had actually tried, so as
not to repeat the exercise and waste
time, effort and money. Their general
consensus was that the problem was
due to the AGC circuits crushing the
sync pulses. A large scale integrated
IC (IC101, LA7680) which contains
all the IF and RF stages (including the
AGC) had already been changed, so it
appeared that a peripheral component
was to blame.
I removed the covers and connected
the set to a colour bar generator. I first
fed the signal in as RF and then via
the AV sockets at the rear. When the
AV input was selected, the picture
was sharp and clear. Conversely, when
the RF input was selected, the fault
was very pronounced when cold but
improved when hot.
As the temperature seemed critical, I tried freezing and heating and
noticed that the fault varied quite
dramatically when I was close to
Q110. This transistor is an NPN power
regulator that supplies 9V to IC101
and to the front end. I measured the
rail to find it a little low at 8.8V but
not unduly so.
A common problem with many
manufacturers is that rail vol
tages
are not always accurately shown on
the circuit. The circuit – if you are
lucky enough to have one – is really
only a guide.
Anyway, I exhausted my investigations around the AGC circuit and on
Sanyo’s advice replaced D801 (1N
4148), which comes off the IF AGC
line, as well as C115 (0.47µF). This
made no difference and so I came back
to the 9V rail.
This rail starts from pin 15 of the
switchmode power supply chopper
transformer as B5 (15V) on the cathode
of D554. It is then switched by Q554
(2SB764) from the remote microprocessor CPU (IC701) and Q792, Q552
and D562, before going through IC551
to become B6, a 12V rail. This 12V is
then applied to the collector of Q110
which produces 9V, courtesy of R110
and D110.
June 1998 29
Serviceman’s Log – continued
All this was working as expected
and there was no unusual noise on
the rails themselves, as shown by the
CRO. I replaced electrolytic capacitor
C117 just in case but was still going
nowhere.
My next step was to connect an
isolated variable power supply to the
emitter of Q110 and chassis. When I
varied the level, the symptoms were
quite obvious below 9V but the set
behaved perfectly at this voltage and
above. The ridiculous thing here is
that we are only talking about 0.2V
but it was enough to make the difference.
Since there are only about five
components in this simple circuit, I
removed and checked each one but
could not fault any of them. Finally, I
replaced them one at a time with new
ones and only when I replaced D110,
a 10V zener diode, did the fault clear.
Now it might appear that this is
what I should have done as soon as I
suspected the 9V rail but the spooky
thing is that when I tested it across
a current limited power supply, the
zener worked out exactly on 10V,
30 Silicon Chip
as indeed did a new one. So I put it
down to a dodgy zener. I don’t have
the luxury of unlimited time to make
exhaustive tests as to why that part
didn’t work properly when cold – it
was enough to track it down.
Anyway, it fixed the problem and
the set was still working when the
owner called to pick it up a week later.
Both he and I were on cloud nine.
Resurrecting Sam
The next customer was a lady who
complained that her Samsung Winner
VB306 VCR was dead. And she was
right. The mains fuse hadn’t actually
failed but to all intents and purposes
nothing was working. Fortunately for
me, I have a service manual for this
model, which was a great help.
I decided to start with the power
supply but quickly discovered that it
is very difficult to access the circuit
anywhere in this machine to measure
voltages. In the end, I removed the
switchmode power supply, removed
its covers and soldered pigtails to
each of the secondary voltage rails,
before plugging it back into the
motherboard.
I soon discovered that the 5V rail
was down to 3.5V. By replacing a
470µF capacitor (C3), the 5V was
restored and the machine began to
operate. However, the panel display
was still non-existent. I delved back
into the power supply to find that the
5.8V rail which goes to the filament of
the fluorescent display was down to
only 1V. Replacing a 100µF capacitor
(C38) fixed that problem but since
two of the electrolytics had failed, I
decided to replace all the secondary
electro
lytics to improve reliability.
The lady agreed and is now happily
reunited with her Winner.
The notebook computer
For a change of scene, the next
customer produced a little notebook computer. It was an early KTX
386SX16 monochrome LCD notebook
and not much was happening that
gave anyone any con
fidence. The
green power LED would come on and
the other LEDs would flicker but there
was no display. Worse still, there
were thumping noises from inside,
probably from the hard disc drive.
In short, it rather seemed as though
it was “cactus”. Still, I volunteered to
look at it, especially as I own the very
same model. I proposed to compare
them and swap parts if necessary, to
find the cause of the problem.
The weakest part of this early
notebook is the 12V battery pack.
These never last long due to problems
of charging and discharging them
properly. In this case, the battery was
missing so I dug out my old KTX and
connected it to his AC power adaptor
so that I could see what was supposed
to happen on boot-up, with regard to
LEDs lighting, etc.
To my surprise, my KTX machine
misbehaved in exactly the same
manner as his. Initially, I suspected
that my computer had also given up
the ghost. Then it slowly dawned on
me that perhaps I was looking at this
the wrong way round – it might not
be the computer that was at fault but
the power supply instead. I couldn’t
wait to dig out my power adaptor and
plug it into the customer’s notebook.
Bingo! – it booted up perfectly.
The AC adaptor supplied with the
KTX notebook uses a generic “Go Forward” GS-30 A-18 switchmode power
supply, designed to deliver 18V at up
to 2A. I rigged up a dummy load of
20Ω and measured the voltage across
the primary input filter capacitor
following the bridge rectifier as 340V,
which is correct. On the secondary
side of the circuit, however, there
was only 9V.
A quick inspection revealed a
number of electrolytics on the output voltage rail that were beginning
to leak. I replaced both 1000µF 35V
capacitors with equivalents but
this didn’t fix the problem. I then
replaced a 100µF 63V unit which restored the voltage completely. I then
reworked the soldering and reassembled everything before returning it to
the owner with a bill that was much
less than expected.
and the voltage varies, according to
the light, on pins 42 and 43 of IC601
on the central processing unit.
These light sensitive devices are
notorious for being intermittent and
so I fitted two new ones. Interestingly,
the replacement PN268 looks like a
clear LED while the original is dark
violet or black. The two pigtails are
designated emitter and collector and
not anode and cathode respectively. These devices can be tested on
an ohmmeter, on the 10x range (or
greater), with the red probe (battery
negative) on the long pigtail and the
black probe on the short one (ie, the
opposite polarity to a LED, which also
conducts on the x1 range).
The last thing to check is that the
chassis return for the mode motor
and the sensor is good. This involves
tightening the screw which connects
the lead to the chassis. It was now all
systems go each and every time.
The bouncing VCR
The next VCR I had to deal with
was Mr Young’s Panasonic NV-J11A,
which had bounced back with a
vengeance. It had come in a few weeks
earlier, the customer complaining
that it gave a rolling pattern with
intermittent noise bars. What was
not noticed by Mr Young at that time
was that there was no counter – or
rather, I should say that the counter
didn’t count.
The cause turned out to be dirt
on the ACE head which prevented
control pulses from reaching the
tracking circuits and the real time
clock. Cleaning fixed that problem.
Complex assembly
The next beast
The next beast to repair was another VCR, this time an overseas
JVC HRD211EM (Middle East Multi
System version). This customer’s
problem was that the video was intermittently not accepting his tapes
properly.
First, I checked the 5V and 12V
rails from the IC regulator (STK5481)
and looked for any lurking brown goo
on the PC boards. So far, everything
was OK. The cassette housing is controlled by light sensors (PN268R-NC)
This time, the complaint was
slightly different; it rolled only at
the beginning of a tape. Inspection
confirmed that the counter was
working but the rolling problem was
intermittent as described. With the
covers off, I could see that the tape
was intermittently spilling due to
poor take-up torque.
A new Play Arm (type VXL1861)
underneath the reel pulley fixed this
but I noticed that there was too much
noise on reverse search and the back
tension arm was not being cleared
from touching the tape. A slight touch
with a pair of long nose pliers bent
the lever closer to the plastic lever
underneath, so that it pulled away
further on review mode.
I was beginning to think I was
jinxed on this repair when I discovered that, though the noise was much
reduced, it was still excessive in the
review mode. When I unsoldered the
heads (VEH0532) and measured their
Q factor (VEH0532), all three read
zero out of six on the video head tester. This meant that the heads were far
too worn and it was amazing that they
were still giving any sort of a picture
(new ones read typically five out of
six and anything better than three for
an old machine is good).
I conveyed the bad news to the customer and understandably, it didn’t
go down too well. However, he agreed
to let me fit new heads. This went off
without any hitches and everything
worked perfectly afterwards. However, I did have to explain to the now
incredulous Mr Young that the first
few seconds of recording on any machine have a slight colour patterning,
as the tape has to go from the bulk
erase head to the ACE head before it
is normalised.
Fig.1: this diagram gives some idea of
the compact nature of Orion 10/VR
combination VCR/TV set. The VCR
“block” sits in the bottom of the
cabinet, with the TV “block” above it.
The next repair was an Orion 10/VR
VCR and TV set combination which
was dead. This repair would have
been quite routine had it not been
for the complex way in which the set
was assembled. The unit had been
dropped and, as a result, the tracking
control was now missing and one of
the feet was broken on the outside.
The major difficulty was coping with
the VCR and TV assemblies on the
inside; there literally was no access
to either.
It wasn’t so bad removing both the
TV and VCR together from the front
June 1998 31
Serviceman’s Log – continued
ble the set – you should have seen the
fun and games I had getting the loose
tracking control sub-assembly back
into the front of the case. I then put
it aside to soak test while it waited
for the PRF-1600-F003 IC protector
to arrive. The set was still working a
week later but the main thing I learnt
from the exercise was to steer clear of
this model unless you have plenty of
time and patience.
Whistling Panasonic
shell. The real problem comes after
that because the TV motherboard is
held in a metal frame above the VCR
(which is in a metal box underneath)
and both are connected together by a
dozen or so leads.
The next drama I found from the
service manual was that the TV set
and VCR had separate mains transformers and bridge recti
f iers but
shared some of the regulators and
secondary power supply rails. It was
all very tortured and maze like.
After a lot of trouble, I discovered
that a 12V rail derived from the VCR
wasn’t reaching the TV set on plug
CP7004. This was eventually traced
to a fuse F7002 3.15AT in the VCR
transformer secondary (T7001).
However, there was still no 11.5V
on TP501 in the TV section, which
was still dead.
Gaining access to the TV circuitry
meant unplugging it from the VCR
and unscrewing it from the metal
frame, after which I was able to perform some continuity tests along the
PC board. Eventually, I found a 3.9Ω
0.5W fusible resistor (ICP501) that
32 Silicon Chip
had gone open circuit. This resistor
was wired in series with a 4.2Ω 18W
resistor (R501) and connected in
parallel with power regulator Q503.
I was rather puzzled by this arrangement on two counts. First,
connecting a 0.5W resistor in series
with one rated at 18W seems rather
strange. Second, the fusible resistor
was in fact marked in the service manual as a PRF-1600-F003 IC protector,
whatever that was (my guess is that
this is a circuit protector chip fuse
rated at 1.6A but it doesn’t appear
in any of my generic parts catalogs).
As a temporary measure, I decided
to fit another 3.9Ω 0.5W resistor while
I waited for the correct replacement
part to ar
rive. Unfortunately, that
didn’t cure the problem – the TV set
was still dead.
It didn’t take long to spot the remaining problem, however. Now that
I had the whole TV section in my hot
little hands, I could see that the drop
had fractured the solder connection
to the horizontal output transformer.
I repaired this and the set came good.
It took quite some time to reassem-
My last repair concerns a Panasonic TC-68A61 68cm stereo TV set
which came in with a loud whistling
vibration from the rear. The owner
had finally decided he just couldn’t
take it any more. With the rear cover
removed, it was obvious that the
noise was coming directly from the
deflection yoke assembly on the neck
of the tube. The question was, what to
do about it. A new yoke (TLY15912F)
would probably be rather expensive
and time-consuming to fit.
The “singing” noise was caused
by the copper wire vibrating against
the ferrite core and the only way to
stop this is by securing the winding
and the ferrite together. I decided that
the cheapest and most effective way
was to use superglue and additional
rubber wedges.
I gingerly emptied the contents of
five tubes of glue so that it flowed
down the wire and hopefully onto
the ferrite. As it happened, this was
quite successful and the first application reduced the noise by 75%.
The remainder was cured by adding
thinner wedges to the ones already
fitted (which align the purity and
dynamic convergence of the yoke).
The aim here was to push the wire
harder onto the ferrite former without
disturbing the settings.
I was relieved when this worked as
I didn’t fancy removing the yoke, sealing it and then realigning everything.
No-one can be as accurate as the
manufacturer in installing modern
TV yokes, many of which are actually
cemented to the tube.
Unfortunately, the cure proved to
be short-lived. After about a week
of soak testing, the glue broke down
under the heat and the whistling returned as bad as ever. So it looks like
the repair will be expensive – that’s if
the owner decides to go ahead with it.
Oh well, you win some, you lose
SC
some!
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